Macon-Bibb County is fighting to block a lawsuit over the safety of a Macon Downtown Airport runway.
In
the suit, filed June 5 in Fulton County, Old Republic Insurance Co.
claims the city of Macon and a contractor ignored federal rules that
would have prevented water from pooling up on the runway. A jet owned by
Dewberry Air hydroplaned in September 2012, sliding off the runway and
across Ocmulgee East Boulevard, crashing into trees.
This is the
second suit filed by Old Republic, which paid out a $1 million as a
result of the crash. The first suit, which had been filed in Bibb
County, was dismissed.
Read more here: http://www.macon.com
NTSB Identification: ERA12FA567
14 CFR Part 91: General Aviation
Accident occurred Tuesday, September 18, 2012 in Macon, GA
Probable Cause Approval Date: 06/23/2014
Aircraft: BEECH 400, registration: N428JD
Injuries: 2 Minor,1 Uninjured.
NTSB
investigators either traveled in support of this investigation or
conducted a significant amount of investigative work without any travel,
and used data obtained from various sources to prepare this aircraft
accident report.
The pilot was seated in the left seat and was
the flying pilot. The pilots reported that prior to departure, there
were no known mechanical malfunctions or abnormalities with the
airplane, including the brakes, flaps, anti-skid, or thrust reversers.
The copilot, who was the pilot monitoring, calculated a Vref speed of
108 knots for the landing weight. Postaccident analysis determined that a
more precise Vref based on weight would have been 110 knots. Both
pilots reported that they set their airspeed index bugs to 108 knots
about 11 miles from the airport.
The pilot reported that the
airplane touched down about 1,000 feet from the approach end of the
runway. Both crewmembers reported that, although they used maximum
thrust reversers, brakes, and ground spoilers, they could feel a
“pulsation” in the brake system and that the airplane hydroplaned. The
airplane overran the wet runway with standing water and came to rest 283
feet beyond the paved portion of the runway in a treed area off the
airport.
Postaccident examination of the airspeed index bugs
revealed that the pilot’s was set to 115 knots and that the copilot’s
was set to 105 knots, which correlated with their calculated and
reported V1 and V2 departure speeds. It is likely that they did not move
the airspeed bugs during the approach to landing. Postaccident testing
of the brake system components did not reveal any mechanical
malfunctions or abnormalities that would have precluded normal
operation.
Based on radar data, the airplane was likely 15 to 19
knots above the reference speed of 110 knots when it crossed the runway
threshold. The data further revealed that the approach was flown with
about a 4-degree glideslope approach angle instead of the recommended
3-degree glideslope angle. The pilots reported that the precision
approach path indicator lights, which would have provided an approximate
3-degree approach, became inoperable shortly after activation. Although
the touchdown location could not be accurately determined, given the
approximate glideslope and the excessive speed, the airplane likely
floated before touching down.
It is also likely that the pilots,
familiar with landing at their home airport, which is configured with a
grooved runway that mitigates wet runway conditions more effectively,
relied on their past wet runway experience and failed to calculate their
landing distance using the appropriate performance chart for the
contaminated runway. Based on the airplane’s performance charts, on a
contaminated runway, an airplane with a Vref of 110 knots would need a
4,800-foot runway; at Vref + 10 knots, the airplane would need 6,100
feet to land. The runway was 4,694 feet long. Hence, the lack of a clear
understanding of the actual wet runway landing distance necessary to
stop and the excessive approach speed resulted in the airplane crossing
the approach end of the runway at a speed and flight profile unsuitable
for the wet runway condition and without sufficient distance available
to stop. Further, the pilots exhibited poor crew resource management by
not using the appropriate chart for the contaminated runway, not
recognizing the runway was too short based on the conditions, failing to
reset their airspeed bugs before the approach, and not recognizing and
addressing the excess approach speed.
The National Transportation Safety Board determines the probable cause(s) of this accident to be:
The
pilot’s failure to maintain proper airspeed, which resulted in the
airplane touching down too fast on the wet runway with inadequate runway
remaining to stop and a subsequent runway overrun. Contributing to the
landing overrun were the flight crewmembers’ failure to correctly use
the appropriate performance chart to calculate the runway required to
stop on a contaminated runway and their general lack of proper crew
resource management.
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