Wednesday, January 21, 2015

Letter: General Aviation Helps Alaska's Farms and Businesses Take Off

Cordova Times

By Mike Williams


Mike Williams is the managing partner of Alaska Peony Distributors, LLC and a member of the Alliance for Aviation Across America.


Alaska is known for many things, the vast array of wildlife, breathtaking vistas, hunting, fishing and other recreational activities. But many people may not think of the peony flower when they think of Alaska. The truth is that the peony is a highly sought after commercial flower with a very limited growing season. Peony flowers require highly specific environmental conditions and Alaska is the only region in the world that is currently producing peonies between the months of July and September, a time when many of these flowers are sought for weddings. This has given Alaska a unique advantage and the industry is expanding on a daily basis.

My company, Alaska Peony Distributors, LLC provides post-harvest services including processing, marketing, sales, transportation and storage services to the growing peony industry here in Alaska. We have a distribution network that supports 25 plus farms and covers a service area of over 7300 square miles. These farms are spread far apart and they often have little to no roadway access. In fact, according to the Alaska Department of Transportation & Public Facilities, roughly 82% of Alaska's communities are inaccessible by road. The highway system in Alaska is also limited, and the added hurdles of summer tourist traffic and weather can make our trips an all day endeavor.

For our work, a trip that could take 10 hours by truck can be accomplished in under an hour with the use of air transportation. Fast response times are vital in this industry. When a farm has reached cooler capacity for its current harvest, we can send a twin-engine Piper Navajo or any other suitable airplane to immediately transport the flowers to our refrigerated processing facility near Wasilla Airport. This process allows the farming, shipping and storage process to operate at maximum efficiency during the growing season.

General aviation gives us the potential to expand peony farming to far flung locations like Bethal, Dillingham, Kodiak, Copper River Valley or any other Alaskan location with a suitable microclimate for growing peonies.

Across Alaska, the story is the same – general aviation helps companies to reach far-off markets, transport goods, supplies and staff and make multiple stops in one day. The use of general aviation is also critical for the delivery of healthcare services in our state. For example, Blood Bank of Alaska relies heavily on general aviation aircraft to transport blood to remote communities across Alaska, and these aircraft are also used for disaster relief and law enforcement.

Here in Alaska, luckily, people tend to realize the incredible value of general aviation to the state. Unfortunately, there are many that still don't appreciate the numerous benefits that this form of transportation can provide, particularly outside of our vast state. The President's budget proposal from earlier this year includes a $100 per flight fee that would unfortunately negatively impact the numerous businesses, farms and organizations that rely on general aviation for their work.

Despite this, I am pleased to see that our local elected officials in Alaska have made the effort to recognize the benefits of general aviation and local airports. Recently, Governor Sean Parnell declared September "General Aviation Appreciation Month." In addition, Mayor Jon Eberhart of Fairbanks and Mayor Dan Sullivan of Anchorage both declared September "General Aviation Appreciation Month." It is also encouraging to see that Senator Lisa Murkowski and Representative Don Young are part of the General Aviation Caucus.

These are excellent steps forward, I hope we can build on them and continue to spread awareness about this valuable form of transportation.

Mike Williams is the managing partner of Alaska Peony Distributors, LLC and a member of the Alliance for Aviation Across America.

- See more at: http://www.thecordovatimes.com

Commissioner Kestner speaks on downed planes at Lake County Historical Society

Visiting the Lake County Historical Society’s (LCHS) monthly meeting was Commissioner Ken Kestner. He was their guest speaker to educate members on the three crashed planes in Lake County lakes. The meeting was held at the Western Villa on Thursday, Jan. 15.

Kestner came prepared with a variety of images that were prepared by Dept. Sheriff Chuck Pore for the members to pass around that depicted the remains that were found on the lakebeds. One of these panel images was of the supposed airplane models Helldiver, a Corsair and a P38 that are thought to be the ones that crashed.

Residents of the Goose Lake area reported recently of lootings of the planes, said Kestner, which gave alarm to government agencies to pay attention to these historical planes and the soldiers who flew them. Kestner said that federal law gives ownership of the planes to the government. He added an interesting tidbit that the planes were picked up by ice over the years and carried them across the bed, leaving “scars” on its bottom.

Kestner told a story of two Lakeview men in 1950 who retrieved one of the airplane’s engines by use of snow sled. When law enforcement tracked these men down, they claimed that they were vintage aircraft enthusiasts and “stole it to prevent it from being stolen,” Kestner said, earning much laughter from his audience.

Assuring them that the recovery is continuing with crews returning next spring, he gave some details how agencies are going about it. He said that human scent dogs were sent out to the sites where they picked up indications of a human presence around the cockpits of the plane though no human remains were found. Kestner added that Lynne Engelbert, a former Lakeview citizen who now resides in Central California, trained these dogs. Some of the dogs Englebert trained were a part of the recovery crew of the 9/11 terrorist attacks and also have discovered a 600-year-old cremation burial site in Alaska.

Member Marie Lee asked who was lost in the crash and if they had tried to recover them at the time. Kestner said that there were three different deaths with names unknown and that it is also unclear as to exactly what was recovered and the cause of the crashes.

Nearing the end of his presentation, Kestner addressed the members’ concerns about the emergency lakebed closures by the Department of State Lands (DSL) at the end part of last November.

“The DSL hasn’t seen anything like this before so they are writing the rules as they go,” Kestner said, adding that Lake County will be involved to see that the regulations will not grow to unreasonable measures.

For more information on the LCHS, contact Claudia Reeder at 541-219-0200.

Original article can be found at: http://lakecountyexam.com

Mayor breaks tie, OKs hangar project: Norfolk Regional Airport (KOFK), Nebraska

A proposed $1 million hangar project and taxiway at the Norfolk Regional Airport was cleared for take-off Tuesday.

But Mayor Sue Fuchtman first had to break a tie vote by the city council to approve local financing for the Norfolk Airport Authority project.

Financed with grants and loans, the eight-plane hangar building will require a property tax increase estimated at $60,000 annually for 10 years as the local share for debt service.

After discussing the issue for an hour, the council voted 4-4 on the resolution authorizing the increase. The mayor, who only votes to break ties, then cast the deciding ballot in favor.

After voting, Fuchtman urged the airport authority to keep the city informed.

“The question I would ask you to ask is what percentage is funded by the tax dollars to take care of those rental hangars because I think that’s one of the things that has been very concerning,’’ she said.

The mayor said one of her friends, who has an airplane hangared there, has seen improvements made at the airport.

“I think we can further answer some questions and concerns of some of this council. We’re willing to work with you and be a part of it,’’ Fuchtman told members of the airport authority.

Voting for the measure were Dave Fauss, Shane Clausen, Jim Lange and Josh Moenning. Against were Corey Granquist, Thad Murren, Dick Pfeil and Rob Merrill.

Some discussion focused on who should pay for the hangar and taxiway — businesses and individuals who own private aircraft or the taxpayers.

“Are we asking the taxpayer to subsidize a hangar with their tax dollars?’’ Merrill said.

“Basically,’’ responded Dan Geary, chairman of the airport authority.

But he went on to say the $70,000  from annual hangar rentals goes toward airport operations and is money the authority doesn’t have to ask the city for.

In the past, the authority had accumulated as much as $800,000 from hangar rentals, Geary said, and could pay for hangars. That practice has stopped, and the authority now comes to the city for capital projects.

He further noted that the authority has raised rental rates, effective Jan. 1. All 46 hangars are occupied, and new requests for space from aircraft owners are turned down.

Jerome Bahm, the authority’s accountant, said the authority hadn’t received any budget increase for five years in a row, and only this past year received a 3.5 hike from a rise in valuations, as other city divisions did.

Merrill asked if the authority had looked at raising rental rates even further to pay for the project. He wondered whether hangars are full because rents are cheap.

“We don’t think so,’’ said Terri Wachter, the airport manager who noted that rates at similar airports in Nebraska were examined to come up with the new rates at Norfolk. Future annual increases are built into the rate structure as well.

It would take a 60 percent increase in rental rates to pay for the project, according to the authority.

It was further noted that some local businesses have built their own hangars at the airport on leased land.

Shane Weidner, city administrator, said the airport is important when business prospects come to town.

“The investment we make in our airport . . . is invaluable. Absolutely it’s an economic development tool,’’ he said.

With the green light from the council, the authority can now submit final paperwork needed for loans and grants that have been approved by the Federal Aviation Administration and Nebraska Department of Aeronautics.

City sales tax up

Norfolk has experienced a big increase in local sales tax revenue.

It’s reflected in the last three months of sales tax collections, which are ahead by 13 percent of a year ago. The receipts totaled $2.1 million, or $249,213 more.

Randy Gates, city finance director, attributed the rise to purchases made in the wake of  the June hail storm.

“It’s not exactly how you want your economy to grow,’’ Gates told the council.

But it means sales tax revenue is trending much better than anticipated by the city. Norfolk levies a 1.5-cent tax. It will increase by half a cent this spring to pay for improvements to the public library.

The tax on keno also is yielding more revenue. Norfolk received net proceeds of $44,785 for December, which is $5,868 above the budgeted average of $38,916.

Story and comments:   http://norfolkdailynews.com


Methamphetamine-filled drone crashes near US-Mexico border

MEXICO CITY (AP) — Police in a Mexican border city said Wednesday that a drone overloaded with illicit methamphetamine crashed into a supermarket parking lot.

Tijuana police spokesman Jorge Morrua said authorities were alerted after the drone fell Tuesday night near the San Ysidro crossing at Mexico's border with California.

Six packets of the drug, weighing more than six pounds, were taped to the six-propeller remote-controlled aircraft. Morrua said authorities are investigating where the flight originated and who was controlling it. He said it was not the first time they had seen drones used for smuggling drugs across the border.

Other innovative efforts have included catapults, ultralight aircraft and tunnels.

In April, authorities in South Carolina found a drone outside the fence of a prison that had been carrying cellphones, marijuana and tobacco.

Story and photo:   http://www.utsandiego.com


In this image released by the Tijuana Municipal Police on Wednesday Jan. 21, 2015, a drone loaded with packages containing methamphetamine lies on the ground after it crashed into a supermarket parking lot in the city of Tijuana on Tuesday Jan. 20, 2015. According to police, six packets of the drug, weighing more than six pounds, were taped to the six-propeller remote-controlled aircraft. Authorities are investigating where the flight originated and who was controlling it. He said it was not the first time they had seen drones used for smuggling drugs across the border. Other innovative efforts have included catapults, ultralight aircraft and tunnels. (AP Photo/Secretaria de Seguridad P├║blica Municipal de Tijuana)

No closure of airspace for Air Force One

NEW DELHI: The Modi government has brought India on equal footing with the world's superpowers — at least on one front. This time, Air Force One flying in Barack Obama to Delhi later this week will get exactly the same treatment that Air India One, carrying our president or PM, gets abroad. 

"As of now, there are no instructions to close airspace in Delhi for commercial aircraft when Air Force One lands and takes off from here. We will follow the protocol that is done whenever our president or PM is flying. The VVIP aircraft will be given priority in landing and take-off. There will be no delay or holding. This is what happens when AI One or IAF One (a Boeing Business Jet maintained and operated by IAF) goes abroad or flies within India," said a senior official. 

As a result, Delhi's airspace is closed like each R-Day from 10.45am to 12.15pm from January 18 to 24 and then the 26th for flypast rehearsals and then the actual thing. As of now, there is no airspace closure due to Air Force One, said multiple sources. 

Till some time back, air traffic would be closed on the runway where a VVIP aircraft is to land or take off for 10 minutes before and after its movement. In the case of all places in India except Delhi, it meant shutting airports for commercial traffic for 20 minutes. 

With three runways, Delhi's IGI Airport saw only the runway earmarked for VVIP operations being closed for other traffic for 20 minutes. But now, even this practice has been discontinued with. 

Also, Air India One is treated exactly as per the new Indian protocol when it flies abroad and now VVIP flights from other countries will be treated the same. 

Original article can be found at: http://timesofindia.indiatimes.com

Georgia Supreme Court hears lawsuit over The Vein Guys trademark

Hawker Beechcraft 390 Premier IA, The Vein Guys, N777VG:  Accident occurred February 20, 2013 in Thomson, Georgia

ATLANTA, GA (WFXG) -


The Georgia Supreme Court is hearing a case about who owns the trademarks of Vein Care Pavilion of the South, which includes The Vein Guys, a Columbia County plastic surgery business.


The dispute began in 2010 with the sudden death of Dr. Keith L. Davis. Before his death, Davis had founded Vein Care Pavilion of the South with Dr. Steven M. Roth. One of the trademarks of the medical practice is The Vein Guys, a practice that provides treatment of varicose veins.


An operating agreement stated that Davis and Roth each owned 50 percent of the business. It also stated that in the event of the death of one of the doctors, the surviving doctor had the first option to purchase the rest of the business. That purchase had to occur within 90 days after someone was appointed to handle the deceased doctor's estate.


The agreement also stated that in the event of a dispute over the value of the half of the business owned by the deceased doctor, an accountant would be appointed to determine the value. After Davis' death, the accountant who worked for the medical practice was appointed to determine the value of the business.


Davis' wife, who had been appointed to handle her husband's estate, objected to the accountant doing the valuation because she said he was biased because he then solely worked for Roth.


In December 2010, Roth sued to get the accountant approved to perform the valuation. He also sought a ruling that the trademarks owned by Vein Care Pavilion South, including The Vein Guys, were owned by VCP South. Roth learned after Davis' death that all the trademarks had been registered in Davis' name but had been paid for by VCP South.


The trial court never determined who owns the trademarks, but did rule that the accountant could perform the valuation. The accountant set the value of Davis' interest in the company at about $2.5 million. Davis and her attorney appealed, but the Georgia Court of Appeals upheld the lower court's ruling.


A number of delays occurred in the sale of Davis' interest in the business, including the February 2013 death of Roth, along with four of his employees, in a plane crash near the Thomson-McDuffie airport.


The sale of Davis' interest in the company was not finalized until December 2013 - after Roth's death.


The Georgia Supreme Court now has to decide how much in profits Davis is owed. Davis' attorneys are arguing that she is owed profits from the business through December 2013 - when the sale of her husband's interests in the business was finalized. But Roth's attorneys argue that Davis is only owed profits from the business up until her husband's death in 2010.


The court is also reviewing whether it was fair for Davis to take down The Vein Guys Facebook page. She took it down in March 2014 because she believed her husband owned the trademark. Lower courts have ruled against Davis and ordered her to pay up to $1,000 for each day she refused to reinstate the page.


Original article can be found at: http://www.myfoxal.com



Dr. Steven Roth

http://registry.faa.gov/N777VG


NTSB Identification: ERA13MA139

14 CFR Part 91: General Aviation
Accident occurred Wednesday, February 20, 2013 in Thomson, GA
Probable Cause Approval Date: 10/21/2014
Aircraft: BEECH 390, registration: N777VG
Injuries: 5 Fatal, 2 Serious.
NTSB investigators traveled in support of this investigation and used data obtained from various sources to prepare this aircraft accident report.

The purpose of the flight was to return employees of a vein care practice to their home base at Thomson-McDuffie County Airport (HQU), Thomson, Georgia. The pilot was the pilot flying, and the copilot was the pilot not flying. (The National Transportation Safety Board [NTSB] notes that although the copilot is referred to as such in this report, his role in the cockpit is not required by federal regulations.) The departure from John C. Tune Airport, Nashville, Tennessee, and en route portions of the flight were uneventful. During the flight, the copilot reminded the pilot about a speed restriction and also reminded the pilot to adjust his altimeter. The pilot responded to the altimeter reminder by stating, "say, I'm kinda out of the loop or something. I don't know what happened to me there but I appreciate you lookin' after me there." About 4 minutes later, on approach to HQU, the pilot lowered the landing gear, and the ANTI SKID FAIL message illuminated in the cockpit; the copilot commented on the illumination. The pilot continued the approach; he did not respond to the copilot and did not refer to the Abnormal Procedures section of the Federal Aviation Administration (FAA)-approved Abbreviated Pilot Checklist to address the antiskid system failure message. The airplane touched down on runway 10 about 2005, and about 7 seconds later, the pilot initiated a go-around. (In postaccident interviews, neither the pilot nor the copilot recalled the reason for the go-around.) The airplane lifted off near the departure end of the 5,503 ft-long runway. According to enhanced ground proximity warning system (EGPWS) data, when the airplane was about 63 ft above ground level, the left wing struck a utility pole, which was 72 ft high and about 1,835 ft from the runway threshold, severing the outboard portion of the wing. The airplane continued another 925 ft before crashing in a wooded area. 


Examination of the wreckage revealed no evidence of any preimpact failures or malfunctions of the engines or flight controls. The reason for the antiskid system malfunction could not be determined due to the general destruction of the wreckage. 


For an antiskid inoperative condition, the Abbreviated Pilot Checklist only provides landing distance values for flaps up and flaps 10 degrees. The pilot should have selected one of those two flap settings for landing and determined the landing distance required. The first data recorded by the EGPWS showed that the airplane was configured at flaps 30. The flaps were transitioning through flaps 15 at the time of impact.


When the antiskid system fails, the landing distance required for full stop increases greatly: according to the Abbreviated Pilot Checklist, the landing distance would increase about 130 percent with flaps up and 89 percent with flaps 10. Thus, the required landing distance for the weather conditions that prevailed at HQU at the time of the accident with flaps up was 7,066 ft, and the required landing distance with flaps 10 was 5,806 ft. HQU runway 10's available runway length for landing was 5,208 ft, which did not meet the flaps up or flaps 10 performance penalty requirements with an antiskid system failure, thus requiring a diversion to a longer runway. It is likely that after touchdown, the pilot recognized that the airplane was not slowing as he expected and might not stop before the end of the runway. Rather than risk a high-speed overrun, he elected to conduct a go-around. 


The NTSB determined that at the time the airplane struck the utility pole, the landing gear was extended, the flaps were in transit (retracting) toward the 10-degree position, and the lift dump system was deployed. Lift dump is a critical system to assist in stopping the Beechcraft 390 Premier (Premier 1A) during landing. Section 3A of the airplane flight manual (AFM) (Abnormal Procedures) included the following warning: "Extending lift dump in flight could result in loss of airplane control leading to airplane damage and injury to personnel. Continued safe flight with lift dump extended has not been demonstrated." The wreckage examination as well as drag estimates based on recovered EGPWS data indicate that the lift dump remained extended during the airplane's go-around attempt. The airplane drag associated with lift dump, flaps, and landing gear likely resulted in only marginal climb performance. While Beechcraft does not publish a procedure for a go-around after touchdown, aerodynamic data for the 390 Premier (Premier IA) suggest that if the airplane were configured with lift dump retracted and flaps 10 degrees or less, it would have been capable of a significantly higher climb rate after the failed landing attempt.


The pilot displayed a lack of systems knowledge of the accident airplane. First, the pilot demonstrated a lack of understanding of the antiskid system. Although the pilot had received antiskid system failure training during his recurrent simulator training on January 4, 2013, he stated in postaccident interviews that he did not think they needed the antiskid system for the landing at HQU and that the performance penalty would only apply if you were "trying to make your numbers." Because of this faulty belief, when the antiskid failure illumination occurred, the pilot did not take action. Second, the pilot selected a flap position (flaps 30) that was prohibited by the antiskid failure procedures in the AFM. Third, he performed a go-around with the lift dump extended. Both the AFM and a placard in the cockpit warned against extending the lift dump in flight. When the pilot decided to go around, he should have immediately retracted the lift dump per the AFM restriction for lift dump extension in flight. 


The utility pole (Pole 48) that was struck was erected, along with several others, in 1989 by Georgia Power. The FAA was not notified before the construction of the utility poles in 1989; accordingly, no obstruction evaluation was done, and no depictions or mention of possible obstructions in the area were included on associated aeronautical charts. After the accident, Georgia Power submitted FAA Forms 7460-1 for four utility poles east of the airport, including Pole 48. The FAA conducted aeronautical studies on the poles and, on May 31, 2013, determined in its initial findings that Pole 48 did not comply with FAA obstruction standards and was "presumed to be a hazard to air navigation." The study also stated that if the pole were lowered to a height of 46 ft or less, it would comply with obstruction standards. After the FAA issued the preliminary obstruction determinations, Georgia Power requested that the FAA conduct further study on the four obstructions to determine if a favorable determination could be achieved. On August 12, 2013, the FAA published public notices announcing the four aeronautical studies and invited interested parties to submit relevant comments before September 18, 2013. According to an FAA official, the final determinations for the four obstructions were not completed at the time of this report. Since the initial aeronautical studies were conducted, the FAA Flight Data Center issued several notices to airmen to alert pilots about obstructions and also to amend the approach and departure procedures at HQU accordingly. In addition, the FAA increased the glideslope angle for the runway 28 precision approach path indicator from 3.00 to 3.50 degrees. Although the FAA has deemed the pole a presumed hazard, the pilot's attempted flight with the extended lift dump made airplane control and continued safe flight unlikely. 


In evaluating the pilot's performance, the NTSB considered that the pilot experienced a sleep restriction, a circadian disruption the night before the accident, and long duty hours and extended wakefulness. The pilot normally slept about 8 hours per night; however, he only slept 5 hours the night before the accident (February 19). Further, the pilot awoke about 0200 on the morning of the accident, which was significantly earlier than his normal waking time of about 0600. On the day of the accident, he reported that upon arrival in Nashville, he slept for about 4 hours in a chair in the pilot lounge. However, his cell phone activity indicated outgoing calls during that time, suggesting interruptions to his sleep, which would have fragmented any sleep the pilot did obtain and degrade its restorative quality. Additionally, the accident took place about 2006, indicating an extended period of wakefulness based on the early awakening. Based on the available evidence, the pilot was likely suffering from fatigue at the time of the accident. Research indicates that fatigue associated with sleep loss, circadian disruption, and long duty hours can lead to increased difficulty in sustaining and directing attention, memory errors, and resultant lapses in performance. An NTSB safety study found that flight crewmembers who were awake for more than 12 hours made more procedural errors, tactical decision errors, and errors of omission than those awake less than 12 hours (NTSB. 1994. A Review of Flightcrew-Involved Major Accidents of U.S. Air Carriers, 1978 through 1990. SS-94/01. Washington, DC). Twice during the accident flight, the copilot gave the pilot reminders (one about the speed restriction and one about the altimeter). The pilot responded by indicating that he was "out of the loop." Further, the pilot did not refer to the Abbreviated Pilot Checklist for the antiskid system failure (for which the copilot commented on the illuminated light) or retract the lift dump when he elected to go around. Had the pilot not been fatigued, he likely would have paid closer attention to the flight and not had lapses in performance.


Both pilots survived, with serious injuries, and all five passengers, who were seated in the back, died. Postaccident examination showed that the seat buckles in the back were not fastened and the shoulder harnesses were not attached or pulled out. According to the copilot, the "fasten seatbelt" sign was on (the seatbelt chime was recorded by the cockpit voice recorder), but he did not remember giving a briefing on seatbelts. The pilot indicated that he did not remember seeing if the passengers had their seatbelts on. All six of the passenger seats had been forcibly detached from the airplane fuselage, and three were consumed by fire. All of the passengers sustained multiple traumatic injuries. Although proper use of restraint systems in survivable accidents can dramatically lessen or prevent serious injuries to occupants, due to the high impact forces and fragmentation of the cabin in this accident, it is unknown whether the use of restraints would have affected the survivability of the passengers. 


Member Sumwalt filed a concurring statement that can be found in the public docket for this accident. Member Weener joined the statement.


The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

The pilot's failure to follow airplane flight manual procedures for an antiskid failure in flight and his failure to immediately retract the lift dump after he elected to attempt a go-around on the runway. Contributing to the accident were the pilot's lack of systems knowledge and his fatigue due to acute sleep loss and his ineffective use of time between flights to obtain sleep. 

Member Sumwalt filed a concurring statement that can be found in the public docket for this accident. Member Weener joined the statement.


http://www.ntsb.gov


***This report was modified on August 25, 2014, and October 21, 2014. Please see the docket for this accident to view the original report.***

HISTORY OF FLIGHT

On February 20, 2013, about 2006 eastern standard time (EST), a Beechcraft Corporation 390 Premier (Premier IA), N777VG, collided with a utility pole, trees, and terrain following a go around at Thomson-McDuffie County Airport (HQU), Thomson, Georgia. The airline transport-rated pilot and copilot were seriously injured, and the five passengers were fatally injured. The airplane was registered to the Pavilion Group, LLC, and was operated under the provisions of 14 Code of Federal Regulations (CFR) Part 91 as a business flight. Night visual meteorological conditions prevailed, and an instrument flight rules (IFR) flight plan was filed. The flight originated at John C. Tune Airport (JWN), Nashville, Tennessee, about 1827 central standard time (1927 EST).

On the morning of the accident, the pilot and copilot left their respective homes in South Carolina about 0230 for the 1-hour drive to HQU (where the airplane was based) to fly five passengers, who were employees of Vein Guys®, to JWN. (The National Transportation Safety Board [NTSB] notes that while the copilot is referred to as such in this report, his role in the cockpit is not required by federal regulations.) The airplane departed HQU about 0406 and arrived at JWN about 0459. (Although JWN is located in the central time zone, all subsequent times in this report are in EST unless otherwise noted.) Both pilots stated in postaccident interviews that the flight to JWN was uneventful and the weather was good. They reported that at the JWN terminal, they slept in the crew break room, completed paperwork, and worked on the computer. They left for a late lunch about 1500 and returned to the airport about 1630.

According to security camera footage from the JWN terminal, both pilots were observed walking toward the airplane about 1913, and about 1918, the five passengers were seen walking toward the airplane while one crewmember performed an external walk-around inspection. About 1923, the airplane taxied from the parking area and departed JWN at 1927. The pilot was the pilot flying and was in the left cockpit seat.

About 1927, the flight crew contacted departure control while climbing through 3,500 ft mean sea level (msl) and requested an IFR clearance to HQU. About 1930, the flight crew contacted the Memphis air route traffic control center (ARTCC) while climbing through 14,000 ft msl, and about 1933, the flight was cleared to climb and maintain a cruising altitude of flight level (FL) 270. According to flight crew interviews, the en route weather was good, and a tailwind in excess of 70 knots was observed.

About 1948, the flight crew contacted the Atlanta ARTCC and was cleared to descend to FL240. About 1953, the flight crew was given a further descent clearance to 11,000 ft msl along with the Athens, Georgia, altimeter setting. About the same time, the copilot tuned in the HQU automated weather observation system (AWOS) to receive the most current weather at the destination airport. The AWOS at 1935 reported calm wind, temperature 10 degrees C, 10 statute miles visibility or greater, scattered clouds at 12,000 ft, and an altimeter setting of 30.13 inches of mercury. The pilot then set up the flight management guidance system for a visual approach to runway 10 at HQU with a 3.4-degree descent to the runway from a 5-mile final approach. The copilot tuned the instrument landing system for runway 10 as a backup. 

About 1956, the flight crew advised the Atlanta ARTCC that they were descending through 18,500 ft, and 2 minutes later, they cancelled their IFR flight plan. About 1958, the copilot stated to the pilot, "ten thousand comin' up captain and you blowin' through." About 1959, the copilot told the pilot to adjust his altimeter. The pilot responded, "say, I'm kinda out of the loop or something. I don't know what happened to me there but I appreciate you lookin' after me there." The flight crew was then directed to contact Augusta approach control, and about 2000, the flight crew contacted Augusta approach control and advised that they were descending out of 8,400 ft and had HQU in sight. About 2002, the flight crew advised Augusta approach control that they would switch to the local HQU advisory frequency. 

Concurrently, the pilot began to perform an "S" turn along the final approach path to the runway. About 1 minute later, the enhanced ground proximity warning system (EGPWS) aural alert announced that the airplane was 1,000 ft above the ground, and the pilot lowered the landing gear. According to the cockpit voice recorder (CVR), after the landing gear was lowered, about 2004, the copilot noted that the "ANTI SKID FAIL" annunciator light illuminated. The pilot continued the approach, and, about 2005, the airplane touched down on runway 10. Witnesses reported that after the airplane touched down, they heard or saw it go around. According to the CVR, the takeoff warning horn sounded about 0.3 seconds before the pilot stated that he was performing a go-around. The airplane lifted off near the departure end of the runway. The copilot directed the pilot to increase pitch. According to EGPWS data, as the airplane climbed to an altitude of about 63 ft above the ground, about 9 seconds after liftoff, the left wing struck a utility pole located about 0.25 miles east of the departure end of the runway. The airplane continued about 925 ft before colliding with trees and terrain. It was destroyed by impact forces and a postcrash fire.

During a postaccident interview, when asked about the approach, landing, and go-around at HQU, the pilot recalled checking the airplane's landing light switches to prepare for the landing. The next thing he remembered was waking up in the hospital on February 24, 2013. He did not recall any additional details about the approach, landing, or go-around or any airplane system anomalies, including any antiskid problems, during the flight.

In postaccident interviews, the copilot did not recall anything unusual about the glidepath and recalled being about 1 or 2 knots above reference speed. The copilot thought that the airplane touched down on runway 10 within 200 ft of the 1,000-ft runway marker. As he began to reference the after landing checklist, he heard the pilot announce a go-around, but the copilot did not know the reason for the go-around. He stated that he began to monitor the airspeed indicator, saw that they were at 105 knots approaching the end of the runway, and thought "it was going to be close." The engines sounded like they always did on a normal takeoff. He thought something hit the airplane on his side and recalled seeing trees in the windshield. The next thing he remembered was seeing someone with a flashlight at the accident scene. He did not recall any alarm or aural caution before the go-around and indicated that everything looked normal. 

PERSONNEL INFORMATION

The Pilot

The pilot, age 56, held an airline transport pilot (ATP) certificate with a single pilot type rating on the Premier IA. (The 390 Premier is the same as the Premier I/IA series.) He also held a flight instructor certificate with airplane single engine land, airplane multiengine land, and instrument airplane privileges. He was the director of operations for Sky's the Limit, doing business as Executive Shuttle, a 14 CFR Part 135 operator based in Greenwood, South Carolina. He was hired by the Pavilion Group to provide private pilot services for their Premier IA under the provisions of 14 CFR Part 91. The pilot reported 13,319 hours total flying time, including 12,609 hours as pilot-in-command (PIC). He reported 198 hours, all as PIC, in the Premier IA. The pilot held a second-class Federal Aviation Administration (FAA) medical certificate, issued October 29, 2012, with a limitation to possess glasses for near/intermediate vision. 

According to interviews and training records, the pilot attended the FlightSafety Premier I Series (RA-390) initial training course at the FlightSafety Wichita Learning Center, Wichita, Kansas, from June 7, 2012, through June 22, 2012. The ground instruction consisted of 58 hours of ground training and 11.5 hours of briefing/debriefing. The pilot also attended flight simulator training, which consisted of 15 hours of simulator training. He was type rated on the Premier IA on June 22, 2012, following a 2.2-hour simulator session and a 2.5-hour oral/written examination.

The pilot also attended the FlightSafety Premier I Series (RA-390) recurrent PIC course at the FlightSafety Greater Philadelphia/Wilmington Learning Center, Wilmington, Delaware, from January 3, 2013, through January 5, 2013. The ground instruction consisted of 12 hours of training and 4.5 hours of briefing/debriefing. The simulator portion of the training consisted of 7 hours of simulator time.

A copilot who previously flew with the pilot stated that the pilot was experienced, professional, and possessed good flying skills. Both copilots who flew with the pilot, including the accident copilot, stated that they did not have a specific role on the flights they flew with him in the Premier IA.

On February 15, the pilot flew the owner of Vein Guys® and his family to Orlando, Florida, and remained in Orlando until Monday, February 18. He did not use a copilot for the Orlando trip. On February 18, he flew the family to HQU and then drove to his residence, going to bed about 2100. On February 19, he awoke about 0500 for a 0930 flight to Olive Branch, Mississippi, with the accident copilot and Vein Guys® staff. The return flight landed at HQU about 1700 that evening. He arrived at his residence about 1820 and went to bed about 2100.

On the day of the accident, the pilot awoke about 0200 and arrived at HQU about 0330 for the 0400 flight to JWN. He described February 20 as a "tough, tough day" because of the early departure time. After arriving at JWN, he slept for about 4 hours in a chair in the pilot lounge. He did not sleep again that day. A review of the pilot's cell phone records revealed three outgoing calls were made during his 4-hour sleep break. The pilot indicated that he normally slept about 8 hours per night and that he typically awoke about 0600.

The Copilot

The copilot, age 40, held an ATP certificate. He possessed no type ratings. He was employed by and flew charters for Executive Shuttle, which was owned by the accident pilot. He accompanied the accident pilot on the Premier IA flights at the pilot's request and estimated that he had about 45 flight hours in the Premier IA. He reported 2,932 hours total time, including 2,613 hours as PIC. The copilot held a second-class FAA medical certificate, issued February 12, 2013, with no limitations.

The copilot received no simulator training in the Premier IA before the accident and did not complete formal training courses in the Premier IA. He received a 14 CFR 61.55 logbook endorsement on October 10, 2012, from the accident pilot, stating that he demonstrated the skill and knowledge required for safe operation of the Premier IA as second-in-command. 

On Monday, February 18, the copilot was at home and awoke between 0600 and 0630 and went to bed about 2200. On Tuesday, February 19, he awoke between about 0530 and 0600 and flew with the captain to Olive Branch. After returning to HQU, the copilot made the 1-hour drive to his home but was not certain what time he went to bed or fell asleep. The last cell phone activity that day occurred about 2148. On Wednesday, February 20, the copilot awoke between about 0200 and 0215 and drove with the accident captain to HQU for the flight to JWN. The copilot told investigators he was able to sleep for about 4 to 5 hours in the pilot lounge (awakening about 1000 central time). 

AIRCRAFT INFORMATION

The Premier IA was a carbon fiber composite fuselage, metal low-wing airplane powered by two Williams FJ44-2A turbofan engines mounted on the aft fuselage each rated at 2,300 lbs of thrust.

The Premier IA was not equipped with reverse thrust, and wheel braking was the primary means of stopping the airplane after landing. (The lift dump assists in putting weight on the wheels, which makes braking more effective.) The airplane was equipped with an electrically controlled antiskid system. According to the manufacturer, the system offered protection from skids and could provide consistently shorter landing rolls for all runway conditions. The ANTI SKID FAIL annunciator would illuminate if a malfunction existed in the system when the ANTI SKID switch was in the NORM (normal) position.

Activation of the lift dump switch extended the three spoiler panels on each wing and overrode normal spoiler operation. A placard was located on the cockpit pedestal immediately aft of the lift dump switch that read, "WARNING DO NOT EXTEND IN FLIGHT." In addition, the Hawker Beechcraft Premier I/IA Model 390 Airplane Flight Manual (AFM), Section 3A—Abnormal Procedures, page A-25, states, "Do not extend lift dump in flight." Section 3A of the AFM (Abnormal Procedures) included the following warning: "Extending lift dump in flight could result in loss of airplane control leading to airplane damage and injury to personnel. Continued safe flight with lift dump extended has not been demonstrated."

The airframe and engine maintenance logbooks were not located after the accident. Pavilion Group used CAMP Systems as their maintenance management provider, and the Hawker Beechcraft Service Center, Atlanta, Georgia, also provided maintenance services.

The most recent record of maintenance performed on the airplane occurred on January 29, 2013, at Aeronautical Services, Greenwood, South Carolina. The maintenance included replacement of the left and right main tires, touching up exterior paint, and a battery capacity check. The total time on the airplane was not recorded at that time.

The most recent maintenance record indicating aircraft total time was on January 4, 2013, when the airframe total time was 635.4 hours. The most recent comprehensive airframe and engine inspection was recorded on June 15, 2012. The 600-hour Schedule A inspection was accomplished at 503.3 hours total time and 565 total airframe cycles.

METEOROLOGICAL INFORMATION

The National Weather Service (NWS) reported no significant weather and no precipitation over the region. The area forecast applicable for HQU expected light wind and scattered to broken high cirrus clouds, with visibility unrestricted. The NWS also issued an airmen's meteorological information that was current at the time of the accident for moderate turbulence below 8,000 ft over the area.

HQU was equipped with an AWOS that issued observations every 20 minutes. The HQU 1955 observation reported calm wind, visibility 10 miles or greater, sky clear, temperature 9 degrees C, dew point -4 degrees C, and altimeter setting 30.12 inches of mercury. The HQU 2015 observation reported wind from 240 degrees at 6 knots, visibility 10 miles or greater, broken ceiling at 12,000 ft above ground level (agl), temperature 11 degrees C, dew point -3 degrees C, and altimeter setting 30.15 inches of mercury.

AIRPORT INFORMATION

General

HQU was a general aviation airport with one asphalt runway (runway 10-28) measuring 5,503 ft long and 100 ft wide, with precision instrument markings on both ends. The runway had high-intensity runway edge lights that changed from white to amber for the last 2,000 ft in both directions. Both ends had red threshold lights and green approach lights. Adjacent to the touchdown zone for both ends of the runway was a two-unit precision approach path indicator (PAPI) system set at 3 degrees. (As later discussed, following an aeronautical study after the accident, the FAA changed the glidepath angle for the runway 28 PAPI to 3.5 degrees.) Postaccident tests and inspections of the airport lighting systems indicated that the lighting system was operating normally at the time of the tests. 

The runway and taxiway lights were pilot-adjustable to low, medium, and high settings and would remain on for 15 minutes after activation. The PAPIs would not activate when the runway lights were set to the low setting. A City of Thomson administrator managed the airport with the help of an on-site airport manager who also managed a local fixed base operation (Spirit Aviation). The airport manager did not prepare or keep any logs about airport self-inspections, regular maintenance, wildlife strikes, lighting activation, or periodic inspection/calibration of the PAPI units. According to the airport manager, a local electrical contractor accomplished all preventative and repair work on the airport's lights and navigational aids on an as needed basis. After the accident, the airport began keeping weekly logs of lighting outages, maintenance, and general field conditions. 

The Georgia Department of Transportation (GDOT) inspected HQU biennially to ensure compliance with the requirements set out in GDOT's Rules and Regulations for Licensing of Certain Open-to-the-Public Airports. The GDOT inspections also included an airport inspection for the FAA's Airport Safety Data Program. The two most recent inspection reports from 2010 and 2012 determined that HQU met the minimum state licensing requirements but failed to meet federal requirements for precision and visual approaches. Specifically, runway 10 failed to meet FAA Part 77 reporting requirements for a 50:1 obstruction-free, precision instrument approach to 200 ft from the runway end. Similarly, runway 28 failed to meet the FAA Part 77 reporting requirements for a 34:1 obstruction-free, nonprecision instrument approach to 200 ft from the runway end. The obstructions listed for both approaches were trees, left and right of centerline. The 2012 inspection report for the runway 28 approach included an obstruction characterized as a power line, 66 ft high, and 2,200 ft from the displaced threshold, extending from the centerline to 400 ft right of centerline, which provided a 27:1 approach to 200 ft from the runway end and a 33:1 approach to the displaced threshold. 

The Thomson city administrator stated that before 2012, no GDOT inspection report had identified the power line east of the airport as a potential obstruction. To determine whether the power line was an obstruction and to provide data in support of an official airport layout plan, the city administrator authorized a formal survey of the airport. The survey had not been completed at the time of the accident or at the time of this report. 

Airport Obstructions

During the accident sequence, the airplane struck a concrete electrical utility pole (Pole 48) that was about 1,835 ft east of the runway 28 threshold and 50 ft left of the extended runway centerline. Pole 48 was 72 ft high, and the airplane struck the pole about 58 ft agl. The pole was not equipped with lights, but orange visibility balls were on the adjacent wires. 

The pole was owned and maintained by Georgia Power, a regional utility that supplied electric power to local businesses and residents. Pole 48 was erected in 1989, along with similar poles and electrical utility lines, to provide electrical power to the Milliken and Company textile plant adjacent to HQU. Thomson McDuffie County entered into an "aviation easement" agreement with Deering Milliken, the owner of the Milliken Kingsley textile factory adjacent to HQU, in September 1973. The provisions of the easement were designed to protect the approach surface east of the airport. The text of the easement stated that Deering Milliken "…will not hereafter erect or permit the erection or growth of any structure, trees, or other object within or upon said parcel, which lies within the approach area of the 9-27 [now 10-28] runway to a height above the approach surface. Said approach surface being an inclined plane with a slope of 34:1, i.e. one ft of elevation for each 34 ft of horizontal distance, located directly over the center of said parcel." Milliken and Company entered into easement agreements with Georgia Power in May 1977 and again in August 1989 to grant the right to construct, erect, install, operate, and maintain "poles, wires, transformers, service pedestals, and other necessary apparatus" to supply electrical power to the Milliken Kingsley textile plant.

Title 14 CFR Part 77 establishes standards for approach surfaces to runways of various types and requires notice to the FAA of any proposed construction or alteration of existing structures that may affect the national airspace system. FAA Advisory Circular 70-7460-1K, "Obstruction Marking and Lighting," provides guidance on compliance with 14 CFR Part 77 and procedures for notifying the FAA of proposed construction or alteration. Specifically, a Notice of Proposed Construction or Alteration Form (FAA Form 7460-1) is required for notification. Upon receipt of Form 7460-1, the FAA will conduct an aeronautical study to determine the effects of the construction or alteration on navigable airspace. Then, the FAA will determine if the construction or alteration constitutes a hazard to air navigation. 

Georgia Power did not notify the FAA before constructing the utility poles in 1989; therefore, the FAA had no knowledge of the poles as potential obstructions. Accordingly, there were no depictions or mention of possible obstructions on associated aeronautical charts. 

After the accident, Georgia Power submitted FAA Forms 7460-1 for four utility poles east of the airport, including Pole 48. The FAA conducted aeronautical studies on the poles and, on May 31, 2013, issued initial findings from the studies. Regarding Pole 48, the FAA determined in its initial findings that "…the structure as described exceeds obstruction standards and/or would have an adverse physical or electromagnetic interference effect upon navigable airspace or air navigation facilities. Pending resolution of the issues described below, the structure is presumed to be a hazard to air navigation." The study also stated that if the pole were lowered to a height of 46 ft or less it would not exceed obstruction standards, and a favorable determination could subsequently be issued. The FAA reported similar findings on the other three structures. The FAA stated in its findings that to pursue a favorable determination at the originally submitted height, further study would be necessary, and a formal request would be required within 60 days.

After the FAA issued the preliminary obstruction determinations, Georgia Power requested that the FAA conduct further study on the four obstructions to determine if a favorable determination could be achieved. On August 12, 2013, the FAA published public notices announcing the four aeronautical studies and invited interested parties to submit relevant comments before September 18, 2013. According to an FAA official, the final determinations for the four obstructions were not completed at the time of this report. Since the aeronautical studies were conducted, the FAA Flight Data Center issued several notices to airmen to alert pilots about obstructions and also to amend the approach and departure procedures at HQU accordingly. In addition, the FAA increased the glideslope angle for the runway 28 PAPI from 3.00 to 3.50 degrees. 

FLIGHT RECORDERS

Although not required, the airplane was equipped with an L-3/Fairchild FA2100-1010 CVR. The CVR recording contained the last 30 minutes of digital audio, which was stored in solid-state memory modules. The CVR sustained significant heat and structural damage as a result of the accident. Despite the damage to the unit, three channels of recorded audio were available, ranging from good to excellent quality. The recording began at 1935:13 as the flight was at FL240, and the recording stopped about 2006 during the crash sequence. The airplane was not equipped with a flight data recorder, nor was it required to be so equipped.

WRECKAGE AND IMPACT INFORMATION

The airplane struck Pole 48, and sections of the pole and attached power lines were found along the wreckage debris path, which was oriented from west to east on an approximate magnetic heading of 085 degrees. The left wing was completely severed about 13 ft inboard from the wing tip and exhibited no fire damage. The severed wing was located about 320 ft east of Pole 48. 

Various fragments of the airplane structure were found along the debris path leading to the main wreckage site, which was located about 925 ft east of Pole 48. Multiple trees, up to 2 ft in diameter, were severed or toppled in the main wreckage impact zone. The main wreckage consisted of the center wing section, a portion of the right wing, the main landing gear, the baggage compartment, the emergency locator transmitter rack, and the empennage. The main wreckage was damaged by a postcrash fire and contained melted aluminum and burnt composite material. The forward fuselage was about 60 ft east of the main wreckage and was damaged by a postcrash fire.

The right engine was separated from the fuselage and was on the south side of the debris path between the main wreckage and the forward fuselage shell. The left engine was severed into two main sections with the compressor and the turbine and exhaust section located in a shallow pond on the north side of the debris path. A large portion of the ground in the vicinity of the accident site was charred and burned by a postcrash fire.

All three landing gear assemblies were located on scene. The left and right main landing gear actuators separated from the landing gear but remained attached to the wing structure. Measurements of the actuator positions, as found, corresponded to the "gear extended" or "down" position. 

An examination of the nose landing gear actuator piston revealed that its extension was at an intermediate position. The nose landing gear had an external downlock mechanism to secure the gear in the down-and-locked position. The mating side of the external downlock mechanism was not observed and therefore precluded determination of the position of the nose landing gear. Fire and impact damage to the antiskid system components (antiskid control unit, power brake/antiskid control valve, and wheel speed transducers) prevented their functional testing. 

The wreckage was transported to a storage facility where additional examinations of the wreckage were performed. The landing gear switch, which was cockpit-mounted, was found with the instrument subpanel attached to electrical wire. The switch exhibited heat and thermal damage consistent with a postcrash fire. The metal part of the switch handle was found in the down (extended) detent, and the J-hook was engaged on the handle. The lift dump switch assembly, which was mounted on the cockpit center console, was not located.

The electrically controlled and operated wing flap system was examined. The four flap positions available to the pilot were UP (0 degrees), 10, 20, and DN (30 degrees/full down). While the flap handle was found in the 10-degree detent, measurements of the flap actuator positions revealed that the flaps were at approximately the 15-degree position (a nonselectable, in-transit position) at the time of impact.

MEDICAL AND PATHOLOGICAL INFORMATION

Both the pilot and copilot sustained serious injuries. Drug and alcohol testing on the pilot and copilot was conducted by the FAA Civil Aerospace Medical Institute after the accident. Toxicology results were negative for both pilots on a wide range of drugs, including major drugs of abuse. 

The Georgia Bureau of Investigation Division of Forensic Science listed the cause of death for all passengers as blunt force injuries.

SURVIVAL ASPECTS

The pilot's seat was found with the seatback and seat pan cushions attached to the frame, which was severely damaged with broken tubes in the seatback and seat bottom. The upper shoulder area of the seat was crushed forward and to the right. The seat, which was located near the remains of the cockpit, appeared to be forcefully detached from the cockpit floor track rails with small floor track pieces attached to the seat post. First responders removed the pilot from his 4-point restraint by cutting the belt webbing. 

The copilot's seat was found attached to the floor structure in the remains of the cockpit. The seatback, seat pan cushions, and the 4-point restraint were consumed by the postcrash fire. The seat frame was severely damaged with broken tubes in the seatback and seat bottom. First responders found the copilot out of his seat and walking along an access road near the main wreckage area.

All six passenger seats were found scattered among the wreckage and were detached from the airplane floor structure. The seat backs and bottoms of all seats exhibited severe damage, including breakage of the structural tubing framework. The restraint systems on the passenger seats were attached to their respective seat frames, and all six buckles were unlatched. The belt webbing was intact on three of the seats, and the remaining three passenger seat restraints were consumed by fire. One of the six shoulder harnesses was found attached to the lap portion of the female buckle. The other five shoulder harnesses were found retracted in the seatback frame. None of the six passenger seat belt buckles or associated fittings were damaged.

TESTS AND RESEARCH

Enhanced Ground Proximity Warning System

The airplane was equipped with a Honeywell Mark V EGPWS. The nonvolatile memory (NVM) was downloaded, and, by design, the EGPWS recorded airplane performance data based on a parameter exceedance, which was, in this event, an excessive bank angle, most likely the result of the separation of the left wing after impact with Pole 48. The unit captured the data during the 20 seconds before the exceedance. The unit was designed to record for 10 seconds after the exceedance; however, only 2 seconds were recorded because electrical power to the unit ceased during the crash sequence.

The data indicated that during the go-around attempt, the airplane lifted off near the departure end of runway 10 (consistent with the copilot's statement). Per the EGPWS data, the landing gear remained in the down position until impact. The calibrated airspeed was about 125 knots when the airplane lifted off. The airplane continued straight ahead and slowly accelerated and gradually climbed, until a rapid pitch up was recorded, from 10.5 to 27.4 degrees within 1 second. One second later, the roll increased from 2.1 degrees left to 71.7 degrees left. 

The first data recorded by the EGPWS showed that the airplane was configured at flaps 30. The flaps were transitioning through flaps 15 at the time of impact.

Engines

During postaccident examination, the No. 1 (left) engine exhibited extensive impact deformation and was split at the interstage case flange, aft of the axial low pressure compressor (LPC). The fan blades exhibited tip bending opposite the direction of rotation, and the low pressure turbine (LPT) shaft was twisted consistent with a sudden stoppage due to impact.

The No. 2 (right) engine was intact; however, some components, including the LPC, high pressure compressor, high pressure turbine, and LPT all exhibited blade tip rubs with corresponding case rubs. The accessory gearbox tower shaft was sheared, and damage consistent with impact was noted to the fuel pump, oil lube, and scavenge pump.

Wing Spoiler System Actuators

Examination and disassembly of the lift dump actuators revealed that one unit was 0.457 inch from full extension (panel extended), and the other unit was 0.221 inch from full extension. A determination of left or right could not be made due to fire and impact damage.

Examination and disassembly of the left blow-down actuator revealed that the unit was seized at the fully extended position. Damage to the clevis at the end of the actuator was consistent with the roll/speedbrake/spoiler panel in the fully extended position at impact. The right blow-down actuator had minimal damage and was fully functional when tested. Its position at impact could not be determined. 

Examination and disassembly of the left roll control actuator revealed that the unit was 0.022 inch from the fully extended position. The right roll control actuator had minimal damage and was found to be fully functional when tested. Its position at impact was 0.201 inch from the fully extended position. 

Spoiler Control Unit

The spoiler control unit (SCU) interfaced with the hydraulics and controlled hydraulic actuation of the six spoiler panels across the wings. The SCU was responsible for providing surface position commands and monitoring hydraulic components for malfunction detection and protection. 

Exterior examination of the SCU revealed major fire and impact damage to the unit's housing. The bit and diagnostic card was also fire damaged. The data on the NVM chip were downloaded but were inconclusive; therefore, a determination of the actuation of the spoilers before and during the accident could not be made based on SCU data. 

Flight Management Computer (FMC-3000)

The airplane was equipped with a Rockwell Collins FMC-3000 flight management computer. The unit was tested and operated normally on a test bench. NVM analysis indicated that no internal faults occurred on the FMC-3000 near the time of accident. 

Air Data Computers (ADC-3000)

The airplane was equipped with two Rockwell Collins ADC-3000 air data computers (ADC). Examination revealed that the mounts on both ADCs were damaged from impact, indicative of forces during impact in excess of 20g. Both units operated normally on a test bench. The first unit showed a final power cycle with weight coming off wheels at 4 minutes after power on and weight on wheels again at 44 minutes after power on. Following the weight on wheels, within the 44th minute after power on, 3 faults were indicated in the NVM. In order, they were for a faulty Ps (static pressure) counter, a faulty Qc (impact pressure) counter, and an unexpected interruption. According to Rockwell Collins, these faults were most likely due to extreme acceleration causing electrical connections between the circuit cards within the ADC to fail. The second unit showed a final power cycle with weight coming off wheels at 4 minutes after power on and a return to weight on wheels at 44 minutes after power on. No faults were observed in the NVM. 

Airplane Performance Study

The NTSB produced an airplane performance study of the landing and go-around phases of the accident flight largely based on information from the CVR and the EGPWS, as well as the physical evidence documented at the accident site. To attain the unfactored landing distance performance numbers contained in the AFM, the following conditions had to be met: thrust as required to maintain a 3-degree approach angle, retarding thrust to idle at 50 ft agl; approach speed at VREF; flaps down; antiskid normal; maximum braking; and lift dump extended after touchdown. 

Beechcraft calculated stopping performance for several scenarios related to the accident flight. Beechcraft indicated that with the estimated stopping distance for the accident airplane with no antiskid system operative and the lowest braking action recorded during the flight test, the airplane would require about 1,560 ft to stop from the first speed recorded by the EGPWS (83 kts). This estimate decreases to 1,350 ft when moderate braking is applied. Based on EGPWS data, after touching down, the pilot did not stop the airplane within the first 2,900 ft beyond the runway 10 threshold and initiated a go-around with more than 2,400 ft of hard surface remaining; the first speed was recorded at this point. (The actual touchdown point was not recorded and could not be determined.) The wreckage examination, as well as drag estimates based on recovered EGPWS data, indicated that the lift dump remained extended during the go-around attempt. The airplane drag associated with the lift dump, flaps, and landing gear extended resulted in only marginal climb performance.

ORGANIZATIONAL AND MANAGEMENT INFORMATION

According to its website, Vein Guys® was a group of four physicians that operated several vein care centers in the southeastern United States, with offices in Augusta, Georgia; Atlanta, Georgia; Nashville, Tennessee; and Raleigh, North Carolina. According to interviews, the Pavilion Group was a subsidiary established by the owners of Vein Guys® to handle all business activities associated with the ownership and operation of its private airplane, which it used to shuttle physicians and staff between their offices in Georgia, Tennessee, and North Carolina and also for private flights to vacation destinations. 

Before owning the accident airplane, the Pavilion Group owned a King Air 300 (N401BL) and used the pilot services of Executive Shuttle (owned by the accident pilot). The Pavilion Group sold the King Air and, in June 2012, purchased the accident airplane and continued to use the pilot services of Executive Shuttle. The Pavilion Group's airplanes were operated under the provisions of 14 CFR Part 91. According to the accident pilot, the Pavilion Group paid for the pilot's initial and recurrent Premier IA ground and simulator training at FlightSafety. Although Executive Shuttle operated as Sky's the Limit, a 14 CFR Part 135 certificate holder, the pilot stated in interviews that there was no signed contract between Executive Shuttle and the Pavilion Group (or Vein Guys®) for pilot services on the Pavilion Group's airplane, and all Premier IA flights Executive Shuttle operated for the Pavilion Group were conducted under 14 CFR Part 91. 

ADDITIONAL INFORMATION

Takeoff Warning System

The airplane was equipped with a takeoff configuration warning system that provided an automatic aural warning to the flight crew during the initial portion of takeoff if the airplane was in a configuration that would not allow for a safe takeoff. The aural warning would continue until the airplane's configuration was changed to allow for safe takeoff, until action was taken by the pilot to abandon the takeoff roll, or until weight was off of the wheels. If either lift dump surface was not retracted, the speed brake/lift dump lever sensors were in the extended range, either flap position was greater than 22 degrees, or the pitch trim was outside of a predetermined range for takeoff, the aural warning would activate in the cockpit.

Antiskid System Failure and Pilot's Corrective Action

Pilots receiving training at FlightSafety on the Premier IA were taught to use the FAA approved Abbreviated Pilot Checklist to handle system malfunctions. A failure of the antiskid system was included in the Abnormal Procedures section of the checklist. According to the checklist, the pilot should move the antiskid switch to OFF and plan for a flaps 10 or flaps up landing. The antiskid failure procedure also provided a note stating that landing distance would increase about 130 percent with flaps up and 89 percent with flaps 10.

According to the Antiskid Failure Checklist (which is within the Abbreviated Pilot Checklist), the pilot was required to account for the loss of the antiskid system by applying a performance penalty to the normal landing distance, depending on the flap setting selected (flaps 10 or flaps up). Using weather conditions that prevailed at HQU at the time of the accident, the required landing distance with flaps up was 7,066 ft, and the required landing distance with flaps 10 was 5,806 ft. HQU runway 10's available runway length for landing was 5,208 ft, which did not meet the flaps up or flaps 10 performance penalty requirements, and a diversion to a longer runway would have been required. The Premier IA AFM Antiskid Fail procedure included a note that stated, "Use of flaps 20 or DN (30) for landing, with anti-skid failed, is prohibited."

The simulator instructor who provided the pilot's initial training stated in a postaccident interview that he would expect the pilot to use the written checklist for a systems failure, determine the proper flap setting for landing, and then apply the performance penalty for the landing, adding that the Antiskid Failure Checklist emphasized that the landing must be made with only flaps 10 or UP. According to the pilot's FlightSafety training records, he received antiskid system failure training during his recurrent simulator training on January 4, 2013.

On June 17, 2013, both pilots listened to the CVR recording for the accident flight, and according to subsequent interviews, neither pilot recalled seeing the ANTI SKID FAIL annunciator light illuminated on the approach. According to interviews with both pilots and a review of the CVR recording, the ANTI SKID FAIL abnormal checklist as outlined in the Abbreviated Pilot Checklist for the Premier IA was not conducted by the accident crew before landing at HQU. Further, the pilot stated that he did not think they needed the antiskid system on the landing at HQU and said the performance penalty would only apply if you were "trying to make your numbers" in the book made by the test pilots by applying maximum braking. 

Balked Landing/Go-Around

According to recorded data and witness statements, the flight crew attempted a go-around after landing at HQU. The pilot did not recall the event during interviews, while the copilot stated that they conducted a go-around after the airplane touched down. Procedures for the Premier IA (AFM and Pilot Checklist) referred to the discontinuation of a landing approach as a "balked landing."

According to the FAA's Airplane Flying Handbook (FAA-H-8083, page G-2), a balked landing was synonymous with a go-around. Per the FAA Pilot/Controller Glossary, a go around was a situation when a pilot abandons his/her approach to land. The Airplane Flying Handbook (chapter 8), "Approaches and Landings," states the following: "The go around is not strictly an emergency procedure. It is a normal maneuver that may at times be used in an emergency situation.…Although the need to discontinue a landing may arise at any point in the landing process, the most critical go-around will be one started when very close to the ground. Therefore, the earlier a condition that warrants a go-around is recognized, the safer the go around/rejected landing will be." 

According to the FAA's Aeronautical Information Manual (page PCG T-4), a touchdown was the point at which an aircraft first made contact with the landing surfaces. The Airplane Flying Handbook (FAA-H-8083-3A, page 8-7) explained that the landing process was not over until the airplane decelerated to a normal taxi speed or came to a complete stop. The FAA indicated in its May 14, 2013, response to NTSB Information Request 13-267 that a pilot may execute a balked landing/go-around if he/she determined that, after first contact with the landing surface, positive control had not been maintained or if continuing the landing process may expose the aircraft to unsafe conditions such as an unexpected appearance of hazards on the runway.

FlightSafety Premier IA instructors and evaluators in Wichita, Kansas, and Wilmington, Delaware, stated during postaccident interviews that a balked landing was an airborne maneuver typically taught to be performed at an altitude of 50 ft on the approach, and Premier pilots were not taught to execute a balked landing in the Premier IA following touchdown on the runway. The FlightSafety instructors and evaluators also stated that they discouraged students from executing a balked landing after touchdown. Beechcraft Premier IA manuals and FlightSafety training guidance for the Premier IA do not contain language prohibiting a balked landing procedure after touchdown.

The pilot told investigators that he did not recall if anyone at FlightSafety told him not to conduct a go-around or balked landing after touching down during his training. The pilot also stated that the only balked landings he conducted in training were while airborne. When asked by investigators if he recalled anyone at FlightSafety telling him not to conduct a go-around or balked landing after touching down, the pilot said "no." The pilot further stated that a balked landing was something that occurred in the air, and on the ground it was called a "touch and go." The pilot did not remember ever doing a touch and-go in the simulator and had never done one in a Premier. 

On March 29, 2011, the NTSB issued Safety Recommendation A-11-18, asking the FAA to "require manufacturers of newly certificated and in-service turbine-powered aircraft to incorporate in their Aircraft Flight Manuals a committed-to-stop point in the landing sequence (for example, in the case of the Hawker Beechcraft 125-800A airplane, once lift dump is deployed) beyond which a go-around should not be attempted." On June 10, 2013, the FAA indicated that it was impractical to fully implement the recommendation but that it would address the NTSB's concerns by issuing an Information for Operators (InFO). Pending the issuance of the InFO and the NTSB's review of an acceptable plan of action to ensure that all operators incorporate the guidance, the NTSB classified Safety Recommendation A-11-18 "Open—Acceptable Alternate Response."