Sunday, July 29, 2018

Loss of Control in Flight: Robinson R44, N479AT, accident occurred July 27, 2018 at Palm Beach County Park/Lantana Airport (KLNA), West Palm Beach, Florida

Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; West Palm Beach, Florida

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

Investigation Docket - National Transportation Safety Board:  https://dms.ntsb.gov/pubdms

Aviation Accident Data Summary - National Transportation Safety Board:  https://app.ntsb.gov/pdf

https://registry.faa.gov/N479AT

Location: Lantana, FL
Accident Number: GAA18CA450
Date & Time: 07/27/2018, 1845 EDT
Registration: N479AT
Aircraft: Robinson R44
Aircraft Damage: Substantial
Defining Event: Loss of control in flight
Injuries: 1 Minor, 1 None
Flight Conducted Under: Part 91: General Aviation - Instructional

Analysis 

The helicopter instructor reported that, during the approach to land, about 5 ft above the ground, the student pilot overcorrected and moved the cyclic "back hard and slightly right." The right rear skid contacted the ground, and the helicopter rolled to the right. The main rotor blades struck the ground, and the helicopter came to rest on its right side.

The student reported that he believed the skid strike and unusual attitude were caused by his inexperience.

The helicopter sustained substantial damage to the main rotor blades, the fuselage, and the tailboom.

The flight instructor reported that there were no preaccident mechanical failures or malfunctions with the helicopter that would have precluded normal operation. 

Probable Cause and Findings

The National Transportation Safety Board determines the probable cause(s) of this accident to be:
The student pilot's improper pitch control during landing, which resulted in a dynamic rollover.

Findings

Aircraft
Pitch control - Not attained/maintained (Cause)

Personnel issues
Aircraft control - Student pilot (Cause)
Delayed action - Instructor/check pilot

Factual Information

History of Flight

Landing
Miscellaneous/other
Abnormal runway contact
Loss of control in flight (Defining event)
Dynamic rollover
Collision with terr/obj (non-CFIT) 

Flight Instructor Information

Certificate: Flight Instructor; Commercial
Age: 39, Male
Airplane Rating(s): None
Seat Occupied: Left
Other Aircraft Rating(s): Helicopter
Restraint Used: 3-point
Instrument Rating(s): Helicopter
Second Pilot Present: Yes
Instructor Rating(s): Helicopter; Instrument Helicopter
Toxicology Performed: No
Medical Certification: Class 2 With Waivers/Limitations
Last FAA Medical Exam: 11/20/2017
Occupational Pilot: Yes
Last Flight Review or Equivalent: 08/19/2016
Flight Time:   (Estimated) 1188.3 hours (Total, all aircraft), 163.9 hours (Total, this make and model), 1136.6 hours (Pilot In Command, all aircraft), 179.2 hours (Last 90 days, all aircraft), 58.5 hours (Last 30 days, all aircraft), 3.7 hours (Last 24 hours, all aircraft)

Pilot Information

Certificate: Commercial
Age: 31, Male
Airplane Rating(s): Multi-engine Land; Single-engine Land
Seat Occupied: Right
Other Aircraft Rating(s): None
Restraint Used: 3-point
Instrument Rating(s): Airplane
Second Pilot Present: Yes
Instructor Rating(s): None
Toxicology Performed: No
Medical Certification: Class 3 With Waivers/Limitations
Last FAA Medical Exam: 06/12/2014
Occupational Pilot: No
Last Flight Review or Equivalent: 06/08/2018
Flight Time:  (Estimated) 278 hours (Total, all aircraft), 3.3 hours (Total, this make and model), 278 hours (Pilot In Command, all aircraft), 13.3 hours (Last 90 days, all aircraft), 3.3 hours (Last 30 days, all aircraft), 0.3 hours (Last 24 hours, all aircraft)

Aircraft and Owner/Operator Information

Aircraft Make: Robinson
Registration: N479AT
Model/Series: R44 Undesignated
Aircraft Category: Helicopter
Year of Manufacture: 2007
Amateur Built: No
Airworthiness Certificate: Normal
Serial Number: 1768
Landing Gear Type: Skid;
Seats: 4
Date/Type of Last Inspection: 04/04/2018, 100 Hour
Certified Max Gross Wt.: 2400 lbs
Time Since Last Inspection:
Engines: 1 Reciprocating
Airframe Total Time: 3720.8 Hours as of last inspection
Engine Manufacturer: Lycoming
ELT: Not installed
Engine Model/Series: O-540-F1B5
Registered Owner: Airmen Testing And Training Inc Dba
Rated Power: 225 hp
Operator: Airmen Testing And Training Inc Dba
Operating Certificate(s) Held: Pilot School (141) 

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light: Day
Observation Facility, Elevation: KPBI, 21 ft msl
Distance from Accident Site: 6 Nautical Miles
Observation Time: 2247 UTC
Direction from Accident Site: 352°
Lowest Cloud Condition: Few / 3500 ft agl
Visibility:  10 Miles
Lowest Ceiling: Broken / 20000 ft agl
Visibility (RVR):
Wind Speed/Gusts: 6 knots /
Turbulence Type Forecast/Actual: None / None
Wind Direction: 130°
Turbulence Severity Forecast/Actual: N/A / N/A
Altimeter Setting: 30.04 inches Hg
Temperature/Dew Point: 29°C / 24°C
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: Lantana, FL (LNA)
Type of Flight Plan Filed: None
Destination: Lantana, FL (LNA)
Type of Clearance: None
Departure Time: 1815 EDT
Type of Airspace: Class G

Airport Information

Airport: PALM BEACH COUNTY PARK (LNA)
Runway Surface Type: Asphalt
Airport Elevation: 14 ft
Runway Surface Condition: Dry 
Runway Used: 16
IFR Approach: None
Runway Length/Width: 3421 ft / 100 ft
VFR Approach/Landing: Full Stop; Traffic Pattern

Wreckage and Impact Information

Crew Injuries: 1 Minor, 1 None
Aircraft Damage: Substantial
Passenger Injuries: N/A
Aircraft Fire: None
Ground Injuries: N/A
Aircraft Explosion: None
Total Injuries: 1 Minor, 1 None
Latitude, Longitude:  26.592778, -80.085278 (est)



 



LANTANA, Fla. - Two people suffered minor injuries following a small helicopter crashed at Lantana Airport Friday, according to Palm Beach County Fire Rescue. 

Crews arrived at the scene at 7 p.m. and found the small helicopter resting on its side. 

Two people on board the aircraft were evaluated by paramedics and treated for minor injuries. They did not require to be transported to a hospital, officials say.

The cause of the crash is being investigated by the Federal Aviation Administration. 

Original article can be found here ➤ https://www.wptv.com

Flightstar SC II, registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as personal flight, N953RJ: Accident occurred July 27, 2018 near Concord Airpark (2G1), Lake County, Ohio

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:

Federal Aviation Administration / Flight Standards District Office; Cleveland, Ohio

Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf


Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms


http://registry.faa.gov/N953RJ    

Location: Painesville, OH
Accident Number: CEN18LA301
Date & Time: 07/27/2018, 1645 EDT
Registration: N953RJ
Aircraft: FLIGHTSTAR SC II
Aircraft Damage: Substantial
Defining Event: Loss of engine power (partial)
Injuries: 1 Serious, 1 Minor
Flight Conducted Under: Part 91: General Aviation - Personal 

On July 27, 2018, about 1645 eastern daylight time, a Flightstar SC II, N953RJ, sustained substantial damage when it impacted terrain during approach to land on runway 2 at the Concord Airpark (2G1), near Painesville, OH. The student pilot received serious injuries and his passenger received minor injuries. The airplane was registered to and operated by the pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as personal flight. Visual meteorological conditions prevailed for the flight, which was not on a flight plan. The local flight was originating at the time of the accident.

The pilot reported that he had purchased the airplane a few months prior to the accident and had performed some repairs in the interim, including replacing a broken propeller. He said that he planned to have the repairs inspected by a certificated mechanic and the airplane had not been flown since its purchase. On the day of the accident, the pilot and his spouse were performing taxi practice with no intention for flight. He said that they were taking turns with the controls. He said that on one of his turns he must have gone too fast and the airplane unexpectedly became airborne. When this happened, the airplane was already 3/4 of the way down the runway and he didn't think there was enough room to land on the remaining runway, so he elected to "go around". The pilot was unable to maintain altitude and maneuvered the airplane to land but struck trees during the attempted landing. In his report the pilot indicated that there were no mechanical failures or malfunctions of the airplane.

In a telephone conversation the pilot reported that he had set the propeller blade pitch angles based on information from the airplane maintenance records using a digital protractor. He acknowledged that his method of setting the propeller blade angles could have been slightly off. He had intended to have a certified mechanic check his work but that had not been done since he had not intended to fly the airplane when the accident occurred.

The weather conditions at the Willoughby Lost Nation Municipal Airport, Willoughby, Ohio, about the time of the accident included a temperature of 23° C, a dew point of 12° C, and an altimeter setting of 29.98 inches of mercury. The carburetor icing susceptibility at these readings is moderate icing at cruise power settings, and serious icing at descent power settings. The calculated density altitude was 2,273 ft. 

Pilot Information

Certificate: Student
Age: 31, Male
Airplane Rating(s): None
Seat Occupied: Left
Other Aircraft Rating(s):None 
Restraint Used:
Instrument Rating(s): None
Second Pilot Present: No
Instructor Rating(s):None 
Toxicology Performed:No 
Medical Certification: Class 3 Without Waivers/Limitations
Last FAA Medical Exam: 02/02/2015
Occupational Pilot: No
Last Flight Review or Equivalent:
Flight Time:   21 hours (Total, all aircraft), 0 hours (Total, this make and model), 0 hours (Pilot In Command, all aircraft), 9 hours (Last 90 days, all aircraft), 9 hours (Last 30 days, all aircraft), 1.5 hours (Last 24 hours, all aircraft)

Aircraft and Owner/Operator Information

Aircraft Make: FLIGHTSTAR
Registration: N953RJ
Model/Series: SC II
Aircraft Category: Airplane
Year of Manufacture: 2001
Amateur Built: No
Airworthiness Certificate: Special Light-Sport
Serial Number: 325
Landing Gear Type: Tricycle
Seats: 2
Date/Type of Last Inspection:
Certified Max Gross Wt.:  998 lbs
Time Since Last Inspection:
Engines: 1 Reciprocating
Airframe Total Time:
Engine Manufacturer: HKS
ELT: C91A installed, not activated
Engine Model/Series: 700E
Registered Owner: On file
Rated Power: 60 hp
Operator: On file
Operating Certificate(s) Held: None

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light: Day
Observation Facility, Elevation: LNN, 626 ft msl
Distance from Accident Site: 8 Nautical Miles
Observation Time: 1655 EDT
Direction from Accident Site: 270°
Lowest Cloud Condition: Scattered / 9000 ft agl
Visibility:  10 Miles
Lowest Ceiling: Overcast / 11000 ft agl
Visibility (RVR):
Wind Speed/Gusts: 3 knots /
Turbulence Type Forecast/Actual: /
Wind Direction: 310°
Turbulence Severity Forecast/Actual: /
Altimeter Setting: 29.98 inches Hg
Temperature/Dew Point: 23°C / 12°C
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: Painesville, OH (2G1)
Type of Flight Plan Filed: None
Destination: Painesville, OH (2G1)
Type of Clearance: None
Departure Time: 1645 EDT
Type of Airspace: Class G

Airport Information

Airport: Concord Airpark (2G1)
Runway Surface Type: Asphalt
Airport Elevation: 998 ft
Runway Surface Condition: Dry
Runway Used: 2
IFR Approach: None
Runway Length/Width: 2181 ft / 38 ft
VFR Approach/Landing: Traffic Pattern

Wreckage and Impact Information

Crew Injuries: 1 Serious
Aircraft Damage: Substantial
Passenger Injuries: 1 Minor
Aircraft Fire: None
Ground Injuries:N/A 
Aircraft Explosion: None
Total Injuries: 1 Serious, 1 Minor

Latitude, Longitude:  41.666944, -81.197222

Location: Painesville, OH
Accident Number: CEN18LA301
Date & Time: 07/27/2018, 1700 EDT
Registration: N953RJ
Aircraft: FLIGHTSTAR SC II
Injuries: 1 Serious, 1 Minor
Flight Conducted Under: Part 91: General Aviation - Personal

On July 27, 2018, about 1700 eastern daylight time, a Flightstar SC II, N593RJ, sustained substantial damage when it impacted terrain during approach to land on runway 2 at the Concord Airpark (2G1), near Painesville, OH. The pilot received serious injuries and his passenger received minor injuries. The airplane was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as personal flight. Visual meteorological conditions prevailed for the flight, which was not on a flight plan. The local flight was originating at the time of the accident.


Aircraft and Owner/Operator Information


Aircraft Make: FLIGHTSTAR

Registration: N953RJ
Model/Series: SC II
Aircraft Category: Airplane
Amateur Built: No
Operator: On file
Operating Certificate(s) Held: None

Meteorological Information and Flight Plan


Conditions at Accident Site: Visual Conditions

Condition of Light: Day
Observation Facility, Elevation: LNN, 626 ft msl
Observation Time: 1655 EDT
Distance from Accident Site: 8 Nautical Miles
Temperature/Dew Point: 23°C / 12°C
Lowest Cloud Condition: Scattered / 9000 ft agl
Wind Speed/Gusts, Direction: 3 knots / , 310°
Lowest Ceiling: Overcast / 11000 ft agl
Visibility: 10 Miles
Altimeter Setting: 29.98 inches Hg
Type of Flight Plan Filed: None
Departure Point: Painesville, OH (2G1)
Destination:  Painesville, OH (2G1)

Wreckage and Impact Information


Crew Injuries: 1 Serious

Aircraft Damage: Substantial
Passenger Injuries: 1 Minor
Aircraft Fire: None
Ground Injuries: N/A
Aircraft Explosion: None
Total Injuries: 1 Serious, 1 Minor
Latitude, Longitude:  41.666944, -81.197222




This evening, July 27th, just after 5 PM, the Lake County Sheriff’s Office responded to a reported plane crash in Concord Twp. Upon arrival deputies found that an ultralight plane made an emergency landing in a wooded area behind the homes on Summerwood Drive in Concord Township. Both the male and female passengers have been transported to the hospital for evaluation by Concord Township Fire. 


 Although this accident is in our patrol area it will be investigated by the Ohio State Highway patrol who is responsible for investigating such plane accidents. Future inquiries regarding this accident can be referred to the Ohio State highway patrol post in Chardon.


Chief Deputy Frank Leonbruno




CONCORD TOWNSHIP, Ohio - An ultralight aircraft made an emergency landing in a wooded area in Concord Township, and two people were taken to a hospital, authorities said.


Just after 5 p.m., the Lake County Sheriff’s Office responded to a reported plane crash. Upon arrival at a wooded area behind homes on Summerwood Drive, deputies found the ultralight aircraft, according to a Facebook post by the sheriff’s office.


A man and a woman were taken to a nearby hospital for evaluation by Concord Township Fire, the post states.


Original article ➤ https://www.news5cleveland.com

Low Altitude Operation/Event: Aeronca 7AC, N85506; fatal accident occurred July 28, 2018 in Alexandria, Douglas County, Minnesota

Accident Site Overview. 

Accident Site Overview With Damaged Power Line and Utility Pole.

Main Wreckage.

Right Main Landing Gear.

Left Main Landing Gear.

Engine Overview (Right Side).

Engine Overview (Left Side).

Propeller Tip “A”.

Propeller Tip “B”.

Google Earth overlay of the recorded Track Log for the entire flight.

Google Earth overlay of the recorded Track Log at the end of the accident flight. Times prior to 00:20:14 UTC are shown.

Google Earth overlay of the recorded Track Log at the end of the accident flight. Times from 00:20:14 UTC onward are shown.


The National Transportation Safety Board traveled to the scene of this accident.

Additional Participating Entity:

Federal Aviation Administration / Flight Standards District Office; Minneapolis, Minnesota

Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf


Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

http://registry.faa.gov/N85506 

Location: Alexandria, MN
Accident Number: CEN18FA297
Date & Time: 07/28/2018, 1920 CDT
Registration: N85506
Aircraft: Aeronca 7AC
Aircraft Damage: Substantial
Defining Event: Low altitude operation/event
Injuries: 1 Fatal
Flight Conducted Under: Part 91: General Aviation - Personal 

On July 28, 2018, at 1920 central daylight time, an Aeronca 7AC airplane, N85506, was substantially damaged when it was involved in an accident near Alexandria, Minnesota. The private pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

According to track data recovered from the pilot's mobile telephone, the flight departed from Chandler Field Airport (AXN), Alexandria, Minnesota, at 1915, and flew north and climbed to a maximum altitude of 1,870 ft mean sea level (msl) (about 478 ft above the ground) before it entered a left descending turn. At 1917:20, the airplane flew over the north shore of a lake on a southwest course, at an altitude of 1,722 ft mean sea level (about 330 ft above the ground), and at a groundspeed of 80 knots. At 1918:00, the airplane continued on a southwest course over the lake at an altitude of 1,372 ft msl (about 12 ft above the surface) and a groundspeed of 74 knots. At 1919:40, the airplane made a left turn. The airplane was still about 12 ft above the lake while flying parallel to the shoreline on a south-southeast course. The airplane then made a left turn. At 1919:20, the airplane flew over the southwest shoreline while on a west-northwest course; the airplane's altitude remained at 1,372 ft msl, and its groundspeed increased to 78 knots. The airplane continued to the west-northwest and then turned north. At 1920:07, the airplane was heading north while at an altitude of 1,415 ft msl (about 13 ft above the ground) and at a groundspeed of 73 knots. The airplane's groundspeed decelerated to zero shortly afterward.

The airplane wreckage was located near the airplane's last recorded position in an area with multiple power lines that had been struck and a fractured power line pole.

Multiple witnesses saw and/or heard the airplane before the accident. Two witnesses reported that the airplane had approached their cabin (on the north shore of the lake) from the northeast and overflew the cabin at treetop level, which they estimated to be about 50 ft above the ground. One of these witnesses stated that the airplane had "barely cleared the trees" when it overflew his cabin. The witnesses reported that the airplane then descended below treetop level while flying south over the lake. The witnesses stated that they observed the airplane complete at least two low passes over a house located at the southwest side of the lake.

Another witness, who was a friend of the pilot, owned the house on the southwest side of the lake that was referenced by the two witnesses. This witness was inside his house when he heard an airplane overfly the house. The witness reported that the pilot would often overfly his house at a low altitude. The witness stated that the engine sounded normal when the airplane overflew his house. The accident site was located about 1 mile north-northwest of his house.

Three additional witnesses, located about ¼ mile northeast of the accident site, reported seeing the airplane approach their position at a low altitude. The witnesses reported that the airplane was flying toward the northwest when it descended behind a small ridge and collided with power lines. Two of these witnesses reported that they couldn't hear the engine as the airplane approached their position, but they noted that music was playing in the background at the time. The witnesses reported that the music should not have precluded them from hearing engine sounds because they were able to hear a "thud" when the airplane impacted the ground.

Pilot Information

Certificate: Private
Age: 64, Male
Airplane Rating(s): Single-engine Land; Single-engine Sea
Seat Occupied: Front
Other Aircraft Rating(s): None
Restraint Used:
Instrument Rating(s): Airplane
Second Pilot Present: No
Instructor Rating(s): None
Toxicology Performed:Yes 
Medical Certification: Class 3 With Waivers/Limitations
Last FAA Medical Exam: 10/28/2016
Occupational Pilot: No
Last Flight Review or Equivalent:
Flight Time: (Estimated) 500 hours (Total, all aircraft) 

The pilot's logbook was not recovered, so the pilot's recent flight experience and his number of hours flying the accident airplane make and model could not be determined.

Aircraft and Owner/Operator Information

Aircraft Make: Aeronca
Registration: N85506
Model/Series: 7AC
Aircraft Category: Airplane
Year of Manufacture: 1946
Amateur Built: No
Airworthiness Certificate: Normal
Serial Number: 7AC-4246
Landing Gear Type: Tailwheel
Seats: 2
Date/Type of Last Inspection: 06/28/2018, Annual
Certified Max Gross Wt.: 1300 lbs
Time Since Last Inspection: 12 Hours
Engines: 1 Reciprocating
Airframe Total Time: 5991.72 Hours at time of accident
Engine Manufacturer: Continental
ELT: C91 installed, not activated
Engine Model/Series: C90-8F
Registered Owner: Jeffrey M. McManigle
Rated Power:90 hp 
Operator:On file 
Operating Certificate(s) Held: None

The maintenance records showed no unresolved airworthiness issues. 

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light: Day
Observation Facility, Elevation: AXN, 1425 ft msl
Distance from Accident Site: 3 Nautical Miles
Observation Time: 1853 CDT
Direction from Accident Site: 113°
Lowest Cloud Condition: Clear
Visibility:  10 Miles
Lowest Ceiling: None
Visibility (RVR):
Wind Speed/Gusts: 4 knots /
Turbulence Type Forecast/Actual: None / None
Wind Direction: 350°
Turbulence Severity Forecast/Actual: N/A / N/A
Altimeter Setting: 30.13 inches Hg
Temperature/Dew Point: 26°C / 12°C
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: Alexandria, MN (AXN)
Type of Flight Plan Filed: None
Destination: Alexandria, MN (AXN)
Type of Clearance: None
Departure Time: 1915 CDT
Type of Airspace: Class E

At the time of the accident, the sun was about 14.85° above the horizon to the west-northwest (281.92°). Sunset was at 2056 on the day of the accident. 

Wreckage and Impact Information

Crew Injuries: 1 Fatal
Aircraft Damage: Substantial
Passenger Injuries: N/A
Aircraft Fire: None
Ground Injuries: N/A
Aircraft Explosion: None
Total Injuries: 1 Fatal
Latitude, Longitude: 45.882500, -95.449722 

The main wreckage was located in a grass drainage ditch northwest of the airplane's last recorded position. Multiple power lines and a power pole had been struck and were lying across a road on a northwest heading. The main wreckage consisted of the entire airplane, which was found inverted in the drainage ditch facing south. There was no evidence of fire.

Flight control cable continuity was established from each flight control surface to its respective cockpit control. Both main landing gear oleo-struts and the propeller exhibited damage consistent with an in-flight wire impact. There was no evidence of a wire strike on either wing or the empennage.

The forward seat throttle was positioned about three-quarters of full travel. The primer control was pushed in and secured. The magneto switch was in the BOTH position. The carburetor heat control and the cabin heat control were in the OFF position. The airplane's only circuit breaker was not tripped.

The fuel shutoff valve was in the ON position. The fuel caps were remained secured on all fuel tanks. Fuel was observed in the main/header tank and both auxiliary wing tanks. Collected fuel samples had a color (blue) and a smell consistent with 100 low-lead aviation fuel and did not exhibit any evidence of water or particulate contamination. The fuel selectors for the auxiliary wing tanks were in the OFF position. A functional test of the fuel shutoff valve revealed no anomalies and confirmed that fuel flow was from the main/header tank. The fuselage-mounted gascolator had shattered during impact, and fuel was observed flowing from the fuel supply line.

The engine remained attached to the firewall. The propeller remained attached to the propeller flange. One propeller blade was bent aft about midspan and exhibited chordwise scratching and leading edge gouging that were consistent with an in-flight wire strike. The other propeller blade exhibited a slight aft bend, a single leading edge gouge, and minor chordwise scratching near the blade tip. Internal engine and valve train continuity were confirmed by rotating the propeller. Compression and suction were noted on all cylinders along with crankshaft rotation, and acceptable cylinder pressures were measured using a differential pressure gauge. The induction manifold and intake pipes exhibited signatures of normal operation with no excessive fuel staining observed.

The upper spark plugs were removed and were found to exhibit features consistent with normal engine operation. A borescope inspection of each cylinder revealed no anomalies with the cylinders, pistons, valves, valve seats, or lower spark plugs. The right magneto remained attached to its installation point and provided spark on all posts while the crankshaft was rotated. The left magneto remained attached to the engine, but the impulse coupling did not function as the crankshaft was rotated. The left magneto was removed and provided a spark on all posts when manually rotated. Right magneto-to-engine timing was confirmed to be at the top center on the No. 1 cylinder.

A teardown of the engine revealed no internal component failures. Adequate lubrication oil was observed throughout the engine, and no evidence indicated oil starvation or excessive heat. No metal material was observed after a magnet was passed through the engine sump. The oil filter tube pickup and oil filter screen were free of metallic material. Throttle control cable continuity was confirmed from the cockpit to the carburetor throttle arm. The carburetor mixture arm was safety-wired in the full rich position. The carburetor bowl did not contain evidence of water or particulate contamination. Disassembly of the carburetor revealed no anomalies with the single-piece venturi, metal floats, or needle valve.

Postaccident examination of the airframe and engine revealed no anomalies that would have precluded normal operation during the flight.

Medical And Pathological Information

The Midwest Medical Examiner's Office, Ramsey, Minnesota, performed an autopsy of the pilot. His cause of death was blunt-force injuries. Toxicology testing performed at the FAA Forensic Sciences Laboratory identified 0.029 gm/dl of ethanol in the pilot's blood specimens, 0.053 gm/dl of ethanol in the pilot's vitreous specimens, and naproxen in the pilot's urine specimens.

Ethanol is the intoxicant commonly found in beer, wine, and liquor. Ethanol acts as a central nervous system depressant. After ingestion at low doses, ethanol impairs judgment, psychomotor functioning, and vigilance; at higher doses, ethanol can cause coma and death. The effects of ethanol on aviators are generally well understood; it significantly impairs pilots' performance, even at very low levels. Because ingested alcohol is distributed throughout the body, levels from different postmortem tissues are usually similar. Ethanol may also be produced in body tissues by postmortem microbial activity, but intact vitreous is relatively protected from the effects of microbial activity. Because of the characteristics of the wall of eye globe, ethanol may be slow to collect in vitreous, and levels may drop more slowly than blood levels after alcohol ingestion has stopped.

FAA regulation (14 CFR 91.17) prohibits any person from acting or attempting to act as a crewmember of a civil aircraft while having 0.040 gm/dl or more ethanol in the blood.

Naproxen, often marketed with the brand name Aleve, is a mild anti-inflammatory drug available over the counter. It is not considered impairing.
========
Location: Alexandria, MN
Accident Number: CEN18FA297
Date & Time: 07/28/2018, 1923 CDT
Registration: N85506
Aircraft: Aeronca 7AC
Injuries: 1 Fatal
Flight Conducted Under:  Part 91: General Aviation - Personal 

On July 28, 2018, about 1923 central daylight time, an Aeronca 7AC single-engine airplane, N85506, impacted powerlines and terrain while maneuvering at a low altitude near Alexandria, Minnesota. The pilot was fatally injured, and the airplane was substantially damaged. The airplane was registered to a private individual and operated by the private pilot under the provisions of Title 14 Code of Federal Regulations (CFR) Part 91 as a personal flight. Day visual meteorological conditions prevailed at the time of the accident. The local area flight departed Chandler Field Airport (AXN), Alexandria, Minnesota, about 1918.

There were multiple witnesses who saw and/or heard the airplane flying at low altitude before the accident. Two witnesses reported that the airplane had approached their cabin on the north shore of Lake Latoka from the northeast and overflew their cabin at treetop level, which they estimated to be about 50 ft above the ground. One witness stated that the airplane had "barely cleared the trees" when the airplane overflew his cabin. The witnesses reported that the airplane then descended below treetop level while flying south over Lake Latoka. The witnesses stated that they observed the airplane complete at least two low passes over a house located at the southwest side of the lake.

Another witness, who acknowledged being a friend of the pilot, owned the house located on the southwest side of Lake Latoka. The witness was inside his house eating dinner when he heard an airplane overfly his house. He reported that it was common for the pilot to overfly his house at a low altitude. The witness stated that the airplane's engine sounded normal when it overflew his house. He noted that he had a "very bad feeling" that the airplane had crashed when his house lights flickered shortly after the airplane overflew his house. The accident site was located about a mile north-northwest of his house.

Three additional witnesses reported seeing the airplane approach their position, about 1/4 mile northeast of the accident site, at a low altitude and slow airspeed. These witnesses reported that the airplane was flying toward the northwest when it descended behind a small ridge and collided with powerlines. Two of the witnesses reported that they couldn't hear the engine as the airplane approached their position; however, they noted they had music playing at the time. The witnesses reported that they heard an audible "thud" when the airplane impacted the ground.

The accident site was located in a grass drainage ditch northwest of the intersection of Townhall Road and 10th Avenue SW. There were multiple powerlines and a fractured power pole strung across the road on a northwest heading. The main wreckage, which consisted of the entire airplane, was found inverted in the drainage ditch facing south. There was no evidence of an inflight or postimpact fire. Flight control cable continuity was established from each flight control surface to its respective cockpit control. Both main landing gear oleo-struts and the propeller exhibited damage consistent with an inflight wire impact. There was no evidence of a wire strike on either wing or the empennage. The recording tachometer indicated 2,665.72 hours. The forward seat throttle was positioned about 3/4 full travel. The airplane was not equipped with a mixture control. The primer control was IN and secured. The magneto switch was on BOTH. The carburetor heat control was OFF. The cabin heat control was OFF. The airplane was not equipped with an electric master switch, but the single 10 ampere circuit breaker was not tripped. The single communication radio was selected to the common traffic advisory frequency (123.0 megahertz). The airplane was not equipped with a transponder. The fuel shutoff valve was ON. Fuel was recovered from the main/header tank and both right and left auxiliary wing tanks. The fuel samples were blue in color and had an odor consistent with 100 low-lead aviation fuel. The fuel caps were installed and secured on all fuel tanks. The fuel selectors for the auxiliary wing tanks were in the OFF position. A functional test of the fuel shutoff valve did not reveal any anomalies and confirmed fuel flow from the main/header tank. The fuselage mounted gascolator had shattered during impact and fuel was observed flowing from the fuel supply line. The postaccident examination did not reveal any anomalies that would have precluded normal airplane operation during the flight.

The engine remained attached to the firewall. The propeller remained attached to the propeller flange. One propeller blade was bent aft about midspan and exhibited chordwise scratching and leading-edge gouging that was consistent with an inflight wire strike. The other propeller blade exhibited a slight aft bend, a single leading-edge gouge, and minor chordwise scratching near the blade tip. Internal engine and valve train continuity were confirmed as the propeller was rotated. Compression and suction were noted on all cylinders in conjunction with crankshaft rotation, and acceptable cylinder pressures were measured using a differential pressure gauge. The induction manifold and intake pipes exhibited signatures of normal operation, with no excessive fuel staining observed. The upper spark plugs were removed and exhibited features consistent with normal engine operation. A borescope inspection of each cylinder did not reveal any anomalies with the cylinders, pistons, valves, valve seats, or lower spark plugs. The right magneto attached to its installation point and provided spark on all posts while the crankshaft was rotated. The left magneto remained attached to the engine; however, the impulse coupling did not function as the crankshaft was rotated. The left magneto was removed and provided a spark on all posts when rotated by hand. Right magneto-to-engine timing was confirmed to be at top-dead-center on the number 1 cylinder. A full teardown of the engine did not reveal any internal component failures. Adequate lubrication oil was observed throughout the engine and there was no evidence of oil starvation or excessive heat. No metal material was observed after a magnet was passed through the engine sump. The oil filter tube pickup and oil filter screen were free of metallic material. Throttle control cable continuity was confirmed from the cockpit to the carburetor throttle arm. The carburetor mixture arm was safety-wired in the full rich position. The carburetor bowl contained about 1/2 fluid ounce of fuel; however, the airplane had been inverted for nearly 24 hours before being recovered. The carburetor bowl did not contain evidence of water or particulate contamination. Disassembly of the carburetor did not reveal any anomalies with the single-piece venturi, metal floats, or needle valve. The postaccident examination did not reveal any anomalies that would have precluded normal engine operation during the flight.

According to FAA records, the 64-year-old pilot held a private pilot certificate with single-engine land airplane, single-engine sea airplane, and instrument airplane ratings. His most recent FAA third-class medical certificate was issued on October 28, 2016, with a limitation for corrective lenses. A search of FAA records showed no previous accidents, incidents, or enforcement proceedings. A pilot logbook was not recovered during the on-scene investigation.

The 1946-model-year airplane, serial number 7AC-4246, was a high-wing monoplane of fabric-covered steel tube and wood construction. The airplane was powered by a 90-horsepower, 4-cylinder, Continental C90-8F reciprocating engine, serial number 47229-9-8. The engine provided thrust through a fixed-pitch, two-blade, Sensenich 76AK-2-43 propeller, serial number 23704. The two-seat airplane was equipped with a fixed conventional landing gear. The airplane had a maximum allowable takeoff weight of 1,300 pounds. According to maintenance documentation, the last annual inspection was completed on June 28, 2018, at 5,980 total airframe hours. The airplane had accumulated 11.72 hours since the last annual inspection. The airframe had accumulated a total service time of 5,991.72 hours when the accident occurred. The engine had accumulated 791.72 hours since being overhauled on January 17, 1978. A postaccident review of the maintenance records found no history of unresolved airworthiness issues.

A postaccident review of available meteorological data established that day visual meteorological conditions prevailed at the accident site. The nearest aviation weather reporting station was located at Chandler Field Airport (AXN) about 3 miles southeast of the accident site. At 1853, about 30 minutes before the accident, the AXN automated surface observing system reported: wind 350° at 4 knots, 10 miles surface visibility, a clear sky, temperature 26°C, dew point 12°C, and an altimeter setting 30.13 inches of mercury.

Aircraft and Owner/Operator Information

Aircraft Make: Aeronca
Registration: N85506
Model/Series: 7AC
Aircraft Category: Airplane
Amateur Built: No
Operator: On file
Operating Certificate(s) Held: None 

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light: Day
Observation Facility, Elevation: AXN, 1425 ft msl
Observation Time: 1853 CDT
Distance from Accident Site: 3 Nautical Miles
Temperature/Dew Point: 26°C / 12°C
Lowest Cloud Condition: Clear
Wind Speed/Gusts, Direction: 4 knots / , 350°
Lowest Ceiling: None
Visibility:  10 Miles
Altimeter Setting: 30.13 inches Hg
Type of Flight Plan Filed: None
Departure Point: Alexandria, MN (AXN)
Destination: Alexandria, MN (AXN)

Wreckage and Impact Information

Crew Injuries: 1 Fatal
Aircraft Damage: Substantial
Passenger Injuries: N/A
Aircraft Fire: None
Ground Injuries: N/A
Aircraft Explosion: None
Total Injuries: 1 Fatal
Latitude, Longitude:  45.882500, -95.449722


Kenneth "Ken" James Ryan
JULY 18, 1954 ~ JULY 28, 2018 (AGE 64)

Ken Ryan age 64, of Alexandria, died on Saturday, July 28th, 2018.  Memorial service will be held on Saturday, August 4, 2018, 10:00 a.m. at the United Methodist Church in Alexandria.  Visitation will be held on Friday, August 3, 2018, 4:00 - 7:00 PM at the Anderson Funeral Home and one hour prior to the service at the church on Saturday.

https://www.andersonfuneral.net



(Alexandria, MN)  A pilot is dead following a Saturday evening plane crash near Alexandria.  Authorities have now identified the pilot as 64 year old Kenneth James Ryan of Alexandria.  Ryan was an instructor at Alexandria Technical and Community College.  He also served on several committees including the Alexandria Planning Commission and was a member of the Alexandria Municipal Airport Commission.  He was also a Computer Repair Technologist in the U.S. Air Force before being honorably discharged in 1976.  Ken is a retired Adult and Pediatric Urologic Surgeon as well.  


The plane appears to have flown into an REA power pole.  Ryan was alone in the plane.  The aircraft landed on its roof on the west side of Town Hall Road, near the intersection of 10th Avenue SW.  Power lines were scattered on the road.  Medical personnel arrived on scene and found the sole occupant of the plane to be deceased.


Saturday night's plane crash took out power for nearly an hour. Friends gathered at the crash site Sunday morning say Ken was an experienced pilot.  FAA records indicate the aircraft was a 1946 fixed wing single-engine plane.


The crash took place after 7:00pm, about 24 hours after another plane crashed in the southeast side of Lake Winona.  On Friday night, a pilot was doing "touch and goes" from the Alexandria Airport when his plane lost power. That pilot was able to get out of the aircraft and was not injured.


Local authorities contacted the Federal Aviation Administration and the National Transportation Safety Board to handle the investigation.


Original article ➤  https://www.voiceofalexandria.com








Authorities have released the name of a pilot who died after his airplane sheared off a power pole and crashed west of Alexandria Saturday night.

His name is Kenneth James Ryan, 64, of Alexandria. Ryan was an instructor at the Alexandria Technical and Community College, and served on the Alexandria Planning Commission.  

The small aircraft ended up on its roof in a ditch near the intersection of Town Hall Road and 10th Avenue SW in LaGrand Township shortly before 7:30 pm.

Three ambulances arrived on scene but left without transporting anyone. The Douglas County Sheriff's Office confirmed that Ryan, who flying alone, died in the crash.

Within minutes of the crash being reported, several other vehicles were parked on Town Hall Road with their lights flashing, including those from the Douglas County Sheriff's Office, the Alexandria Police Department, State Patrol and Alexandria Fire Department.

Downed powerlines were also on the road.

Local authorities contacted the Federal Aviation Administration and the National Transportation Safety Board to handle the investigation.

It was the second airplane crash near Alexandria in two days. At about 7 p.m. Friday night, a pilot was conducting "touch and goes" from the Alexandria Airport when his single-engine Piper Archer lost power and he crash-landed on the southwest side of Lake Winona, about a mile southeast of Saturday's crash. He was able to get out of the aircraft and was not injured.

Original article can be found here ➤ http://www.echopress.com