Thursday, October 01, 2015

Beechcraft D55 Baron, Major Aviation LLC, N7641N: Fatal accident occurred August 03, 2013 in Conway, South Carolina

A brief released by the National Transportation Safety Board on September 29 regarding a plane crash in Conway that killed three shows that the pilot didn't put the right amount of fuel in the airplane before taking off.

The report says that the right fuel tank had about five gallons remaining which was below the minimum required for takeoff.

Instead of landing after the approach, "the pilot chose to continue the flight and return to his home airport. While on final approach for landing and about 600 feet above the ground, the airplane made a steep, 270-degree right turn, departed controlled flight, and crashed at the entrance to a housing development."

The report says that the pilot likely did not follow the checklist procedures for a loss of single engine power and that he then lost control of the airplane.

The NTSB also looked at the pilot's medical records that revealed that he had been prescribed medications for the treatment of depression and anxiety, and toxicological testing the presence of a drug to treat depression in the pilot's liver and blood. However, based on the evidence, it is unlikely that the pilot was impaired by depression or the medication he used to treat it at the time of the accident.

The three killed in the crash were identified as James Major, 39, of Conway, Kenneth Piuma, 42, of Myrtle Beach and Donald Dale Becker, 16, of Conway.

NTSB Air safety investigator Jay Neylon said at the time of the crash that the plane took off at the Conway-Horry County Airport, went to the Myrtle Beach Airport and was returning to Conway when it crashed

Source: http://wpde.com


http://dms.ntsb.gov

http://registry.faa.gov/N7641N

NTSB Identification: ERA13FA348

14 CFR Part 91: General Aviation
Accident occurred Saturday, August 03, 2013 in Conway, SC
Probable Cause Approval Date: 09/29/2015
Aircraft: BEECH D55, registration: N7641N
Injuries: 3 Fatal.

NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

After departing on the accident flight, the pilot performed a practice instrument approach to an airport located about 25 minutes away. Onboard video taken during the final portion of the approach showed that the right main fuel tank had about 5 gallons of fuel remaining (about 20 minutes of flight at the computed consumption rate), which was below the minimum fuel quantity specified for takeoff in the pilot's operating handbook (POH). Instead of landing after the approach, the pilot chose to continue the flight and return to his home airport. While on final approach for landing and about 600 ft above the ground, the airplane made a steep, 270-degree right turn, departed controlled flight, and crashed at the entrance to a housing development.

Examination of both engines and their propellers revealed evidence consistent with the left engine operating at high power and with the right engine operating at low or possibly no power at impact. Disassembly of each engine revealed no evidence of any preimpact mechanical malfunctions or failures. Based on the limited fuel in the right main fuel tank on the previous approach and the lack of power at impact, it is likely that the right engine lost power due to fuel starvation.

All of the engine controls were found full-forward in their quadrants, and the right engine propeller was not feathered. The POH engine failure checklist stated that the controls on the inoperative engine should be closed and that the inoperative engine should be feathered. The POH also noted that, in the event of an engine failure, it is necessary "to maintain lateral and directional control" by operating the airplane above the single-engine minimum controllable airspeed (Vmca). The published Vmca for the accident airplane was 80 knots, and performance calculations revealed that the airplane slowed to below 80 knots. Based on the airplane's configuration at impact and the performance calculations, it is likely that the pilot did not follow the POH checklist procedures for a loss of single engine power and that he subsequently lost control of the airplane.

A review of the pilot's medical records revealed that he been prescribed medications for the treatment of depression and anxiety, and toxicological testing revealed the presence of sertraline, a medication used to treat depression, in the pilot's liver and blood. However, based on the evidence, it is unlikely that the pilot was impaired by depression or the medication he used to treat it at the time of the accident.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot's loss of airplane control, which resulted from his failure to follow the loss of single engine power checklist procedures after a total loss of right engine power due to fuel starvation. Contributing to the accident was the pilot's improper preflight fuel planning and in-flight fuel management.

***This report was modified on September 24, 2015. Please see the docket for this accident to view the original report.*** 


 
 


 

Jabiru J200, 19-3607: Incident occurred October 01, 2015 near Port Lincoln, South Australia

The plane which crash landed into a wheat paddock at Hawson, near Port Lincoln. 



A pilot  has escaped injury after crash landing his plane in a paddock near Port Lincoln.

The plane came down in a paddock off Little Swamp Lane, Hawson, at 11am on Thursday.

An SA Ambulance spokesman said the elderly male pilot refused treatment at the scene.

A police spokesman said the pilot had tried to land at Port Lincoln Airport before the plane came down.

Source:  http://www.theaustralian.com.au