Thursday, November 09, 2017

Piper PA-32-260, N43249, registered to and operated by BEC Industries Ltd: Accident occurred October 23, 2015 in Bluemont, Loudoun County, Virginia

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; Dulles, Virginia

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

http://registry.faa.gov/N43249 


Location: Bluemont, VA
Accident Number: ERA16LA022
Date & Time: 10/23/2015, 1530 EDT
Registration: N43249
Aircraft: PIPER PA-32-260
Aircraft Damage: Substantial
Defining Event: Loss of engine power (total)
Injuries: 2 None
Flight Conducted Under: Part 91: General Aviation - Personal

Analysis 

The commercial pilot stated that, after departure, while climbing through 4,500 ft mean sea level, engine power decreased, the engine "vibrated violently," and he noted that the oil pressure dropped to zero. Soon after, the engine experienced a total loss of power and the pilot elected to perform a forced landing to a nearby field. An examination of the engine revealed that the No. 5 connecting rod had separated from the crankshaft. While several of the cylinders and connecting rods exhibited corrosion, the root cause for the separation of the No. 5 connecting rod from the crankshaft could not be determined. The manufacturer recommended a time between overhaul of 2,000 hours of operation or 12 years, whichever occurs first. At the time of the accident, the engine had accumulated about 2,500 hours of operation in the approximate 17 years since its last overhaul. 

Probable Cause and Findings

The National Transportation Safety Board determines the probable cause(s) of this accident to be:
A total loss of engine power as a result of the separation of the No. 5 connecting rod for reasons that could not be determined based on the available information. 

Findings

Aircraft
Recip eng cyl section - Failure (Cause)
Engine (reciprocating) - Not serviced/maintained

Factual Information

History of Flight

Enroute-climb to cruise
Loss of engine power (total) (Defining event)

Emergency descent
Off-field or emergency landing

Landing-flare/touchdown
Collision with terr/obj (non-CFIT) 

On October 23, 2015, about 1530 eastern daylight time, a Piper PA-32-260, N43249, was substantially damaged during a forced landing to a field near Bluemont, Virginia. The commercial pilot and passenger were not injured. Day visual meteorological conditions prevailed and no flight plan was filed for the personal flight, which was conducted under the provisions of 14 Code of Federal Regulations Part 91. The flight originated from Upperville Airport (2VG2), Upperville, Virginia, about 1520, and was destined for Monmouth Executive Airport (BLM), Farmingdale, New Jersey.

According to the pilot, after departure, while climbing through 4,500 feet mean sea level (msl), the engine power decreased, the engine "vibrated violently," and he noted that the oil pressure dropped to zero. He contacted air traffic control and attempted to return to the departure airport; however, he realized the airplane would not make the airport. Therefore, he elected to perform a forced landing to a nearby field.

According to the passenger, the pilot performed a preflight inspection of the airplane and added a quart of oil to the engine prior to departure. During the climb, the "engine sound became very loud with obvious serious knocking." Soon after, the engine seized and the pilot elected to land the airplane in a field. During the landing, the airplane slid across the field, struck two fences, and then came to rest upright. After the pilot and passenger egressed the airplane, the pilot checked the oil level and the passenger reported that it was "full." 

Pilot Information

Certificate: Commercial
Age: 73, Male
Airplane Rating(s): Single-engine Land
Seat Occupied: Left
Other Aircraft Rating(s): None
Restraint Used: 3-point
Instrument Rating(s): Airplane
Second Pilot Present: No
Instructor Rating(s): None
Toxicology Performed: No
Medical Certification: Class 2 With Waivers/Limitations
Last FAA Medical Exam: 10/26/2013
Occupational Pilot: No
Last Flight Review or Equivalent: 10/24/2014
Flight Time:  3195 hours (Total, all aircraft), 2500 hours (Total, this make and model), 3180 hours (Pilot In Command, all aircraft) 

According to the pilot, he held a commercial pilot certificate with a rating for airplane single-engine land and instrument airplane. He reported 3,195 total hours of flight experience, 2,500 hours of which were in the accident airplane make and model. His most recent Federal Aviation Administration (FAA) second-class medical certificate was issued on October 26, 2013. 

Aircraft and Owner/Operator Information

Aircraft Manufacturer: PIPER
Registration: N43249
Model/Series: PA-32-260
Aircraft Category: Airplane
Year of Manufacture: 1974
Amateur Built: No
Airworthiness Certificate: Normal
Serial Number: 32-7400042
Landing Gear Type: Tricycle
Seats:
Date/Type of Last Inspection: 06/02/2015, Annual
Certified Max Gross Wt.: 3400 lbs
Time Since Last Inspection:
Engines: 1 Reciprocating
Airframe Total Time: 4610 Hours as of last inspection
Engine Manufacturer: LYCOMING
ELT:
Engine Model/Series: O-540 SERIES
Registered Owner: BEC INDUSTRIES LTD
Rated Power: 250 hp
Operator: BEC INDUSTRIES LTD
Operating Certificate(s) Held: None 

According to the FAA, the airplane was manufactured in 1974 and was registered to a corporation in 1991. According to the maintenance records, the most recent annual inspection was performed on June 2, 2015, at which time the airplane had a total time of 4,610 hours and a tachometer time of 2,414.2 hours. At that time, the oil and oil filter were changed, and the oil filter was inspected for contaminants, with none noted. Then two other oil changes were noted in the engine logbook, which corresponded to 2,462 hours and 2,512.5 hours. There was no indication in the engine logbook that the oil filters were examined for contaminants at the time they were changed. The oil filter installed on the airplane at the time of the accident indicated it was installed on September 9, 2015, at a tachometer time of 100 hours, and there was no corresponding entry in the engine logbook.

The tachometer in the airplane at the accident location indicated 117.5 hours; however, no maintenance log entry was found that corresponded to a tachometer replacement.

The airplane was equipped with a Lycoming O-540-E4B5, 260-hp engine. The most recent engine overhaul occurred in 1998. At the most recent annual inspection, the engine had accumulated 2,285.8 hours of time since major overhaul, it was calculated that at the most recent oil change in the engine logbook, the engine had accumulated 2,384.1 hours. Since there was no maintenance log entry that corresponded with the tachometer replacement, the engine had at least an estimated total time of 2,501.6 hours at the time of the accident. 

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light: Day
Observation Facility, Elevation: JYO, 389 ft msl
Observation Time: 1535 EDT
Distance from Accident Site: 12 Nautical Miles
Direction from Accident Site: 92°
Lowest Cloud Condition: Clear
Temperature/Dew Point: 20°C / 6°C
Lowest Ceiling: None
Visibility:  10 Miles
Wind Speed/Gusts, Direction: 4 knots, 330°
Visibility (RVR):
Altimeter Setting: 30.22 inches Hg
Visibility (RVV):
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: UPPERVILLE, VA (2VG2)
Type of Flight Plan Filed: None
Destination: BELMAR/FARMINGDALE, NJ (BLM)
Type of Clearance: VFR Flight Following
Departure Time: 1520 EDT
Type of Airspace:

Wreckage and Impact Information

Crew Injuries: 1 None
Aircraft Damage: Substantial
Passenger Injuries: 1 None
Aircraft Fire: None
Ground Injuries: N/A
Aircraft Explosion: None
Total Injuries: 2 None
Latitude, Longitude:   39.086667, -77.816111 (est) 

An examination of the airplane revealed that the right wing was impact separated and the left wing was removed by recovery personnel. The engine remained attached to the airplane and the propeller remained attached to the engine. One propeller blade was bent aft in an approximate 45-degree angle and the other blade was bent aft in an approximate 5 degree angle.

The engine cowling was removed and no damage was noted on the exterior of the engine crankcase. The carburetor drain nut was removed and about 12 ounces of fluid similar in color to 100LL aviation fuel was drained out of the carburetor. No debris was noted in the fluid. About 9 quarts of oil was noted in the engine, which had a capacity for 12 quarts. Crankshaft continuity was confirmed by rotating the propeller by hand without resistance, and crankshaft continuity was confirmed to the rear accessory section of the engine. The top spark plugs were removed and thumb compression was confirmed on all cylinders except cylinder No. 5.

The bottom of the crankcase was fractured near the No. 5 connecting rod. The oil pump was removed from the engine and rotated freely by hand. It was disassembled with no anomalies noted. The engine oil sump was removed from the engine and there were multiple pieces and particles of metal in the oil sump. The oil filter was removed from the engine, disassembled, and metallic debris was noted in the filter. The oil suction screen was examined and metallic debris was noted in the screen.

All cylinders except cylinder No. 5 were removed, and corrosion was noted on the Nos. 2, 3, and 4 cylinder walls. The No. 5 connecting rod was separated from the crankshaft and corrosion was noted on the connecting rod surface that interfaced with the crankshaft bearing. Cylinder No. 5 was unable to be removed due the connecting rod damage. In addition, corrosion was noted on the No. 6 connecting rod.

The No. 3 piston exhibited scoring on one side of the piston and the piston pin cap was deformed into an oval shape. The No. 3 cylinder was sent to the NTSB Materials Laboratory for further examination.

No. 3 Cylinder Assembly Examination

The piston exhibited a wear scar around the piston pin hole. The lines within the wear scar on the piston were consistent with reciprocating rubbing along the axis of the cylinder. The piston pin did not exhibit deformation, but it did exhibit superficial circumferential wear scars, consistent with rotation inside the piston crown. The inside walls of the cylinder exhibited deposits that were consistent with rust. Furthermore, the inner cylinder had a circular wear scar, which was consistent with the shape of the piston pin plug. There was a lack of corrosion in the circular wear region, which suggested that the corrosion of the cylinder was present before the wear or rubbing between the piston assembly and the cylinder occurred. 

Additional Information

According to the Lycoming Service Instruction on the required time between overhaul, it stated that the time between overhaul (TBO) takes "into account service experience, variations in operating conditions, and frequency of operation…Continuous service assumes that the aircraft will not be out of service for more than 30 consecutive days." The investigation was unable to conclusively determine if the engine was out of service for any period greater than 30 days.

"Engine deterioration in the form of corrosion (rust) and the drying out and hardening of composition materials such as gaskets, seals, flexible hoses and fuel pump diaphragms can occur if an engine is out of service for an extended period of time. Due to the loss of protective oil film after an extended period of inactivity, abnormal wear on soft metal bearing surfaces can occur during engine start. Therefore, all engines that do not accumulate the hourly period of TBO specified in this publication are recommended to be overhauled every twelfth year."


The TBO listed for an O-540-E4B5 engine was 2,000 hours. 




NTSB Identification: ERA16LA022
14 CFR Part 91: General Aviation
Accident occurred Friday, October 23, 2015 in Bluemont, VA
Aircraft: PIPER PA-32-260, registration: N43249
Injuries: 2 Uninjured.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.


On October 23, 2015, about 1530 eastern daylight time, a Piper PA-32-260, N43249, experienced a total loss of engine power and the pilot performed a forced landing to a field near Bluemont, Virginia. The commercial pilot and passenger were not injured. Day visual meteorological conditions prevailed and no flight plan was filed for the personal flight, which was cond
ucted under the provisions of Title 14 Code of Federal Regulations Part 91. The flight originated from Upperville Airport (2VG2), Upperville, Virginia, about 1520, and was destined for Monmouth Executive Airport (BLM), Farmingdale, New Jersey. 

According to the pilot, after departure, while climbing through 4,500 feet mean sea level (msl), the engine power decreased, the engine "vibrated violently," and he noted that the oil pressure dropped to zero. He contacted air traffic control and attempted to return to the departure airport; however, he realized the airplane would not make the airport. Therefore, he elected to perform a forced landing to a nearby field. 

According to the passenger, the pilot performed a preflight and added a quart of oil prior to departure. During the climb, the "engine sound became very loud with obvious serious knocking." Soon after, the engine seized and the pilot elected to land the airplane in a field. During the landing, the airplane slid across the field, struck two fences, and then came to rest upright. After the pilot and passenger egressed the airplane, the pilot checked the oil level and the passenger reported that it was "full."

A postaccident examination of the airplane revealed that the right wing was impact separated and the left wing was removed by recovery personnel. The engine remained attached to the airplane and the propeller remained attached to the engine. One propeller blade was bent aft in an approximate 45 degree angle and the other blade was bent aft in an approximate 5 degree angle. 

The engine cowling was removed and no damage was noted on the exterior of the engine crankcase. The carburetor drain nut was removed and about 12 ounces of fluid similar in color to 100LL aviation fuel was drained out of the carburetor. No debris was noted in the fluid. The oil dipstick was removed and about 9 quarts of oil was noted in the engine. Crankshaft continuity was confirmed by rotating the propeller by hand without resistance. The top spark plugs were removed and thumb compression was confirmed on all cylinders except cylinder No. 5. 

The engine was retained for further examination.
========
Loudoun fire and rescue crews were called to the scene of a light aircraft crash near Bluemont this afternoon. 

The call was made at 3:30 p.m. and crews from Round Hill, Hamilton, Purcellville, Mount Weather, the Office of Emergency Management and the Loudoun County Fire Marshal’s Office responded.

The plane was found in a field on Walsh Farm Lane south of Bluemont.

Two people were aboard. They declined medical treatment.

The State Police said the pilot was experiencing some trouble with the plane and landed in the field as a precaution. The plane, which hit a fence, was damaged, but largely intact.

According to FAA records, the aircraft is a single-engine 1974 Piper registered to BEC Industries Ltd. in Monmouth County, NJ. 

According to Loudoun Fire-Rescue, the plane departed from a private airfield in Upperville and was headed to an executive airport in New Jersey when the crash occurred.  The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; Dulles, Virginia

Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

Registered Owner: BEC Industries Ltd

Operator: BEC Industries Ltd

http://registry.faa.gov/N43249 



NTSB Identification: ERA16LA022
14 CFR Part 91: General Aviation
Accident occurred Friday, October 23, 2015 in Bluemont, VA
Aircraft: PIPER PA-32-260, registration: N43249
Injuries: 2 Uninjured.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

HISTORY OF FLIGHT

On October 23, 2015, about 1530 eastern daylight time, a Piper PA-32-260, N43249, was substantially damaged during a forced landing to a field near Bluemont, Virginia. The commercial pilot and passenger were not injured. Day visual meteorological conditions prevailed and no flight plan was filed for the personal flight, which was conducted under the provisions of 14 Code of Federal Regulations Part 91. The flight originated from Upperville Airport (2VG2), Upperville, Virginia, about 1520, and was destined for Monmouth Executive Airport (BLM), Farmingdale, New Jersey.

According to the pilot, after departure, while climbing through 4,500 feet mean sea level (msl), the engine power decreased, the engine "vibrated violently," and he noted that the oil pressure dropped to zero. He contacted air traffic control and attempted to return to the departure airport; however, he realized the airplane would not make the airport. Therefore, he elected to perform a forced landing to a nearby field.

According to the passenger, the pilot performed a preflight inspection of the airplane and added a quart of oil to the engine prior to departure. During the climb, the "engine sound became very loud with obvious serious knocking." Soon after, the engine seized and the pilot elected to land the airplane in a field. During the landing, the airplane slid across the field, struck two fences, and then came to rest upright. After the pilot and passenger egressed the airplane, the pilot checked the oil level and the passenger reported that it was "full."

PERSONNEL INFORMATION

According to the pilot, he held a commercial pilot certificate with a rating for airplane single-engine land and instrument airplane. He reported 3,195 total hours of flight experience, 2,500 hours of which were in the accident airplane make and model. His most recent Federal Aviation Administration (FAA) second-class medical certificate was issued on October 26, 2013.

AIRPLANE INFORMATION

According to the FAA, the airplane was manufactured in 1974 and was registered to a corporation in 1991. According to the maintenance records, the most recent annual inspection was performed on June 2, 2015, at which time the airplane had a total time of 4,610 hours and a tachometer time of 2,414.2 hours. At that time, the oil and oil filter were changed, and the oil filter was inspected for contaminants, with none noted. Then two other oil changes were noted in the engine logbook, which corresponded to 2,462 hours and 2,512.5 hours. There was no indication in the engine logbook that the oil filters were examined for contaminants at the time they were changed. The oil filter installed on the airplane at the time of the accident indicated it was installed on September 9, 2015, at a tachometer time of 100 hours, and there was no corresponding entry in the engine logbook.

The tachometer in the airplane at the accident location indicated 117.5 hours; however, no maintenance log entry was found that corresponded to a tachometer replacement.

The airplane was equipped with a Lycoming O-540-E4B5, 260-hp engine. The most recent engine overhaul occurred in 1998. At the most recent annual inspection, the engine had accumulated 2,285.8 hours of time since major overhaul, it was calculated that at the most recent oil change in the engine logbook, the engine had accumulated 2,384.1 hours. Since there was no maintenance log entry that corresponded with the tachometer replacement, the engine had at least an estimated total time of 2,501.6 hours at the time of the accident.

WRECKAGE AND IMPACT INFORMATION

An examination of the airplane revealed that the right wing was impact separated and the left wing was removed by recovery personnel. The engine remained attached to the airplane and the propeller remained attached to the engine. One propeller blade was bent aft in an approximate 45-degree angle and the other blade was bent aft in an approximate 5 degree angle.

The engine cowling was removed and no damage was noted on the exterior of the engine crankcase. The carburetor drain nut was removed and about 12 ounces of fluid similar in color to 100LL aviation fuel was drained out of the carburetor. No debris was noted in the fluid. About 9 quarts of oil was noted in the engine, which had a capacity for 12 quarts. Crankshaft continuity was confirmed by rotating the propeller by hand without resistance, and crankshaft continuity was confirmed to the rear accessory section of the engine. The top spark plugs were removed and thumb compression was confirmed on all cylinders except cylinder No. 5.

The bottom of the crankcase was fractured near the No. 5 connecting rod. The oil pump was removed from the engine and rotated freely by hand. It was disassembled with no anomalies noted. The engine oil sump was removed from the engine and there were multiple pieces and particles of metal in the oil sump. The oil filter was removed from the engine, disassembled, and metallic debris was noted in the filter. The oil suction screen was examined and metallic debris was noted in the screen.

All cylinders except cylinder No. 5 were removed, and corrosion was noted on the Nos. 2, 3, and 4 cylinder walls. The No. 5 connecting rod was separated from the crankshaft and corrosion was noted on the connecting rod surface that interfaced with the crankshaft bearing. Cylinder No. 5 was unable to be removed due the connecting rod damage. In addition, corrosion was noted on the No. 6 connecting rod.

The No. 3 piston exhibited scoring on one side of the piston and the piston pin cap was deformed into an oval shape. The No. 3 cylinder was sent to the NTSB Materials Laboratory for further examination.

No. 3 Cylinder Assembly Examination

The piston exhibited a wear scar around the piston pin hole. The lines within the wear scar on the piston were consistent with reciprocating rubbing along the axis of the cylinder. The piston pin did not exhibit deformation, but it did exhibit superficial circumferential wear scars, consistent with rotation inside the piston crown. The inside walls of the cylinder exhibited deposits that were consistent with rust. Furthermore, the inner cylinder had a circular wear scar, which was consistent with the shape of the piston pin plug. There was a lack of corrosion in the circular wear region, which suggested that the corrosion of the cylinder was present before the wear or rubbing between the piston assembly and the cylinder occurred.

ADDITIONAL INFORMATION

According to the Lycoming Service Instruction on the required time between overhaul, it stated that the time between overhaul (TBO) takes "into account service experience, variations in operating conditions, and frequency of operation…Continuous service assumes that the aircraft will not be out of service for more than 30 consecutive days." The investigation was unable to conclusively determine if the engine was out of service for any period greater than 30 days.

"Engine deterioration in the form of corrosion (rust) and the drying out and hardening of composition materials such as gaskets, seals, flexible hoses and fuel pump diaphragms can occur if an engine is out of service for an extended period of time. Due to the loss of protective oil film after an extended period of inactivity, abnormal wear on soft metal bearing surfaces can occur during engine start. Therefore, all engines that do not accumulate the hourly period of TBO specified in this publication are recommended to be overhauled every twelfth year."

The TBO listed for an O-540-E4B5 engine was 2,000 hours.



NTSB Identification: ERA16LA022
14 CFR Part 91: General Aviation
Accident occurred Friday, October 23, 2015 in Bluemont, VA
Aircraft: PIPER PA-32-260, registration: N43249
Injuries: 2 Uninjured.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.


On October 23, 2015, about 1530 eastern daylight time, a Piper PA-32-260, N43249, experienced a total loss of engine power and the pilot performed a forced landing to a field near Bluemont, Virginia. The commercial pilot and passenger were not injured. Day visual meteorological conditions prevailed and no flight plan was filed for the personal flight, which was cond
ucted under the provisions of Title 14 Code of Federal Regulations Part 91. The flight originated from Upperville Airport (2VG2), Upperville, Virginia, about 1520, and was destined for Monmouth Executive Airport (BLM), Farmingdale, New Jersey. 

According to the pilot, after departure, while climbing through 4,500 feet mean sea level (msl), the engine power decreased, the engine "vibrated violently," and he noted that the oil pressure dropped to zero. He contacted air traffic control and attempted to return to the departure airport; however, he realized the airplane would not make the airport. Therefore, he elected to perform a forced landing to a nearby field. 

According to the passenger, the pilot performed a preflight and added a quart of oil prior to departure. During the climb, the "engine sound became very loud with obvious serious knocking." Soon after, the engine seized and the pilot elected to land the airplane in a field. During the landing, the airplane slid across the field, struck two fences, and then came to rest upright. After the pilot and passenger egressed the airplane, the pilot checked the oil level and the passenger reported that it was "full."

A postaccident examination of the airplane revealed that the right wing was impact separated and the left wing was removed by recovery personnel. The engine remained attached to the airplane and the propeller remained attached to the engine. One propeller blade was bent aft in an approximate 45 degree angle and the other blade was bent aft in an approximate 5 degree angle. 

The engine cowling was removed and no damage was noted on the exterior of the engine crankcase. The carburetor drain nut was removed and about 12 ounces of fluid similar in color to 100LL aviation fuel was drained out of the carburetor. No debris was noted in the fluid. The oil dipstick was removed and about 9 quarts of oil was noted in the engine. Crankshaft continuity was confirmed by rotating the propeller by hand without resistance. The top spark plugs were removed and thumb compression was confirmed on all cylinders except cylinder No. 5. 

The engine was retained for further examination.

No comments:

Post a Comment