Sunday, May 28, 2017

Golden Circle Air T-Bird II, N92744: Accident occurred December 13, 2015 near Lower Creek Airport (NC27), Lenoir, Caldwell County, North Carolina

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

NTSB Identification: ERA16LA067
14 CFR Part 91: General Aviation
Accident occurred Sunday, December 13, 2015 in Lenoir, NC
Probable Cause Approval Date: 07/20/2017
Aircraft: GOLDEN CIRCLE AIR INC T BIRD II, registration: N92744
Injuries: 1 Serious.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

The private pilot was departing in the experimental light sport airplane. Onboard video footage from a wingtip-mounted camera provided a view of the cockpit. The pilot could be seen with his left hand on the control yoke, but his right hand, which was near the engine throttle, was obscured. The airplane took off and completed the upwind leg of the traffic pattern, and the pilot initiated a right turn toward the crosswind leg. The sound of the engine was smooth and continuous throughout the takeoff and climb. As the airplane entered the turn, a reduction in power was heard, but the engine sound remained smooth and continuous. At the moment of power reduction and the initiation of the turn, the pilot simultaneously applied left aileron, right rudder, and back pressure on the yoke. As the airplane rolled right and nosed down into a spin, the engine could be heard accelerating.

The “Remove Before Flight” flag on the locking pin for the airframe parachute deployment handle was observed in the camera’s field of view, as the pilot struggled with one hand and then two hands to remove the pin during the descent. Eventually, the pilot freed the pin and actuated the deployment handle as the nose of the airplane entered the tops of the trees. Postaccident examination of the wreckage revealed no pre-impact mechanical anomalies. The airframe parachute was free from its canister, but was not fully deployed due to the airplane’s low altitude at the time of deployment. 

The video footage of the pilot simultaneously reducing engine power, increasing the airplane’s pitch attitude, and applying opposite aileron and rudder controls is consistent with a cross-controlled aerodynamic stall and subsequent spin. 

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot’s failure to maintain airspeed and a coordinated turn in the traffic pattern, which resulted in the airplane exceeding its critical angle of attack and entering an aerodynamic stall and spin. Contributing to the accident was the pilot’s failure to remove the airframe parachute activation handle locking pin before flight. 

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; Charlotte, North Carolina

Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

http://registry.faa.gov/N92744 

NTSB Identification: ERA16LA067
14 CFR Part 91: General Aviation
Accident occurred Sunday, December 13, 2015 in Lenoir, NC
Aircraft: GOLDEN CIRCLE AIR INC T BIRD II, registration: N92744
Injuries: 1 Serious.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On December 13, 2015, at 1724 eastern standard time, an experimental light sport Golden Circle Air T Bird II, N92744, was destroyed after it departed controlled flight and crashed into trees and terrain after takeoff from Lower Creek Airport (NC27), Lenoir, North Carolina. The private pilot/owner was seriously injured. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight, which was conducted under the provisions of Title14 Code of Federal Regulations Part 91.

The Federal Aviation Administration (FAA) inspector who responded to the scene said he recovered a wing-mounted video camera, removed the data card, and downloaded the contents. Review of the data revealed the accident flight was captured on the card.

Examination of the video revealed that the camera was mounted on the left wing, pointed spanwise along the wing, and provided a view of the cockpit. The pilot could be seen with his left hand on the yoke, but his right hand, which was in the vicinity of the engine throttle, was obscured.

The airplane took off and completed the upwind leg of the traffic pattern, and initiated a turn to the right towards the crosswind leg. The sound of the engine was smooth and continuous throughout the takeoff and climb. As the airplane entered the turn, a reduction in power was heard, but the engine sound remained smooth and continuous. At the moment of power reduction and the initiation of the turn, the pilot simultaneously applied left aileron, right rudder, and back pressure on the yoke.

As the airplane rolled right and into a nose-down spin, the engine could be heard accelerating.

The "Remove Before Flight" flag on the locking pin for the Ballistic Recovery System (BRS) parachute deployment handle was observed in the camera's field of view, as the pilot struggled with one hand and then two hands to remove the pin during the descent. Eventually, the pilot freed the pin, and actuated the deployment handle as the nose of the airplane entered the tops of the trees.

The pilot held a private pilot certificate with a rating for airplane single-engine land. His most recent second-class Federal Aviation Administration (FAA) medical certificate was issued on July 8, 2011, and he reported 40 total hours of flight experience on that date.

Examination of excerpts from the pilot's logbook revealed he had logged 90.6 total hours of flight experience, 25 hours of which were in the accident airplane make and model. The pilot logged 7 hours of flight experience in the 90 days prior to the accident, and 1.2 hours in the 30 days prior; all of which was in the accident airplane.

The airplane was manufactured in 2001. The maintenance records were not recovered, therefore the maintenance and inspection history of the airplane could not be determined.

At 1735, the weather recorded at Morgantown-Lenoir Airport, 10 miles southwest of the accident site, (MRN) included winds from 140 degrees at 3 knots.

Examination of the wreckage by the FAA inspector revealed no pre-impact mechanical anomalies. The BRS parachute was free from its canister, but was not fully deployed.

According to the FAA Airplane Flying Handbook:

The aerodynamic effects of the uncoordinated, cross-control stall can surprise the unwary pilot because it can occur with very little warning and can be deadly if it occurs close to the ground… A cross-control stall occurs when the critical AOA is exceeded with aileron pressure applied in one direction and rudder pressure in the opposite direction, causing uncoordinated flight. A skidding cross-control stall is most likely to occur in the traffic pattern during a poorly planned and executed base-to-final approach turn in which the airplane overshoots the runway centerline and the pilot attempts to correct back to centerline by increasing the bank angle, increasing back elevator pressure, and applying rudder in the direction of the turn (i.e., inside or bottom rudder pressure) to bring the nose around further to align it with the runway.

NTSB Identification: ERA16LA067
14 CFR Part 91: General Aviation
Accident occurred Sunday, December 13, 2015 in Lenoir, NC
Aircraft: GOLDEN CIRCLE AIR INC T BIRD II, registration: N92744
Injuries: 1 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On December 13, 2015, at 1724 eastern standard time, an experimental amateur-built Golden Circle Air T Bird II, N92744, was destroyed after it departed controlled flight and crashed into trees and terrain after takeoff from Lower Creek Airport (NC27), Lenoir, North Carolina. The private pilot/owner was seriously injured. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight, which was conducted under the provisions of Title14 Code of Federal Regulations Part 91. 

The Federal Aviation Administration (FAA) inspector who responded to the scene said he recovered a wing-mounted video camera, removed the data card, and downloaded the contents. Review of the data revealed the accident flight was captured on the card. The inspector then forwarded the video of the flight to the NTSB for review. 

Examination of the video revealed that the camera was mounted on the left wing, pointed spanwise along the wing, and provided a view of the cockpit. The pilot could be seen with his left hand on the yoke, but his right hand, which was in the vicinity of the engine throttle, was obscured. 

The airplane took off and completed the upwind leg of the traffic pattern, and initiated a turn to the right towards the crosswind leg. The sound of the engine was smooth and continuous throughout the takeoff and climb. As the airplane entered the turn, a reduction in power was heard, but the engine sound remained smooth and continuous. At the moment of power reduction and the initiation of the turn, the pilot simultaneously applied left aileron, right rudder, and back pressure on the yoke. 

As the airplane rolled right and into a nose-down spin, the engine could be heard accelerating. 

The "Remove Before Flight" flag on the locking pin for the Ballistic Recovery System (BRS) parachute deployment handle was observed in the camera's field of view, as the pilot struggled with one hand and then two hands to remove the pin during the descent. Eventually, the pilot freed the pin, and actuated the deployment handle as the nose of the airplane entered the tops of the trees. 

The pilot held a private pilot certificate with a rating for airplane single-engine land. His most recent second-class Federal Aviation Administration (FAA) medical certificate was issued on July 8, 2011, and he reported 40 total hours of flight experience on that date. 

Examination of excerpts from the pilot's logbook revealed he had logged 90.6 total hours of flight experience, 25 hours of which were in the accident airplane make and model. The pilot logged 7 hours of flight experience in the 90 days prior to the accident, and 1.2 hours in the 30 days prior; all of which was in the accident airplane. 

The airplane was manufactured in 2001. The maintenance records were not recovered, therefore the maintenance and inspection history of the airplane could not be immediately determined. 

At 1735, the weather recorded at Morgantown-Lenoir Airport, 10 miles southwest of the accident site, (MRN) included winds from 140 degrees at 3knots. 

Examination of the wreckage by the FAA inspector revealed no pre-impact mechanical anomalies. The BRS parachute was free from its canister, but was not fully deployed.

FAA Flight Standards District Office: FAA Charlotte FSDO-68



LENOIR, NC (WBTV) -  The Caldwell County Sheriff's Office says an ultralight plane crashed near Lenoir Sunday night.

The crash reportedly happened near Lower Creek Airfield in Lenoir.

Caldwell County Emergency Management got the call about the crash on Blue Sky Lane at 5:24 p.m.

Caldwell County officials say the aircraft crashed in the woods just short of the nearby airstrip. 

Caldwell County Emergency Services Director Dino Dibernardi said the pilot was removed from the wreckage by firefighters and taken to Caldwell Memorial Hospital. From there the pilot was airlifted to Carolinas Medical Center in Charlotte.

The Federal Aviation Administration is investigating the crash.

Source:  http://www.wbtv.com





The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; Charlotte, North Carolina

Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

http://registry.faa.gov/N92744 




NTSB Identification: ERA16LA067
14 CFR Part 91: General Aviation
Accident occurred Sunday, December 13, 2015 in Lenoir, NC
Aircraft: GOLDEN CIRCLE AIR INC T BIRD II, registration: N92744
Injuries: 1 Serious.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On December 13, 2015, at 1724 eastern standard time, an experimental light sport Golden Circle Air T Bird II, N92744, was destroyed after it departed controlled flight and crashed into trees and terrain after takeoff from Lower Creek Airport (NC27), Lenoir, North Carolina. The private pilot/owner was seriously injured. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight, which was conducted under the provisions of Title14 Code of Federal Regulations Part 91.

The Federal Aviation Administration (FAA) inspector who responded to the scene said he recovered a wing-mounted video camera, removed the data card, and downloaded the contents. Review of the data revealed the accident flight was captured on the card.

Examination of the video revealed that the camera was mounted on the left wing, pointed spanwise along the wing, and provided a view of the cockpit. The pilot could be seen with his left hand on the yoke, but his right hand, which was in the vicinity of the engine throttle, was obscured.

The airplane took off and completed the upwind leg of the traffic pattern, and initiated a turn to the right towards the crosswind leg. The sound of the engine was smooth and continuous throughout the takeoff and climb. As the airplane entered the turn, a reduction in power was heard, but the engine sound remained smooth and continuous. At the moment of power reduction and the initiation of the turn, the pilot simultaneously applied left aileron, right rudder, and back pressure on the yoke.

As the airplane rolled right and into a nose-down spin, the engine could be heard accelerating.

The "Remove Before Flight" flag on the locking pin for the Ballistic Recovery System (BRS) parachute deployment handle was observed in the camera's field of view, as the pilot struggled with one hand and then two hands to remove the pin during the descent. Eventually, the pilot freed the pin, and actuated the deployment handle as the nose of the airplane entered the tops of the trees.

The pilot held a private pilot certificate with a rating for airplane single-engine land. His most recent second-class Federal Aviation Administration (FAA) medical certificate was issued on July 8, 2011, and he reported 40 total hours of flight experience on that date.

Examination of excerpts from the pilot's logbook revealed he had logged 90.6 total hours of flight experience, 25 hours of which were in the accident airplane make and model. The pilot logged 7 hours of flight experience in the 90 days prior to the accident, and 1.2 hours in the 30 days prior; all of which was in the accident airplane.

The airplane was manufactured in 2001. The maintenance records were not recovered, therefore the maintenance and inspection history of the airplane could not be determined.

At 1735, the weather recorded at Morgantown-Lenoir Airport, 10 miles southwest of the accident site, (MRN) included winds from 140 degrees at 3 knots.

Examination of the wreckage by the FAA inspector revealed no pre-impact mechanical anomalies. The BRS parachute was free from its canister, but was not fully deployed.

According to the FAA Airplane Flying Handbook:

The aerodynamic effects of the uncoordinated, cross-control stall can surprise the unwary pilot because it can occur with very little warning and can be deadly if it occurs close to the ground… A cross-control stall occurs when the critical AOA is exceeded with aileron pressure applied in one direction and rudder pressure in the opposite direction, causing uncoordinated flight. A skidding cross-control stall is most likely to occur in the traffic pattern during a poorly planned and executed base-to-final approach turn in which the airplane overshoots the runway centerline and the pilot attempts to correct back to centerline by increasing the bank angle, increasing back elevator pressure, and applying rudder in the direction of the turn (i.e., inside or bottom rudder pressure) to bring the nose around further to align it with the runway.





NTSB Identification: ERA16LA067
14 CFR Part 91: General Aviation
Accident occurred Sunday, December 13, 2015 in Lenoir, NC
Aircraft: GOLDEN CIRCLE AIR INC T BIRD II, registration: N92744
Injuries: 1 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On December 13, 2015, at 1724 eastern standard time, an experimental amateur-built Golden Circle Air T Bird II, N92744, was destroyed after it departed controlled flight and crashed into trees and terrain after takeoff from Lower Creek Airport (NC27), Lenoir, North Carolina. The private pilot/owner was seriously injured. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight, which was conducted under the provisions of Title14 Code of Federal Regulations Part 91. 

The Federal Aviation Administration (FAA) inspector who responded to the scene said he recovered a wing-mounted video camera, removed the data card, and downloaded the contents. Review of the data revealed the accident flight was captured on the card. The inspector then forwarded the video of the flight to the NTSB for review. 

Examination of the video revealed that the camera was mounted on the left wing, pointed spanwise along the wing, and provided a view of the cockpit. The pilot could be seen with his left hand on the yoke, but his right hand, which was in the vicinity of the engine throttle, was obscured. 

The airplane took off and completed the upwind leg of the traffic pattern, and initiated a turn to the right towards the crosswind leg. The sound of the engine was smooth and continuous throughout the takeoff and climb. As the airplane entered the turn, a reduction in power was heard, but the engine sound remained smooth and continuous. At the moment of power reduction and the initiation of the turn, the pilot simultaneously applied left aileron, right rudder, and back pressure on the yoke. 

As the airplane rolled right and into a nose-down spin, the engine could be heard accelerating. 

The "Remove Before Flight" flag on the locking pin for the Ballistic Recovery System (BRS) parachute deployment handle was observed in the camera's field of view, as the pilot struggled with one hand and then two hands to remove the pin during the descent. Eventually, the pilot freed the pin, and actuated the deployment handle as the nose of the airplane entered the tops of the trees. 

The pilot held a private pilot certificate with a rating for airplane single-engine land. His most recent second-class Federal Aviation Administration (FAA) medical certificate was issued on July 8, 2011, and he reported 40 total hours of flight experience on that date. 

Examination of excerpts from the pilot's logbook revealed he had logged 90.6 total hours of flight experience, 25 hours of which were in the accident airplane make and model. The pilot logged 7 hours of flight experience in the 90 days prior to the accident, and 1.2 hours in the 30 days prior; all of which was in the accident airplane. 

The airplane was manufactured in 2001. The maintenance records were not recovered, therefore the maintenance and inspection history of the airplane could not be immediately determined. 

At 1735, the weather recorded at Morgantown-Lenoir Airport, 10 miles southwest of the accident site, (MRN) included winds from 140 degrees at 3knots. 

Examination of the wreckage by the FAA inspector revealed no pre-impact mechanical anomalies. The BRS parachute was free from its canister, but was not fully deployed.

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