Saturday, October 17, 2015

STOL CH 701, N4931M: Accident occurred October 14, 2015 at Weedon Field Airport (KEUF), Eufaula, Barbour County, Alabama

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:

Federal Aviation Administration / Flight Standards District Office; Birmingham, Alabama

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf


Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms


http://registry.faa.gov/N2EU

Location: Eufaula, AL
Accident Number: ERA16LA014
Date & Time: 10/14/2015, 1445 CDT
Registration: N4931M
Aircraft: GROSS MICHAEL E STOL CH 701
Aircraft Damage: Substantial
Defining Event: Loss of control in flight
Injuries: 1 None
Flight Conducted Under: Part 91: General Aviation - Personal

Analysis 

The private pilot had purchased the airplane a day earlier and, while flying it back to his home airport, stopped at an en route airport to refuel. The pilot stated that, about midfield during the takeoff, the engine began to run roughly and vibrate, was not producing full power, and the flight controls "got mushy." Shortly after the takeoff, at an altitude of 50 ft, the airplane veered to the left, impacted the ground, and nosed over. The pilot noted that the airplane took longer to take off due to a crosswind; however, weather recorded at the airport 13 minutes after the accident included calm winds. Postaccident examination of the airframe and engine revealed no evidence of any preexisting mechanical anomalies that would have precluded normal operation, and the reason for the loss of engine power could not be determined. 

Probable Cause and Findings

The National Transportation Safety Board determines the probable cause(s) of this accident to be:
A partial loss of engine power during takeoff for reasons that could not be determined, because postaccident examination revealed no evidence of any preimpact mechanical malfunctions or failures. Also causal was the pilot's decision to continue the takeoff following the loss of power. 

Findings

Aircraft
Angle of attack - Capability exceeded

Personnel issues
Incorrect action performance - Pilot (Cause)

Factual Information 

On October 14, 2015, about 1445 central daylight time, an experimental amateur-built Zenith STOL CH701, N4931M, was substantially damaged shortly after taking off from Weedon Field (EUF), Eufala, Alabama. The private pilot was not injured. Visual meteorological conditions prevailed, and no flight plan had been filed for the flight to Eu-Wish Airport (MU68), Hermann, Missouri. The personal flight was operating under the provisions of 14 Code of Federal Regulations Part 91.

After the accident, the pilot was granted permission by the NTSB investigator in charge to transport the airplane to his home in Missouri, being advised that additional information would be requested. The pilot subsequently failed to respond to any NTSB information requests, either directly or through his attorney. The investigation could thus only rely on the information gathered onsite by the responding Federal Aviation Administration (FAA) inspector, and on a written statement from the pilot subsequently provided through his attorney to the FAA inspector.

According to the pilot, he had purchased the airplane the day before in Florida, and was flying it home to Missouri, stopping at EUF to refuel. After refueling, the engine would not start, and the battery discharged. After charging the battery, the engine started "normally."

In a written statement the day of the accident, the pilot stated that after takeoff, about 50 feet above the runway, the airplane "turned left and did not respond to any control inputs to trim right and stay over the runway. Instead, it continued a left bank and impacted the ground."

In a later statement, the pilot stated that he had performed an engine run-up at 4,000 rpm without noting any anomalies. After which, he taxied to south end of runway 36 and commenced the takeoff. After applying full power, the airplane took longer than normal to take off due to crosswind conditions. About 50 feet above the runway, at mid-field, the engine began to run roughly and vibrate, and was not producing full power. The pilot attempted to "smooth out" the engine by adjusting the throttle; there was no mixture control.

The pilot then attempted to land the airplane back on the runway, but in the process, it veered off the left side and flipped upside-down. The pilot egressed the airplane, and reached back in to turn off the fuel valve as the emergency vehicles arrived.

According to the responding FAA inspector, the airplane had been moved to a hangar prior to her arrival. There, she noted that one blade of the three-bladed composite propeller was broken off and one was cracked. There was no bending or twisting of the propeller blades. There was no dripping or splattering of oil on the engine cowling. No anomalies were noted within the engine compartment.

The fuel bowl on the left side of the engine was full, and both wing fuel tanks were full of fuel. The inspector also drained fuel from each of the two wing tanks, and the fuel sump on the underside of the fuselage, just aft the engine compartment, and all samples were "clear and clean."

The inspector noted no control binding to the elevator or rudder, and while checking for aileron binding (none noted), the pilot stated that the controls "got mushy."

The FAA inspector subsequently drove out along the runway to where the airplane was recovered, which was about 3,200 feet from the departure end of the 5,000-foot runway.

Weather, recorded at the airport 13 minutes after the accident, included clear skies and calm winds. 

History of Flight

Initial climb
Loss of control in flight (Defining event) 

Pilot Information

Certificate: Private; Sport Pilot
Age: 66, Male
Airplane Rating(s): Single-engine Land
Seat Occupied: Left
Other Aircraft Rating(s): None
Restraint Used: Unknown
Instrument Rating(s): None
Second Pilot Present: No
Instructor Rating(s): None
Toxicology Performed: No
Medical Certification: None
Last FAA Medical Exam:
Occupational Pilot: No
Last Flight Review or Equivalent: 10/10/2015
Flight Time:  218 hours (Total, all aircraft), 6 hours (Total, this make and model), 8 hours (Last 90 days, all aircraft), 6 hours (Last 24 hours, all aircraft) 

Aircraft and Owner/Operator Information

Aircraft Manufacturer: GROSS MICHAEL E
Registration: N4931M
Model/Series: STOL CH 701
Aircraft Category: Airplane
Year of Manufacture: 2006
Amateur Built: Yes
Airworthiness Certificate: Experimental
Serial Number: 7-4931
Landing Gear Type: Tricycle
Seats: 2
Date/Type of Last Inspection: 02/11/2015, Annual
Certified Max Gross Wt.:
Time Since Last Inspection: 25 Hours
Engines: 1 Reciprocating
Airframe Total Time: 738 Hours
Engine Manufacturer: ROTAX
ELT: Installed, not activated
Engine Model/Series: 912UL
Registered Owner: Karl H. Paubel
Rated Power: hp
Operator: On file
Operating Certificate(s) Held: None

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light: Day
Observation Facility, Elevation: EUF, 285 ft msl
Observation Time: 1958 UTC
Distance from Accident Site: 0 Nautical Miles
Direction from Accident Site: 
Lowest Cloud Condition: Clear
Temperature/Dew Point: 28°C / 9°C
Lowest Ceiling: None
Visibility:  10 Miles
Wind Speed/Gusts, Direction: Calm
Visibility (RVR):
Altimeter Setting: 29.99 inches Hg
Visibility (RVV):
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: Eufala, AL (EUF)
Type of Flight Plan Filed: None
Destination: Hermann, MO (MU68)
Type of Clearance: None
Departure Time: 1445 CDT
Type of Airspace: Class G

Airport Information

Airport: Weedon Field (EUF)
Runway Surface Type: Asphalt
Airport Elevation: 285 ft
Runway Surface Condition:  Dry
Runway Used: 36
IFR Approach: None
Runway Length/Width: 5000 ft / 100 ft
VFR Approach/Landing: Forced Landing 

Wreckage and Impact Information

Crew Injuries: 1 None
Aircraft Damage: Substantial
Passenger Injuries: N/A
Aircraft Fire: None
Ground Injuries: N/A
Aircraft Explosion: None
Total Injuries: 1 None
Latitude, Longitude:  31.951389, -85.128889 (est)




NTSB Identification: ERA16LA014

14 CFR Part 91: General Aviation
Accident occurred Wednesday, October 14, 2015 in Eufala, AL
Aircraft: GROSS MICHAEL E STOL CH 701, registration: N4931M
Injuries: 1 Uninjured.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On October 14, 2015, about 1445 central daylight time, an experimental amateur-built Zenith STOL CH701, N4931M, was substantially damaged shortly after taking off from Weedon Field (EUF), Eufala, Alabama. The private pilot was not injured. Visual meteorological conditions prevailed, and no flight plan had been filed for the flight to Eu-Wish Airport (MU68), Hermann, Missouri. The personal flight was operating under the provisions of 14 Code of Federal Regulations Part 91.

According to the pilot, he had purchased the airplane the day before in Florida, and was flying it home, stopping at EUF to refuel. After refueling, the engine would not start, and the battery discharged. After charging the battery, the engine started "normally."

The pilot subsequently performed an engine run-up at 4,000 rpm without noting any anomalies. After which, he taxied to south end of runway 36 and commenced the takeoff. After applying full power, the airplane took longer than normal to take off due to cross wind conditions. About 50 feet above the runway, at mid-field, the engine began to run roughly and vibrate, and was not producing full power. The pilot attempted to "smooth out" the engine by adjusting the throttle; there was no mixture control.

The pilot then attempted to land the airplane back on the runway, but in the process, it veered off the left side and flipped upside-down. The pilot egressed the airplane, and reached back in to turn off the fuel valve as the emergency vehicles arrived.

According to the responding Federal Aviation Administration (FAA) inspector, the airplane had been moved to a hangar prior to her arrival. There, she noted that one blade of the three-bladed propeller was broken off and one was cracked. There was no bending or twisting of the propeller blades. There was no dripping or splattering of oil on the engine cowling. No anomalies were noted within the engine compartment, and all fuel samples were clear. The fuel bowl on the left side of the engine was full, and both wing fuel tanks were full of fuel.

The FAA inspector subsequently drove out along the runway to where the airplane was recovered, which was about 3,200 feet from the departure end.

With concurrence from the NTSB investigator in charge, the airplane was subsequently ground-transported to the pilot's home in Missouri. The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; Birmingham, Alabama

Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

http://registry.faa.gov/N2EU


NTSB Identification: ERA16LA014
14 CFR Part 91: General Aviation
Accident occurred Wednesday, October 14, 2015 in Eufala, AL
Aircraft: GROSS MICHAEL E STOL CH 701, registration: N4931M
Injuries: 1 Uninjured.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On October 14, 2015, about 1445 central daylight time, an experimental amateur-built Zenith STOL CH701, N4931M, was substantially damaged shortly after taking off from Weedon Field (EUF), Eufala, Alabama. The private pilot was not injured. Visual meteorological conditions prevailed, and no flight plan had been filed for the flight to Eu-Wish Airport (MU68), Hermann, Missouri. The personal flight was operating under the provisions of 14 Code of Federal Regulations Part 91.

After the accident, the pilot was granted permission by the NTSB investigator in charge to transport the airplane to his home in Missouri, being advised that additional information would be requested. The pilot subsequently failed to respond to any NTSB information requests, either directly or through his attorney. The investigation could thus only rely on the information gathered onsite by the responding Federal Aviation Administration (FAA) inspector, and on a written statement from the pilot subsequently provided through his attorney to the FAA inspector.

According to the pilot, he had purchased the airplane the day before in Florida, and was flying it home to Missouri, stopping at EUF to refuel. After refueling, the engine would not start, and the battery discharged. After charging the battery, the engine started "normally."

In a written statement the day of the accident, the pilot stated that after takeoff, about 50 feet above the runway, the airplane "turned left and did not respond to any control inputs to trim right and stay over the runway. Instead, it continued a left bank and impacted the ground."

In a later statement, the pilot stated that he had performed an engine run-up at 4,000 rpm without noting any anomalies. After which, he taxied to south end of runway 36 and commenced the takeoff. After applying full power, the airplane took longer than normal to take off due to crosswind conditions. About 50 feet above the runway, at mid-field, the engine began to run roughly and vibrate, and was not producing full power. The pilot attempted to "smooth out" the engine by adjusting the throttle; there was no mixture control.

The pilot then attempted to land the airplane back on the runway, but in the process, it veered off the left side and flipped upside-down. The pilot egressed the airplane, and reached back in to turn off the fuel valve as the emergency vehicles arrived.

According to the responding FAA inspector, the airplane had been moved to a hangar prior to her arrival. There, she noted that one blade of the three-bladed composite propeller was broken off and one was cracked. There was no bending or twisting of the propeller blades. There was no dripping or splattering of oil on the engine cowling. No anomalies were noted within the engine compartment.

The fuel bowl on the left side of the engine was full, and both wing fuel tanks were full of fuel. The inspector also drained fuel from each of the two wing tanks, and the fuel sump on the underside of the fuselage, just aft the engine compartment, and all samples were "clear and clean."

The inspector noted no control binding to the elevator or rudder, and while checking for aileron binding (none noted), the pilot stated that the controls "got mushy."

The FAA inspector subsequently drove out along the runway to where the airplane was recovered, which was about 3,200 feet from the departure end of the 5,000-foot runway.

Weather, recorded at the airport 13 minutes after the accident, included clear skies and calm winds.



NTSB Identification: ERA16LA014

14 CFR Part 91: General Aviation
Accident occurred Wednesday, October 14, 2015 in Eufala, AL
Aircraft: GROSS MICHAEL E STOL CH 701, registration: N4931M
Injuries: 1 Uninjured.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On October 14, 2015, about 1445 central daylight time, an experimental amateur-built Zenith STOL CH701, N4931M, was substantially damaged shortly after taking off from Weedon Field (EUF), Eufala, Alabama. The private pilot was not injured. Visual meteorological conditions prevailed, and no flight plan had been filed for the flight to Eu-Wish Airport (MU68), Hermann, Missouri. The personal flight was operating under the provisions of 14 Code of Federal Regulations Part 91.

According to the pilot, he had purchased the airplane the day before in Florida, and was flying it home, stopping at EUF to refuel. After refueling, the engine would not start, and the battery discharged. After charging the battery, the engine started "normally."

The pilot subsequently performed an engine run-up at 4,000 rpm without noting any anomalies. After which, he taxied to south end of runway 36 and commenced the takeoff. After applying full power, the airplane took longer than normal to take off due to cross wind conditions. About 50 feet above the runway, at mid-field, the engine began to run roughly and vibrate, and was not producing full power. The pilot attempted to "smooth out" the engine by adjusting the throttle; there was no mixture control.

The pilot then attempted to land the airplane back on the runway, but in the process, it veered off the left side and flipped upside-down. The pilot egressed the airplane, and reached back in to turn off the fuel valve as the emergency vehicles arrived.

According to the responding Federal Aviation Administration (FAA) inspector, the airplane had been moved to a hangar prior to her arrival. There, she noted that one blade of the three-bladed propeller was broken off and one was cracked. There was no bending or twisting of the propeller blades. There was no dripping or splattering of oil on the engine cowling. No anomalies were noted within the engine compartment, and all fuel samples were clear. The fuel bowl on the left side of the engine was full, and both wing fuel tanks were full of fuel.

The FAA inspector subsequently drove out along the runway to where the airplane was recovered, which was about 3,200 feet from the departure end.

With concurrence from the NTSB investigator in charge, the airplane was subsequently ground-transported to the pilot's home in Missouri.
========

Eufaula Fire and Rescue, along with officers from the Eufaula Police Department, responded to a 911 call in reference to an airplane crash at Eufaula’s Weedon Field on Wednesday, Oct. 14.

Units arrived shortly after the 3:48 p.m. call reporting the plane crash, to find the pilot of the single engine fixed wing aircraft out of the plane, despite the plane being upside down.

According to a press release from the EPD, the plane was approximately 125 yards to the west of the runway.

The pilot, Karl Paubel of Herman Missouri was not injured during the crash and did not require transport by Rescue.

A problem during takeoff with the mechanics of the plane is thought to have contributed to the accident. An official investigation by the FAA and local authorities is being conducted currently; no further information about the crash is available at this time.

No other aircraft were involved in the incident and the airport remains operational.

- Source:  http://www.dothaneagle.com

EUFAULA, AL (WTVM) -  On Wednesday, October 14 the Eufaula Police Department received a 911 call in reference to an airplane crash at Weedon Field at approximately 3:48 p.m. CST.

Eufaula Fire Department and police department units responded and discovered a fixed wing single engine aircraft upside down, approximately 125 yards to the west of the runway. 

The pilot, Karl Paubel of Herman, Missouri, was not injured. 

The FAA was contacted and the crash is under investigation by local and Federal authorities at this time.   No other aircraft were involved and the airport is operational at this time.

2 comments:

  1. Replies
    1. It's included in the National Transportation Safety Board final report.

      Flight Time:
      218 hours (Total, all aircraft), 6 hours (Total, this make and model), 8 hours (Last 90 days, all aircraft), 6 hours (Last 24 hours, all aircraft)

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