Sunday, March 11, 2012

Chicago, Illinois - Pilot putting region's old airports on the radar

Chicago area's former airfields that provided vital WWII training are subjects of planned book

Nick Selig, 76, is researching a planned book about dozens of the Chicago area's old airports.
 (Keri Wiginton, Chicago Tribune / March 2, 2012)




Jon Hilkevitch: Getting Around

Veteran pilot Nick Selig is flying solo on a mission to salute Chicagoland's ghost airports, the grass airfields carved out of farmland that helped sow the seeds of victory in World War II.

Almost all of the approximately 45 airports are long gone. Some are abandoned while others are buried under the highways, shopping malls and residential subdivisions of suburban Chicago.

They include Elmhurst Airport near Lake Street and state Route 83, which opened in 1927 and thrived until a utility line was erected through the airfield in 1956, followed by Interstate Highway 290; Maywood Field, an airmail field where Charles Lindbergh once landed that is now the home of Hines VA Hospital; and Ravenswood Airport, along Touhy Avenue near Rosemont, which opened in the late 1920s and was among about six muddy airfields close to Orchard Field Airport, which became O'Hare International Airport.

"There was a creek running through the middle of Ravenswood," Selig said. "Two runways went across a bridge over the creek. Pilots had to negotiate that when taking off and landing.

"Unfortunately, it's also where the American Airlines DC-10 crashed in 1979 after taking off from O'Hare."

All 271 people aboard the plane and two on the ground were killed, making it the deadliest air disaster in the U.S. until the9/11terror attacks.

Selig fondly remembers visiting Chicagoland Airport near the village of Half Day, which today is part of Vernon Hills. It was one of 15 airports the Navy built to train pilots during WWII. An old farmhouse on the site served as the airport office.

"I always thought it was unique because it was the only airport I ever saw with a swing for kids to play on," said Selig, adding that the airport operated until the 1970s.

"These little airports, only 20 to 40 acres on average, came to be at any open field around the suburbs," Selig said.

Selig, 76, is a retired O'Hare airplane mechanic who is a part-time flight instructor. He spends time at libraries and historical societies researching the old airfields and the pilots who trained for WWII or who scratched out a living selling rides, lessons and airplanes.

"I hope to record it all in a book for posterity before the participants of the era expire, including me," said Selig, who lives with his wife, Suzette, also a pilot, at Naper Aero, a residential airpark community in Naperville.

He has written 25 of the 45 "ghost airport" stories and is working with a publisher, he said. Some of the tales have come from fellow old pilots he meets when he presents a slide show on the topic to aviation clubs and other groups.

The airfields that the Navy built in the Chicago area during WWII were used to train up to 90 percent of Navy pilots, Selig estimated.

"Very few people know about these suburban airports. What I am trying to put across in my book is that at the beginning of World War II, if it hadn't been for these little dirt and sod airfields to train all the pilots we needed for the war, it might have been a significantly different outcome," he said.

The personalities Selig has come across are a big part of the story he wants to tell.

There was Dick Lloyd, for instance, who in the mid-1940s bought Sky Haven Airport near Bensenville and operated it on land he leased from a railroad until the field closed in 1955.

"Dick Lloyd had a wooden leg. Before we had these sticky Post-it Notes, he used to thumbtack notes to himself on his wooden leg," Selig said.

Another larger-than-life character was Willie Howell, who ran Howell Airport at Cicero Avenue and Route 83 near Crestwood in southern Cook County. The airport closed in 1990, replaced by the Rivercrest Shopping Center.

"If you landed your airplane at this airport, you'd better pay Howell's landing fee because he would run out in his Cadillac car and park in front of your airplane so you couldn't move it," Selig said, quoting Howell's former flight students.

Selig is eager to talk to survivors of this bygone era of aviation. He can be contacted at nickselig35@gmail.com.

Linden, Michigan - Woman who retrained as jet engine mechanic shows 'people can reinvent themselves'

Ryan Garza | MLive
Debbie Monchilov, of Linden, recently graduated with a technical school degree from the Aviation Technology Institute to be a jet engine mechanic.


By Blake Thorne, MLive.com

LINDEN, Michigan -- Debra Monchilov didn't listen to the criticisms surrounding her choice to change career paths.

Criticisms that she was too old to become a jet engine mechanic.

Or too female.

"I always had a passion," said Monchilov, a Linden resident who at age 51 just became a licensed airframe and powerplant technician. She trained at Michigan Institute of Aviation and Technology in Canton.

Completion of the 20-month program means Monchilov can do complex maintenance and upkeep on airplanes, windmills, military drones, even some amusement park rides.

It's a world of opportunity for a former stay-at-home mom and insurance agent who, before this, had no formal engineering or mechanical training and no college credits.

"I had to start from the bottom up," Monchilov said.

Monchilov always had an interest in aviation. She remembers watching planes as a 6-year-old girl and daydreaming about working on them.

She was taking flying lessons at Bishop International Airport a few years ago when she got to talking with a man who worked as a recruiter for Michigan Institute of Aviation and Technology, or MIAT.

So she enrolled. She never missed a day of class. She even had the letters "FLYNHI" -- for "Flyin' High" -- on her license plate.

Soon, Monchilov was learning all the complex electronics and mechanical skills required. She built special equipment used to test circuits. She hung propellers and cleaned jet engines. She even built the tool box she uses.

"It was amazing the stuff they had to learn," said her husband, Ron Monchilov.

The hard work paid off. Last April, she was named the national aviation maintenance technician student of the year by the Aviation Technician Education Council. The honor earned her a trip to Orlando to receive the award and rub elbows with industry leaders.

It was a top honor made more special, considering the field in still mostly dominated by men.

"I was the only girl in the class," she said. "Everybody called me the classroom mom."

It's a title she embraced. She would bring in baked goods for her 20- and 30-something male classmates.

"I only remember two, three girls in the whole school," she said.

It's a growing field. The industry is expecting to add 19,600 jobs through 2018, according to the U.S. Department of Labor.

"This is a hiring machine," Ron Monchilov said of the industry.

"The aviation industry is the new auto industry," he added.

The job offers have been pouring in for Monchilov. Offers from across the country, and here in Michigan, have asked her to work on everything from planes to drones to amusement park rides.

She hasn't taken anything yet. She'd like to stay in the area. Her dreams are to work at Bishop and to work on private planes.

Ron Monchilov said he's very proud of his wife. Her story, he said, shows that there are opportunities out there for people willing to work hard and leave their comfort zone.

"People can reinvent themselves," he said.

Plane Forced Off Runway At Allegheny County Airport (KAGC), Pittsburgh, Pennsylvania


WEST MIFFLIN (KDKA) — The pilot of a small plane was reportedly not hurt in an accident at the Allegheny County Airport Sunday afternoon.

NewsChopper 2 flew over the scene in West Mifflin showing the airplane down in a grassy area.

According to our news partners at the Pittsburgh Post-Gazette, the Piper Archer suffered some nose gear damage when a wind gust caused the airplane to come down.

The Post-Gazette reports that Airport Authority officials said the pilot was practicing landings and takeoffs when the accident happened.

The incident closed the airport for a short time Sunday afternoon, but as the Post-Gazette reports, it reopened at about 3:30 p.m.

Source:  http://pittsburgh.cbslocal.com

Flight triggered warning in cockpit

LATEST: A departing Pacific Blue aircraft triggered a cockpit warning most pilots would not encounter in their entire careers, an expert witness told the Queenstown District Court today.

A 54-year-old pilot, of Papakura, appeared for the sixth day of a defended hearing before Judge Kevin Phillips.

The pilot, who has interim name suppression, has denied operating a Boeing 737 in a careless manner on June 22, 2010, a charge laid by the Civil Aviation Authority.

CAA allege the pilot should not have taken off for Sydney after 5.14pm because Pacific Blue rules stipulated departing aircraft at Queenstown needed at least 30 minutes before civil twilight at 5.45pm.

The aircraft departed at 5.25pm.

Expert witness Colin Glasgow, a former commercial airline pilot, Air New Zealand chief pilot and CAA airline inspector, told the court Queenstown Airport was categorized 'x', the highest of a four-level system, because of the terrain, gusting winds, a narrow runway, the then lack of runway lights and no radar.

Pilots flying in and out of Queenstown were required to undergo specific training, including flying with an examiner.

The departure route was an approved flight path over the Frankton arm, around Deer Park Heights to a reference point between the hill and The Remarkables, after which the aircraft could engage instruments and ascend into cloud.

Visual rules for the initial takeoff segment were designed to enable a pilot to deal with an emergency before the reference point, when there was no going back.

A minimum altitude was specified for the aircraft between Deer Park Hts and The Remarkables, to ensure aircraft could climb safely over the Southern Alps if an engine failed.

"As he was leaving when he did he would not be able to land the aircraft before light faded completely.

"He took away [the return to Queenstown] procedure if a malfunction occurred during this critical stage of flight.''

The aircraft descended slightly after takeoff, triggering an automatic "don't sink'' warning and "cut a corner'' flying around Slope Hill instead of directly overhead, the court was told.

As the craft turned around Deer Park Hts, it banked up to 30-degrees, when normal aircraft banking was typically 15-degrees.

This manoeuvre triggered an automatic cockpit "bank angle'' warning, a scenario that can lead to stalling.

"Pilots will fly an entire career and not hear this warning other than in a simulator.

"Being able to safely navigate terrain and avoid other aircraft depended on the ability to see through the visual segment, he was struggling to do that.''
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The aircraft did not reach minimum altitude between Deer Park and The Remarkables, a manouevre designed to allow enough climbing performance to ascend to more than 9000 feet and clear the Southern Alps.

"Failure to reach altitude created a real risk that an engine failure after [the reference point between Deer Park and The Remarkables] meant he would not have achieved enough altitude to fly over The Alps.

"He only just managed to make 9000 feet with both engines.''

The hearing continues.

Pilot ignored fundamental rule, court told

A Pacific Blue pilot took away the one option that may have saved passengers' lives in the event of an engine failure, a court has been told.

The pilot, who has name suppression, is facing a charge of careless use of a Boeing 737 after he took off from Queenstown on 22 June 2010.

The flight had 70 passengers and crew on board and was bound for Sydney.

A retired Air New Zealand captain has been called as an expert witness by the prosecution.

Colin Glasgow told the Queenstown District Court on Monday that all takeoffs must factor in the worst thing happening at the worst possible time.

Mr Glasgow said the Pacific Blue captain ignored this by taking off after the airline's daylight curfew as he never could have landed back at Queenstown in darkness on one engine.

He said the pilot left himself no other options and put 70 lives at risk and compromised his position to act in an emergency.

Raw Video: Belly Landing


Plane Lands Without Gear At Hollister Municipal Airport (KCVH), California

HOLLISTER, Calif. - A close call for one pilot as he landed at the Hollister Municipal Airport without landing gear.

It happened just after 11:00 AM Sunday at the airport on San Felipe Road.

Hollister Fire Crews say a man made a rocky landing without his gear but managed to not be injured during the process. He was the only one in the plane. 

Allegheny County (KAGC), Pittsburgh, Pennsylvania: Airport reopened after landing accident

The Allegheny County Airport in West Mifflin has reopened after wind pushed a small plane off the runway earlier today.

A Piper Archer airplane was overcome by a gust of wind as the pilot practiced "touch and gos," or landings and take-offs without stopping, around 1:45 p.m., according to JoAnn Jenny, a spokeswoman for the Allegheny County Airport Authority.

The plane was forced back down in mid take-off and was pushed to a grassy area on the side of the runway.

The pilot was uninjured and the plane's nose gear suffered damage.

The West Mifflin Fire Department and the airport operations department responded to the scene. The airport closed after the incident and reopened around 3:30 p.m.

Ice Pilots - No landing Gear


The Turkish pilot was practicing touch-and-go landings in their brand spanking new aircraft and forgot to put the landing gear down.

Piper Arrow has rough landing at Marco Island Airport (KMKY), Florida

Story Created: Mar 11, 2012 at 3:56 PM

MARCO ISLAND, Fla. - The Collier County Sheriff's Office said a small plane experienced rough landing at the Marco Island Executive Airport on Sunday afternoon.

Authorities say the Piper Arrow aircraft arrived at the runway without landing gear.

The pilot was identified as a 66 year old man from New York, who was the only person on board. He was not injured.

The Marco Island airport is temporarily closed while authorities await the National Transportation Safety Board to arrive and begin an investigation.

Bottle thrown at landing helicopter - County Down, Ireland

Sunday March 11 2012

A man has been arrested after a bottle was thrown at a helicopter as it landed in Co Down.

The glass bottle was thrown at the rotor blades of the privately owned aircraft as it touched down in Newcastle.

The helicopter was damaged in the incident, but no-one was injured.

Police said they arrested a man over endangering an aircraft.

Feds: Selfridge wing walker let go too soon, falling to death. Boeing A75N1 Stearman, N49739,and Hughes 269C, N7505B. Accident occurred August 21, 2011 in Mt. Clemens, Michigan

A wing walker who fell to his death in August while attempting an aerial stunt at an air show at Selfridge Air National Guard Base, let go too soon as he tried to transfer from a single engine plane to a helicopter, according to a final report from the National Transportation Safety Board.

Ann Arbor stuntman Todd Green, 48, fell 150 feet to the ground after he attempted to transfer from a Boeing A75N1 Stearman airplane to a Hughes 269C helicopter.

The pilots of the plane and helicopter gave statements to the NTSB and are in the report as part of the investigation of the death of Green, who would have turned 49 on March 2.

The airplane pilot said Green jumped to reach the skid on the helicopter before it was in position and let go of the handle of the airplane. He said Green "did not normally let go of the handle on the airplane until his arm was wrapped around the skid on the helicopter," according to the report released on March 5.

The helicopter pilot said the transfer was to take place after the third pass and that the first two passes went as planned. He said Green let go of the airplane handle and "lunged with both hands for the helicopter skid" before the plane and helicopter were in position. Green attempted to go back to the airplane, but was unable to grab ahold to anything, the helicopter pilot told investigators. The report does not state wind speed as a factor in the accident. The wind was at 13 knots according to the report, which is a moderate breeze.

Green had more than 25 years of experience as a stuntman and was a member of the International Council of Air Shows. His father Eddie "The Grip" Green is in the International Council of Air Shows Foundation Hall of Fame.

On a Facebook page dedicated to his memory, a family member recalled a time when a five-year-old Green climbed through his sister's bedroom window and used a pillowcase to parachute from the roof.

"He was not hurt but we should have know (sic) that life would never be boring with Todd around," the post read.

NTSB Identification: CEN11LA606A
14 CFR Part 91: General Aviation
Accident occurred Sunday, August 21, 2011 in Mt. Clemens, MI
Aircraft: BOEING A75N1(PT17), registration: N49739
Injuries: 1 Fatal,2 Uninjured.

NTSB Identification: CEN11LA606B
14 CFR Part 91: General Aviation
Accident occurred Sunday, August 21, 2011 in Mt. Clemens, MI
Aircraft: SCHWEIZER HUGHES 269C, registration: N7505B
Injuries: 1 Fatal,2 Uninjured.

HISTORY OF FLIGHT
On August 21, 2011, at 1335 eastern daylight time, an attempted aerial transfer of an individual (wing walker) from a Boeing A75N1 Stearman airplane, N49739, to a Hughes 269C helicopter, N7505B, resulted in a fatal injury to the wing walker during an air show performance at Selfridge Air National Guard Base (MTC), Mt. Clemens, Michigan. Neither aircraft was damaged during the accident; nor was either pilot injured. Both aircraft landed normally after the accident. The flight was being conducted under 14 Code of Federal Regulations Part 91 and a Certificate of Waiver issued for the air show. Visual meteorological conditions prevailed for the flight, which was not operated on a flight plan. The local flight originated from RMY about 1315.

Bill Waldock: Aircraft Accident Investigation - Embry-Riddle Prescott Campus College of Aviation


Bill Waldock is a professor of Safety Science at the Embry-Riddle Prescott Campus College of Aviation. He is an expert in Accident Analysis, Aerospace Safety, Aircraft Accident Investigation, Aircraft Accident Survivability, Aircraft Crashworthiness, Aircraft Rescue and Firefighting and Aviation Safety. 

To learn more about our faculty experts visit: news.erau.edu

Beechcraft 76 Duchess N6697L: Accident occurred March 10, 2012 in Rio Linda, California

NTSB Identification: WPR12LA128 

14 CFR Part 91: General Aviation
Accident occurred Saturday, March 10, 2012 in Rio Linda, CA
Aircraft: BEECH 76, registration: N6697L
Injuries: 3 Uninjured.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.


On March 10, 2012, about 1940 Pacific standard time, a Beech 76, N6697L, sustained substantial damage following a dual engine power loss and subsequent forced landing near Rio Linda, California. The airline transport pilot and his two passengers were not injured. The pilot was operating the airplane under the provisions of 14 Code of Federal Regulations Part 91. Night visual meteorological conditions prevailed for the personal cross-country flight, which had originated from Visalia, California, about 1810. A flight plan had not been filed.

The pilot said that he was descending towards his destination when both of the airplane’s engines stopped producing power. He selected a dark space on the ground and performed a forced landing. During the landing the airplane collided with a ditch and a fence. The airplane’s right wing was separated from the fuselage, and the fuselage and left wing were bent and wrinkled.

RIO LINDA (CBS13) – A plane crash-landed Saturday night in Rio Linda but no one was seriously injured.

The incident happened at around 7:30 p.m. in the 6900 block of West 4th Street.

The small two-engine plane was headed to McClellan Airfield when its left engine failed. The right engine then failed, forcing the pilot to land the plane in a field located four miles northwest of the airport, said FAA spokesperson Allen Kenitzer.

The aircraft sustained substantial damage. All three men who were on the plane suffered minor injuries but were able to walk away from the crash.

The plane, a Beech 76 Duchess, was still in the field Sunday, just short distance away from a home where a family was eating dinner Saturday when it went down.

“They got lucky,” said Joseph Delso Sr., who lives in the home near where the plane crashed. “It’s just amazing nobody was hurt. Everybody walked away.”

It’s possible the plane ran out of fuel, but the exact cause of the crash is under investigation.

RIO LINDA, Calif. -- The wreckage of a small plane sat in the yard of a Rio Linda family Sunday after it crashed there Saturday night.

The three men aboard the plane walked away from the crash after narrowly avoiding power lines and landing 120 feet from a home where 40 people were attending a party, said Joseph Delso, whose yard is where the plane crashed.

Delso said the home next door, on the 6000 block of 4th Street -- which belongs to his father-in-law -- is where 40 people were gathered for a party Saturday night when the plane went down. He said the pilot and the other two men aboard the plane appeared to be calm and possibly in shock after the crash. Delso and his family walked them into the home and helped tend to facial cuts and scrapes, which appeared to be the men’s only visible injuries, Delso said.

KCRA-3 could not reach the pilot. Federal Aviation Administration records show the plane is registered to Rajinder Kalar, from Beaverton, Ore.

A spokesman for the National Transportation Safety Board told KCRA-3 on Sunday that the pilot reported that his engines were failing and crashed at about 7:40 p.m. Saturday. Other pilots told KCRA-3 that the failure of both engines would typically indicate a lack of fuel, though investigators could not confirm the exact nature of the problem on Sunday. The NTSB will investigate the accident further once it receives a report from the Federal Aviation Administration, which will send an investigator to the site, according to the NTSB spokesman.

This aircraft went down in a field just outside of Sacramento, CA in Rio Linda at approximately 1930Hrs, March 10, 2012 after both engines failed. There were three souls aboard and all three walked away from the incident.

RIO LINDA - Three men walked away from a plane crash on Saturday night after their aircraft landed in a field near a Rio Linda home.

The small twin engine aircraft, a Beech 76 Duchess, crashed around 7:30 p.m. at the 6900 block of West 4th Street.

"I just don't know how these guys survived. I don't know how they survived," said Adrienne Levy whose home was nearly struck during the incident. The aircraft clipped a telephone pole when it landed, Levy said.


"I think if it hadn't hit that telephone pole it would have come right into our house and we have a full house of people here -- we've got like 10 kids here, so it's pretty scary," said Levy.

FAA spokesperson Allen Kenitzer explains that the aircraft experienced left engine failure followed shortly by right engine failure causing the pilot to force land in a field, 4 miles northwest of its destination.


"All of a sudden I heard a puff and the puff caught my attention," said Joe Delso who was attending the party at Levy's home. "I looked over to the east and I saw a light and I heard wind and all of a sudden I heard a thud," said Delso.

The aircraft was on its way to McClellan Airfield from Visalia, California.

Kenneth Isenhower lives near the crash site and saw the plane coming in as the pilot struggled to find a safe place to land.

"I heard the plane coming overhead and it looked lower than normal and so I come out and look at it and the lights start flickering on the plane and then all of a sudden they go out," said Isenhower.

The three men on board walked away from the crash with minor injuries.

"I know they were extremely thankful and two of them were in pretty big shock -- maybe at shock they're alive," said Levy.

The aircraft sustained substantial damage, according to Kenitzer.

According to the FAA, the registered owner of the aircraft is Rajinder S. Kalar of Oregon.

Read more here:  http://www.news10.net

Sacramento County Sheriff's deputies and Sacramento Metro firefighters responded after a small plane crashed in Rio Linda on Saturday.

The twin engine propeller Beechcraft Duchess crashed in a field off West Fouth Street, less than 7 miles from McClelan Field, and just under 3 miles from the Rio Linda airport.

Investigators believe the three men onboard the aircraft were traveling from Visalia to McClelan Field when both engines failed.

All three men suffered lacerations to their faces. No other injuries were reported.

The Sacramento County Sheriff's Department is investigating. Officials with the NTSB and the FAA are on the way. They will take over the investigation after they arrive.

Watch Video: http://www.kcra.com

A small plane went down Saturday night in Rio Linda because of engine failure, but the pilot and two passengers walked away “virtually uninjured,” said Deputy Jason Ramos, Sacramento County Sheriff’s Department spokesman.

Witnesses reported the crash about 7:30 p.m. as the plane dropped over the semi-rural area. The pilot managed to guide the twin-engine fixed-wing aircraft to a field between houses on large lots in the 6900 block of West Fourth Street, Ramos said. The plane landed hard, but there was no fire, authorities said.

Sheriff’s deputies and firefighters from the Sacramento Metropolitan Fire District officials responded to the scene.

Saturday, March 10, 2012

Student pilot forced to make emergency landing

Student pilot Arnaud Kebaili had his training put to the test Friday afternoon when he experienced trouble with the Cessna plane he was flying and had to make an emergency landing in a field off of Midway Road.
Journal-Courier / Maria Nagle

“It’s not every day that you get a plane landing in your field,” Eric Lakin said as he looked across his landlord’s tilled field to where a Cessna 152 sat intact after making an emergency landing.

Student pilot Arnaud Kebaili managed to land the single-engine, two-seater plane safely just before 2 p.m. Friday in Marie Jackson’s bean field off of Midway Road west of Murrayville.

“I had a loss of power and the engine wasn’t running properly,” said Kebaili, 21, of St. Charles, Mo. “I had to land somewhere other than Jacksonville because I just couldn’t make it there.”

Arnaud was en route to the Jacksonville Municipal Airport.

“It was just a destination I picked. I was suppose to do a touch-and-go there and head back to St. Charles,” Kebaili said.

Kebaili had rented the plane from St. Charles Flying Service to log the 100 nautical-mile round trip toward the required flight training he needs to get a commercial pilot’s license.

“That was one of my lessons,” Kebaili said. “I’m a student pilot. I only have 28 hours on my log book. It was my fourth solo cross-country flight.”

Before taking off, he had checked the fuel level and the plane’s mechanicals and everything was all right, he said.

“Right now, I couldn’t say what happened,” Kebaili said. “I wasn’t very happy in the air when I saw the engine shutting off.”

Just as his instructor had taught him, Kebaili put the plane in glide speed, put down the flaps and took measures to make a soft field landing, he said.

“And it worked,” Kebaili said. “Everything went good. As you can see, the airplane had no damage. That’s a good point.”

A Federal Aviation Administration representative and owner of the plane were coming to the site, Morgan County Deputy Tom Keegan said.

“When they get clearance from the FAA and get it running they probably can take off here,” Keegan said. “If not, they will probably have to dismantle it and take it back to St. Charles on a trailer.”

Friday, March 9, 2012

Further trouble for Manx2 as gear collapsed, runway excursion: Linksair British Aerospace Jetstream 3102, G-CCPW, Flight NM-309. Isle of Man (UK)


An airplane operated on behalf of the same company involved in the fatal crash at Cork Airport last year, crash landed on the Isle of Man on Thursday.

Links Air flight NM-309 was arriving at Ronaldsway Airport on the Isle of Man from Leeds when it veered off the runway into the grass after the right main landing gear apparently collapsed.

There were 12 passengers and 2 crew on board the British Aerospace Jetstream 3102 turboprop aircraft, however no-one was injured. The aircraft sustained substantial damage.

It is also understood that it took fire crews almost five minutes to respond the incident, which was not immediately spotted by air traffic controllers.

It has been reported that it was the crew of another aircraft which reported the incident to the tower.

The incident is currently under investigation by British authorities.

Manx2, a virtual commuter airline, sells flights from the Isle of Man to a number of British airports.

Three airlines, VanAir Europe, FLM Aviation and Links Air, currently operate flights on behalf of Manx2.

In a statement, Manx2 said: "A Jetstream 31 aircraft operated by Links Air, on behalf of Manx2.com, suffered a problem with the right-hand undercarriage after landing."

The company confirmed that engineers from Links Air are also investigating the incident.

One passenger said on Twitter: "My Manx2 plane just crashed landing in Isle of Man. We all walked off OK." The tweeter, named Richard Wild, also posted photos of the evacuation.

On Feb 10 last year, Manx2 flight NM-7100 from Belfast to Cork, operated by Barcelona-based Flightline, crashed in low visibility at Cork Airport killing six people, including both pilots.

The plane had made three attempts to land in dense fog when it flipped over on its back and burst into flames on the third attempt.

Two weeks after the tragedy, Manx2 announced that it was ceasing operations on the Belfast to Cork route.

The Air Accident Investigation Unit of the Department of Transport is continuing its probe of the Cork crash, but confirmed in an interim report last month that an anomaly was found with an engine sensor. 

Poland report shows Smolensk plane crash avoidable

The Smolensk-bound passenger jet that crashed on April 10, 2010, killing Polish President Lech Kaczynski and 88 other top officials, should never have taken off that day because the destination was not on Poland's register of approved airfields, according to a 70-page report from the Polish Supreme Audit Office presented in the Sejm on Friday.

No inspection of the Smolensk-Severny airfield was carried out prior to the flight, as required by established procedures. That inspection would have found the airfield inadequate and prompted a decision to transport the president to Smolensk by helicopter from the nearest suitable airport, the report says.

The report identifies numerous violations in the organization of flights for top Polish officials throughout the entire 2005-2010 period. Indeed, the report gives failing grades to all the government bodies concerned with the flights.

All ninety-six people on board the April 10 flight to Smolensk for the 70th anniversary of the WWII Katyn massacre perished when the Russian-built Tu-154 crashed in poor weather conditions.

http://english.ruvr.ru

Plane crash at Deadman's Cay Airport in Long Island, Bahamas


Reports have reached The Tribune of an airplane crash at Deadman's Cay Airport in Long Island. Problems with the landing gear of a Southern Air plane, flying from Nassau, caused the crash, which has left the plane in the bush at the end of the runway. There are no reported injuries.

Air controller involved in 2nd potential collision

By JOAN LOWY, Associated Press 

WASHINGTON (AP) — An air traffic controller who nearly caused a midair collision last year has again been relieved of duty after putting two planes on converging courses. The case raises questions about whether employee rights are trumping safety at the Federal Aviation Administration.

Shortly after beginning the 7 p.m. work shift at the FAA radar facility at Gulfport-Biloxi International Airport in Mississippi on Feb. 29, controller Robert Beck ordered an Air Force C-130 transport jet to increase its altitude from 2,000 feet to 3,000 feet and to adjust its heading. That put the jet on a converging course with a twin-engine turboprop owned by the Department of Homeland Security, according to an FAA employee with knowledge of the incident.

The controller whom Beck had relieved was standing in the back of the radar room while taking a break. He noticed the mistake and alerted Beck so he was able to separate the planes, avoiding a possible collision, said the employee with knowledge of the incident. The planes were just north of Gulfport at the time.

The employee wasn't authorized to speak publicly and commented only on condition of not being named. An FAA report on the incident, released Friday in response to an Associated Press request under the Freedom of Information Act, confirms most of the details, although it doesn't name the controller involved.

An FAA analysis of radar data shows the planes came within 2.59 miles laterally and 300 feet vertically of each other. Regulations require a minimum separation distance between planes of three miles laterally and 1,000 feet vertically.

Air traffic was light at the time, leaving Beck — who has a history of disciplinary problems — with no planes to handle except the two that he put on a converging course, the employee said.

Beck didn't return a telephone call from the AP. The FAA report said the controller who made the error initially thought he'd been told the planes were at the same altitude, which is why he told the Air Force jet to go up to 3,000 feet.

The controller has been removed from directing air traffic and is "currently assigned to administrative duties while the FAA evaluates the individual's future status with the agency," the FAA said in a statement.

FAA officials are "committed to ensuring the safety of our nation's airspace for the traveling public, and we take seriously and investigate all reported infractions," the statement said. "We are working with (the National Air Traffic Controllers Association) to implement a professional standards pilot program that will help improve performance levels and conduct among employees."

Ralph Humphrey, Beck's former boss, said he tried repeatedly last year to get the controller fired, but FAA officials in Washington ignored his requests.

"It's typical of trying to get rid of problem employees" at FAA, said Humphrey, who was the air traffic manager in Gulfport until he retired in January. "It is damn difficult to get rid of an employee for cause."

One reason is that union officials exploit complex employee protection rules even when controllers are unfit, Humphrey said.

Efforts to obtain comment from the controllers association were not immediately successful.

A mistake by Beck last June caused a regional airliner and a small plane to come within 300 feet of colliding with each other, the National Transportation Safety Board said in a report released in January. Investigators were told Beck had "a history of professional deficiencies that included taking shortcuts with phraseology and not complying with standard checklist procedures." He has been suspended several times within the last five years for tardiness, absenteeism and failure to report an arrest for driving under the influence, the report said.

Beck, a 23-year veteran, was ultimately disciplined by the FAA and required to receive professional re-training but only because he didn't disclose the June incident at the time it occurred, Humphrey said. It was only recently that Beck had been allowed to direct air traffic without another controller sitting beside him to catch any errors, the former manager said.

Bill Voss, president and CEO of the Flight Safety Foundation in Alexandria, Va., said Beck's case underscores a larger problem of FAA's difficulty of firing employees who are safety risks.

"It should never be easy to fire a person at any company, but when an FAA manager has legitimate concerns about safety there needs to be a streamlined process where they can work with the union in order to take timely action," Voss said.

FAA officials should put "a safety valve" in their contract so that managers can "pull a flag that says this isn't a normal situation, this is a safety problem," he said.

The FAA has recently introduced a new system for reporting mistakes that encourages controllers to disclose their errors. In return, the agency has agreed not to punish controllers as long as the mistakes aren't due to negligence.

However, David Conley, the president of the professional association that represents FAA managers, testified before a House committee last year that the new system is preventing managers from "using their experience and intuition to coach, mentor and train controllers toward correcting deficiencies."

The purpose of the new reporting program is to gain more information on errors so that safety trends can be analyzed and problems spotted ahead of time.

 http://www.npr.org

Cessna 320D, N320KP: Slow airspeed blamed in plane crash that killed Navy pilot, daughters. Accident occurred May 22, 2009 at Fallon Municipal Airport (FLX), Nevada

An enduring mystery will enshroud the May 22, 2009, plane crash that killed veteran Navy aviator Lt. Commander Luther H. Hook III and his three daughters.

In a long-awaited final report, federal investigators this week concluded Hook's plane crashed because it fatally slowed while landing amidst stiff winds at Fallon, Nev. The precise reason why, though, remains unknown.

"The pilot's inadequate airspeed...resulted in an aerodynamic stall," the National Transportation Safety Board concluded in a final report officially adopted Thursday.

Clovis, Calif., residents Kaitlyn Elizabeth Hook, 15, Rachel Katherine Hook, 12, and Mackenzie Elena Hook, 9, died in the Memorial Day weekend crash, along with the 44-year-old pilot.

The nearly three-year investigation lasted longer than most safety board probes into fatal aviation accidents, which more typically take 18 months to two years. The final report on a fatal plane crash in New Mexico that killed two on the same day as the Fallon accident, for instance, was wrapped up last June.

Despite the extended time, investigators couldn't pin down exactly how it was that one of the Navy's high-speed fighter pilots allowed his civilian plane to stall. The probable cause report made final this week simply noted the available evidence "could be consistent" with a stall and subsequent loss of control.

Investigators, moreover, avoided loaded terms such as "error" or "mistake" in their final report.

"No anomalies or other conditions were found with either engine that would have precluded normal operation," the safety board added.

Hook's fellow Navy aviators, who called him by the nickname "Meat," knew him as someone supremely prepared to handle flight risk.

A 1986 Naval Academy graduate, Hook was serving as the executive officer of Naval Air Station Fallon at the time of the accident. He had accumulated more than 3,235 hours of flight time, many of them in the Navy's screamingly fast F/A-18 Hornet, which can approach twice the speed of sound.

During his career, Hook had served at Naval Air Station Lemoore in the San Joaquin Valley and had deployed on four different aircraft carriers. He had been awarded, among other decorations, the Air Medal for his combat service in Iraq.

On the day of the accident, he had flown his twin-engine Cessna 320 from Nevada to pick up his daughters from Clovis, where they lived with their mother, Brenda Hook, and stepfather, Pat Doles. Hook was living in Fallon at the time with his second wife, Wende, and their two young daughters.

Hook and his daughters took off from Fresno Yosemite International Airport about 6:30 p.m. About an hour later, investigators found, he radioed ground controllers that he had Fallon Municipal Airport in sight. Winds were blowing about 25 knots with gusts up to about 36 knots, which is enough to make trees sway

"He was flying in a good, controlled manner, and I was thinking how much fun it would be to fly one of them," one witness, Fallon resident Hal David Boehm, told investigators.

Witnesses told investigators that they saw the plane make a right turn to establish a downwind approach, then they saw it make a sharp left turn and descend out of sight.

"(I saw) a huge amount of black smoke, and I notified two daughters at my residence to get medical equipment...and call 911," Fallon resident Louis Madraso told investigators.

NTSB Identification: WPR09FA258
14 CFR Part 91: General Aviation
Accident occurred Friday, May 22, 2009 in Fallon, NV
Probable Cause Approval Date: 03/08/2012
Aircraft: CESSNA 320D, registration: N320KP
Injuries: 4 Fatal.

Witnesses reported seeing the airplane approach the airport from the southwest and cross near mid-field to enter the left traffic pattern for landing. Witnesses observed the airplane make a right 270-degree turn to enter on the downwind and, after becoming established on the downwind, make a sharp left turn and descend out of sight near a point consistent with a turn to a close-in base leg. Witnesses then reported seeing a fireball erupt in the area of the accident site. On the downwind leg, at a radar-recorded ground speed of 93 to 106 knots, the airplane's indicated airspeed could have been between 71 and 81 knots, which is in the range of potential stall speeds. Ground scar and wreckage signatures were consistent with a nose-low and left-wing-low ground impact. The witness observations and the impact attitude could be consistent with a stall and loss of control. No anomalies or other conditions were found with either engine that would have precluded normal operation.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot’s inadequate airspeed, which resulted in an aerodynamic stall.


Champion 7KCAB, N5101X: Metal fatigue caused plane’s landing accident. Accident occurred November 27, 2010 in Rialto, California

Metal fatigue caused a plane's landing gear to collapse shortly after the pilot touched down during a practice flight nearly 1-1/2 years ago at Rialto Municipal Airport, federal crash investigators say.

The two-seat Citabria skidded off the runway and hit a taxiway sign, damaging the plane’s fuselage and left wing during the 10:30 a.m. accident on Nov. 27, 2010. No one was hurt.

Pilot Dustin P. Slater, of Mount Baldy, and instructor pilot Ronald A. Meyer, of San Dimas, had taken off an hour earlier from Cable Airport in Upland and made four practice landings at Rialto, according to National Transportation Safety Board records.

With Slater at the controls, the plane had just touched down for the fifth landing when the left landing gear snapped off the aircraft, Meyer said in a written statement to investigators. Efforts were made to keep the airplane level on its right wheel and tail wheel until the speed decreased and the plane skidded to a stop in a left-hand arc.

The NTSB’s final report on the accident was released Thursday.

NTSB Identification: WPR11LA063
14 CFR Part 91: General Aviation
Accident occurred Saturday, November 27, 2010 in Rialto, CA
Probable Cause Approval Date: 03/08/2012
Aircraft: CHAMPION 7KCAB, registration: N5101X
Injuries: 2 Uninjured.

The certified flight instructor stated that he and the pilot receiving instruction were practicing landings in the tailwheel-equipped airplane. He said that during a wheel landing, with the pilot receiving instruction manipulating the flight controls, the airplane's left main landing gear collapsed, and the airplane skidded to the left and contacted a taxiway sign. The instructor reported that the wind was calm at the time of the accident. Postaccident metallurgical examination revealed that the left landing gear fractured at its inboard end due to fatigue cracking and corrosion damage.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
Fatigue cracking of the left main landing gear leg, which resulted in a gear collapse during landing.

Fleet of fighter aircraft remain grounded


New Delhi: The fleet of frontline Mirage 2000 fighter aircraft remained grounded on Friday for the fifth day as investigations went on into the two air crashes that occurred within a gap of 11 days.

Two whole fleet of 49 Mirage 2000 aircraft was grounded for preliminary checks after the two crashes of which the first took place on February 24 and the second on March 5.

The aircraft did not fly even today. The investigations by an expert team are going on, IAF officials said here.

The Mirage 2000 has a very good flight safety record as only six of them have crashed since their induction in operational service in the mid 1980s.

The first aircraft crashed while it was being flown by Air Officer Personnel (AOP) Air Marshal Anil Chopra a few minutes after it took off from its home base in Gwalior.

The first aircraft had crashed due to technical snags in the engine and the reasons for it are being ascertained, they said.

The IAF is worried over the occurrence of these problems in the aircraft after over two and a half decades.

The IAF has also recently signed two deals worth over USD 3.2 billion for upgrading the capabilities of the Mirage 2000 with French companies Dassault, Thales and MBDA.

Dassault was recently awarded the contract for supplying 126 Rafale aircraft to the IAF. 

Cirrus SR-22, N544SR: Wreckage from plane crash sent offsite for inquest: NTSB reviewing several facets of deadly flight.. Melbourne, Florida

NTSB Identification: ERA12FA196
14 CFR Part 91: General Aviation
Accident occurred Wednesday, February 29, 2012 in Melbourne, FL
Aircraft: CIRRUS DESIGN CORP SR22, registration: N544SR
Injuries: 3 Fatal.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

On February 29, 2012, about 1701 eastern daylight time, a Cirrus SR22, N544SR, was substantially damaged when it collided with terrain following an uncontrolled descent while maneuvering for landing at the Melbourne International Airport (MLB), Melbourne, Florida. The certificated private pilot and two passengers were fatally injured. Visual meteorological conditions prevailed, and no flight plan was filed for the local personal flight, which was conducted under the provisions of Title 14 Code of Federal Regulations Part 91.

Review of preliminary air traffic control information revealed that there were several airplanes and a helicopter in the traffic pattern at MLB, performing simultaneous operations to parallel runways, around the time of the accident. About 1658, the accident pilot contacted the MLB air traffic control tower (ATCT) from a position 5 miles south of the airport, and requested a full-stop landing. The pilot was instructed to report when the airplane was on the downwind leg of the traffic pattern for runway 9 Right (9R). Shortly after, a Cirrus SR20, which was on an approximate 5-mile final approach for runway 9R, was cleared for a touch-and-go landing. Approximately 1659, the ATCT advised the accident pilot that he would be required to extend the downwind leg for the Cirrus on final approach. The accident pilot requested a long landing on runway 9R in order to reduce taxi time to the fixed-base operator (FBO), and the ATCT cleared the accident airplane for landing on runway 9R.

At 1700:50, the ATCT radioed the accident pilot to confirm that he had visual contact with the Cirrus SR20 on a one-mile final for runway 9R. The accident pilot replied that he was on a “real short base” for runway 9R. The ATCT then instructed the accident pilot to “cut it in tight” to runway 9R. Several witnesses described the airplane as it entered a steep bank, followed by a vertical, uncontrolled descent. The airplane disappeared from view into wooded terrain short of runway 9R.

The airplane was examined at the accident site and all major components were accounted for at the scene. An odor of fuel was present at the site. The wreckage closely surrounded the initial impact crater. The engine compartment, firewall, instrument panel, cockpit, and cabin areas were all destroyed by impact. The empennage and tail section remained largely intact. Control cable continuity was established from the flight control surfaces in the tail to the cockpit area. Control cable continuity could not be established to the control surfaces in the wings due to multiple cable breaks; however, all cable breaks displayed signatures consistent with overload failure. The three-bladed propeller was buried in the crater, and separated from the engine. One blade was found separated, and two blades remained in the hub. All three blades displayed similar aft bending, leading edge gouging, polishing, and chordwise scratching.

The Cirrus Airframe Parachute System (CAPS) parachute was found deployed, and entangled in the wreckage. Witness statements, and the location of the CAPS components were consistent with a low-altitude deployment.

An Avidyne Primary Flight Display (PFD),Multifunction Flight Display (MFD), and the airplane's Electronic Ground Proximity Warning System (EGPWS) were recovered from the wreckage and forwarded to the NTSB Recorders Laboratory in Washington, DC.

The 1653 recorded weather observation at MLB included wind from 140 degrees at 14 knots gusting to 20 knots, clear skies, 10 miles of visibility, temperature 24 degrees C, dew point 20 degrees C, and an altimeter setting of 30.11 inches of mercury.


Remnants of the airplane that crashed at Melbourne International Airport last week have been moved to a hangar in Flagler County as the investigation into the accident continues. Three Brevard County men died in the crash.

A memorial service is scheduled Saturday for Robert Kurrus, Jr., 44, who was killed in the Feb. 29 crash. Kurrus founded Melbourne’s Premiere Theaters Oaks Stadium 10. Also killed were two of the theater’s managers, James Franklin, 24, and Justin Gaines, 25, both of Palm Bay.

An initial investigation indicates the plane crashed while attempting to avoid a collision with another plane attempting to land on the same runway.

The National Transportation Safety Board concluded its on-site investigation last weekend. Remnants of the plane, a Cirrus SR22, were moved this week to a hangar in Flagler County by the plane manufacturer’s insurance agency, airport officials said.

Brian Rayner, lead NTSB investigator, said it could take a year to determine what led to the crash, but said several areas of the flight are being reviewed — from the plane’s components to weather conditions to radio communications between the air-traffic tower and the pilot. It still remains a mystery who was piloting the plane, airport officials said. “It’s undeterminable,” airport spokesperson Lori Booker said.

In the past several days, insurance representatives from the plane manufacturer and engine manufacturer visited the crash site, which is in an area on the northwest side of airport property that’s so thick with vegetation rescue personnel had to plow a path to get to the downed plane.

Booker said members of the American Red Cross worked with airport staff to “bring solace and understanding to those among us hardest hit by the realities of this incident.” She said debriefings are also being planned with agencies that were involved with rescue attempts, including Melbourne police and fire officials, Brevard County Fire-Rescue and other area agencies. During a press conference, NTSB officials commended airport workers and the community rescuers for their response efforts.

“It’s usual for them to get together and have a debriefing — ‘What did we learn? Did our systems work well? What do we need to adjust?” Booker said. That debriefing has not yet been scheduled, she said.

Services for Kurrus, president of the National Association of Theater Owners of Florida, are scheduled for 1 p.m. Saturday at Calvary Chapel, 2955 Minton Road, West Melbourne. In lieu of flowers, Kurrus’ family requests donations to funds established at BB&T for the families of Gaines and Franklin.

Funeral services for Gaines are scheduled for 10 a.m. today in Frankfort, Ky.

Services for Franklin have not been announced.


Cirrus SR-22, N444VR: Accident occurred March 09, 2012 in Homestead, Florida

NTSB Identification: ERA12LA219 
 14 CFR Part 91: General Aviation
Accident occurred Friday, March 09, 2012 in Homestead, FL
Aircraft: CIRRUS DESIGN CORP SR22, registration: N444VR
Injuries: 3 Uninjured.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.


On March 9, 2012, about 1034 eastern standard time, a Cirrus SR22, N444VR, was substantially damaged during a forced landing near Homestead, Florida. The certificated flight instructor, private pilot, and passenger, were not injured. Day visual meteorological conditions prevailed, and an IFR flight plan was filed for the instructional flight conducted under 14 Code of Federal Regulations Part 91, which departed Opa-Locka Executive Airport (OPF), Miami Florida, destined for Key West International Airport (EYW), Key West, Florida.

According to the flight instructor, prior to departure from OPF he had the fuel tanks filled to capacity and he added oil to the engine to bring it up to 5 quarts.

They departed to the east from OPF at approximately 1000, and were given the MIAMI ONE DEPARTURE, MNATE TRANSITION (MIA1.MNATE) then direct to EYW. During the departure they were eventually cleared to 6,000 feet above mean sea level (msl). Once they were leveled off and in the approximate vicinity of Ocean Reef Club Airport (07FA), Key Largo, Florida, the engine incurred a loss of power. The flight instructor believed however that at the time, the engine was still producing partial power. He then established best glide speed and turned towards 07FA, while the private pilot declared an emergency with Miami Air Traffic Control Center. They "quickly went through the troubleshoot checklist" but could not regain engine power. The airplane was now descending through 4,000 feet msl. The flight instructor then realized that there was a 20 knot headwind and that they were approximately 10 nautical miles from 07FA and were descending at 1,000 feet per minute. He realized that they would not be able to make the airport, so he turned to the left to take advantage of the tailwind and headed for US Highway 1.

He could not recall the exact altitude but as they got lower, he noticed the amount of cars that were on the highway and decided that the risk was too great to attempt to land on it. At approximately 2,000 feet msl, they considered deploying the installed Cirrus Aircraft Parachute System (CAPS) but noticed a light colored patch of ground which appeared to be a hard dirt surface which landing on, seemed to be a better option than deploying the CAPS.

During the final approach while in ground effect the flight instructor then observed a mound of dirt that was directly in front of him and deployed 50 percent wing flaps to "balloon" the airplane over the obstacle. He then heard the stall warning horn, and the wheels touched down on water "like a soft seaplane landing" and slid over a long mound of dirt. The flight instructor then kept the control wheel all the way back and held it till the airplane came to rest in a water filled marshy area.

Post accident examination by a Federal Aviation Administration (FAA) inspector revealed that the landing gear was separated from its mounting location, and the horizontal stabilizer, elevators, wing leading edges, flaps, boarding steps, and fuselage exhibited differing degrees of damage.

According to FAA records, the flight instructor held a commercial pilot certificate with ratings for airplane single-engine land, airplane single-engine sea, airplane multi-engine land, and instrument airplane. His most recent FAA first-class medical certificate was issued on August 7, 2009. On that date, he reported 1,200 hours of total flight experience.

The private pilot held a certificate with ratings for airplane single-engine land, and instrument airplane. His most recent FAA third-class medical certificate was issued on July 27, 2009. On that date, he reported 360 hours of total flight experience.

According to FAA and airplane maintenance records, the airplane was manufactured in 2003. At the time of accident, the airplane had accrued approximately 2,978.1 total hours of operation.

The recorded weather at Homestead Air Reserve Base (KHST), Homestead, Florida, approximately 10 nautical miles northwest of the accident site, at 1455, included: wind 110 degrees at 12 knots gusting to 15 knots, visibility 10 miles, sky clear, temperature 26 degrees C, dew point 20 degrees C, and an altimeter setting of 30.20 inches of mercury.

The airplane was retained by the NTSB for further examination.



A single-engine plane crashed into shallow waters 10 miles away from the Homestead Airport early Friday morning, but the two people aboard weren't injured, authorities said.

The Federal Aviation Administration said the plane was registered to a Weston-based company called Florida Limited Liability Company.

The plane had departed from Opa-Locka Airport and was headed to Key West, said FAA spokeswoman Kathleen Bergen.

It crashed around U.S. 1 and Mile Marker 119.

Aerial footage showed traffic backed up on U.S.1 and emergency personnel and firetrucks lined along the highway.

FLORIDA CITY  – A small plane made an emergency landing south of Florida City Friday morning. Initial reports said the plane came down in shallow water near MM 119 on US1, and that those aboard are unhurt.

The plane is reported by be a Cirrus SR22 single engine plane, registered to a Weston address. Miami-Dade Fire Rescue has been sent to the scene.

Preliminary information said two people were aboard the plane, and both were able to exit unhurt.

There is no immediate information about what caused the emergency landing or who was aboard.

http://flightaware.com/live/flight/N444VR

http://registry.faa.gov/N444VR

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