Thursday, October 16, 2014

Cessna 172S Skyhawk, N612SP, Sohail Air Ventures LLC: Accident occurred October 16, 2014 in Big Bear, California

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

Docket And Docket Items - National Transportation Safety Board: https://dms.ntsb.gov/pubdms


Aviation Accident Data Summary - National Transportation Safety Board: https://app.ntsb.gov/pdf

Sohail Air Ventures LLC: http://registry.faa.gov/N612SP

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entities:

Federal Aviation Administration / Flight Standards District Office: Riverside, California FSDO-21
Lycoming; Williamsport, Pennsylvania 
Cessna Aircraft; Wichita, Kansas

NTSB Identification: WPR15LA014
14 CFR Part 91: General Aviation
Accident occurred Thursday, October 16, 2014 in Big Bear, CA
Probable Cause Approval Date: 01/18/2017
Aircraft: CESSNA 172S, registration: N612SP
Injuries: 3 Serious.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

The commercial pilot was conducting a personal cross-country flight during daytime visual meteorological conditions over mountainous terrain. He reported that, about 30 minutes into the flight, the engine began to lose power. The airplane descended into a box canyon, and the pilot then attempted to maneuver the airplane to initiate a 180-degree turn out of the canyon toward lower terrain. The airplane continued to descend, and the stall warning horn sounded, so the pilot decided to land in trees.

First responders reported that the wing fuel tanks were breached and that fuel had drained out through holes in the wings. A postaccident examination of the airframe and engine revealed no evidence of any preexisting mechanical malfunctions or failures that would have precluded normal operation. The reason for the partial loss of engine power could not be determined.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
A partial loss of engine power for reasons that could not be determined because postaccident examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation.






HISTORY OF FLIGHT

On October 16, 2014, about 1400 Pacific daylight time, a Cessna 172S, N612SP, was substantially damaged when it collided with terrain near Big Bear City Airport (L35), Big Bear, California. Sohail Air Ventures LLC was operating the rental airplane under the provisions of 14 Code of Federal Regulations (CFR) Part 91. The commercial pilot and two passengers sustained serious injuries. Visual meteorological conditions prevailed and no flight plan was filed for the personal flight. The cross-country flight departed Corona, California, at an undetermined time with an intended destination of L35.

According to a Federal Aviation Administration (FAA) inspector, the pilot reported that he intended on flying to L35 for lunch prior to returning to Corona. Prior to the flight, he verified the fuel level of each fuel tank at 11 to 12 gallons of fuel and noted that the airplanes log sheet indicated 13 gallons of fuel should have been in each wing's fuel tank. The pilot further reported to the inspector that he anticipated getting fuel at Big Bear and that he planned to fly directly above the box canyons of the mountainous terrain west of the airport.

The pilot stated that thirty minutes into the flight, he noticed that he could not maintain altitude above the canyons and the engine was losing power. Once inside a box canyon, he maintained a position on the left side of the canyon with the intent to execute a right turn out of the canyon toward lower terrain. As the airplane continued to sink, he noticed that he did not have enough engine power to maintain a close proximity to the face of the mountain. The pilot further stated that when he heard the stall warning horn, he decided to initiate a landing on top of the trees instead of stalling [the airplane]. The pilot added that he had adjusted the mixture early in the flight, but the events of the flight happened too fast to attempt corrective adjustments immediately prior to the accident.

First responders confirmed that the wing fuel tanks were breached, and fuel had drained out through holes in the wings.

METEOROLOGICAL CONDITIONS

An aviation routine weather report (METAR) for L35, elevation 6,756 feet msl, located about 8 miles northeast of the accident site was issued at 1415. It indicated wind from 260 degrees at 10 knots, 10 miles or greater visibility, sky clear, temperature at 20 degrees C, dew point -17 degrees C, and an altimeter setting at 30.15 inches of mercury. The relative humidity was 7%.

A METAR for San Bernardino International Airport (SBD), elevation 1,159 feet msl, located about 15 miles southwest of the accident site, was issued at 1350. It indicated wind calm, 10 miles or greater visibility, sky few at 5,000 feet, temperature at 24 degrees C, dew point 8 degrees C, and an altimeter setting at 29.96 inches of mercury.

TESTS AND RESEARCH

Examination of the recovered wreckage was conducted on October 28, 2014, by representatives of the FAA, Cessna, and Lycoming Engines under the supervision of the National Transportation Safety Board investigator-in-charge.

Airframe

The electrical master switch was in the ON position. The ignition switch was in the BOTH position with the key in the switch. The auxiliary fuel pump switch was in the ON position. Investigators determined that the fuel selector valve was in the BOTH position. The gascolator contained a clear blue fluid that smelled like aviation gasoline; a water finding paste test had no response indicating that there was no water contamination. The screen was clean.

Engine

Investigators manually rotated the crankshaft with a tool in the vacuum pump drive pad. The crankshaft rotated freely, and the valves moved approximately the same amount of lift in firing order. The accessory gears turned freely. Investigators obtained thumb compression on all cylinders in firing order. A borescope inspection revealed no mechanical deformation on the valves, cylinder walls, or internal cylinder head. When each magneto drive shaft was rotated by hand, both magnetos produced spark at all posts.

The fuel pump's rubber diaphragm was intact and the pump contained a fluid consistent with the appearance and odor of aviation fuel.

Propeller

The two blades were bent and twisted. Both blades exhibited leading edge gouges and chordwise striations.

No evidence of any preexisting mechanical anomalies with the airframe or engine was found that would have precluded normal operation. For further information, see the NTSB Airframe and Engine Examination Notes within the public docket for this accident.

ADDITIONAL INFORMATION

Neither the pilot nor the operator submitted an NTSB form 6120.1, Pilot/Operator Aircraft Accident/Incident Report.










NTSB Identification: WPR15LA014
14 CFR Part 91: General Aviation
Accident occurred Thursday, October 16, 2014 in Big Bear, CA
Aircraft: CESSNA 172S, registration: N612SP
Injuries: 3 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On October 16, 2014, about 1400 Pacific daylight time, a Cessna 172S, N612SP, collided with terrain near Big Bear, California. Sohail Air Ventrues LLC was operating the rental airplane under the provisions of 14 Code of Federal Regulations (CFR) Part 91. The commercial pilot and two passengers sustained serious injuries. The airplane sustained substantial damage during the accident sequence. The cross-country personal flight departed Corona, California, at an undetermined time with a planned destination of Big Bear. Visual meteorological conditions (VMC) prevailed, and no flight plan had been filed.

The airplane collided with terrain while maneuvering in a mountainous area.


National Transportation Safety Board - Aviation Accident Factual Report: http://app.ntsb.gov/pdf 

National Transportation Safety Board  -   Docket And Docket Items: http://dms.ntsb.gov/pubdms

NTSB Identification: WPR15LA014
14 CFR Part 91: General Aviation
Accident occurred Thursday, October 16, 2014 in Big Bear, CA
Aircraft: CESSNA 172S, registration: N612SP
Injuries: 3 Serious.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

HISTORY OF FLIGHT

On October 16, 2014, about 1400 Pacific daylight time, a Cessna 172S, N612SP, was substantially damaged when it collided with terrain near Big Bear City Airport (L35), Big Bear, California. Sohail Air Ventures LLC was operating the rental airplane under the provisions of 14 Code of Federal Regulations (CFR) Part 91. The commercial pilot and two passengers sustained serious injuries. Visual meteorological conditions prevailed and no flight plan was filed for the personal flight. The cross-country flight departed Corona, California, at an undetermined time with an intended destination of L35.

According to a Federal Aviation Administration (FAA) inspector, the pilot reported that he intended on flying to L35 for lunch prior to returning to Corona. Prior to the flight, he verified the fuel level of each fuel tank at 11 to 12 gallons of fuel and noted that the airplanes log sheet indicated 13 gallons of fuel should have been in each wing's fuel tank. The pilot further reported to the inspector that he anticipated getting fuel at Big Bear and that he planned to fly directly above the box canyons of the mountainous terrain west of the airport.

The pilot stated that thirty minutes into the flight, he noticed that he could not maintain altitude above the canyons and the engine was losing power. Once inside a box canyon, he maintained a position on the left side of the canyon with the intent to execute a right turn out of the canyon toward lower terrain. As the airplane continued to sink, he noticed that he did not have enough engine power to maintain a close proximity to the face of the mountain. The pilot further stated that when he heard the stall warning horn, he decided to initiate a landing on top of the trees instead of stalling [the airplane]. The pilot added that he had adjusted the mixture early in the flight, but the events of the flight happened too fast to attempt corrective adjustments immediately prior to the accident.

First responders confirmed that the wing fuel tanks were breached, and fuel had drained out through holes in the wings.

METEOROLOGICAL CONDITIONS

An aviation routine weather report (METAR) for L35, elevation 6,756 feet msl, located about 8 miles northeast of the accident site was issued at 1415. It indicated wind from 260 degrees at 10 knots, 10 miles or greater visibility, sky clear, temperature at 20 degrees C, dew point -17 degrees C, and an altimeter setting at 30.15 inches of mercury. The relative humidity was 7%.

A METAR for San Bernardino International Airport (SBD), elevation 1,159 feet msl, located about 15 miles southwest of the accident site, was issued at 1350. It indicated wind calm, 10 miles or greater visibility, sky few at 5,000 feet, temperature at 24 degrees C, dew point 8 degrees C, and an altimeter setting at 29.96 inches of mercury.

TESTS AND RESEARCH

Examination of the recovered wreckage was conducted on October 28, 2014, by representatives of the FAA, Cessna, and Lycoming Engines under the supervision of the National Transportation Safety Board investigator-in-charge.

Airframe

The electrical master switch was in the ON position. The ignition switch was in the BOTH position with the key in the switch. The auxiliary fuel pump switch was in the ON position. Investigators determined that the fuel selector valve was in the BOTH position. The gascolator contained a clear blue fluid that smelled like aviation gasoline; a water finding paste test had no response indicating that there was no water contamination. The screen was clean.

Engine

Investigators manually rotated the crankshaft with a tool in the vacuum pump drive pad. The crankshaft rotated freely, and the valves moved approximately the same amount of lift in firing order. The accessory gears turned freely. Investigators obtained thumb compression on all cylinders in firing order. A borescope inspection revealed no mechanical deformation on the valves, cylinder walls, or internal cylinder head. When each magneto drive shaft was rotated by hand, both magnetos produced spark at all posts.

The fuel pump's rubber diaphragm was intact and the pump contained a fluid consistent with the appearance and odor of aviation fuel.

Propeller

The two blades were bent and twisted. Both blades exhibited leading edge gouges and chordwise striations.

No evidence of any preexisting mechanical anomalies with the airframe or engine was found that would have precluded normal operation. For further information, see the NTSB Airframe and Engine Examination Notes within the public docket for this accident.

ADDITIONAL INFORMATION

Neither the pilot nor the operator submitted an NTSB form 6120.1, Pilot/Operator Aircraft Accident/Incident Report.

NTSB Identification: WPR15LA014
14 CFR Part 91: General Aviation
Accident occurred Thursday, October 16, 2014 in Big Bear, CA
Aircraft: CESSNA 172S, registration: N612SP
Injuries: 3 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On October 16, 2014, about 1400 Pacific daylight time, a Cessna 172S, N612SP, collided with terrain near Big Bear, California. Sohail Air Ventrues LLC was operating the rental airplane under the provisions of 14 Code of Federal Regulations (CFR) Part 91. The commercial pilot and two passengers sustained serious injuries. The airplane sustained substantial damage during the accident sequence. The cross-country personal flight departed Corona, California, at an undetermined time with a planned destination of Big Bear. Visual meteorological conditions (VMC) prevailed, and no flight plan had been filed.

The airplane collided with terrain while maneuvering in a mountainous area.



 BIG BEAR LAKE (CBSLA.com/AP) — Authorities say a plane that crashed has left three people injured near Big Bear Lake. 

The California Highway Patrol reported the plane crash just before 2 p.m. Thursday in an area described as rugged, rocky and forested, San Bernardino County sheriff’s spokeswoman Cindy Bachman told KNX 1070 NEWSRADIO.

Wreckage of the light aircraft was seen near Highway 18 west of Glory Ridge about 12 miles west of Big Bear Airport, according to San Bernardino County Fire officials.

It was unclear whether the plane was taking off or landing, however, the pilot was able to call 911 when the plane crashed, Bachman said.

A man and two women were hoisted from the wreckage and airlifted out of the forest.

KCAL9’s Laurie Perez spoke with James Ponder of Loma Linda University Medical Center about the conditions of the victims.

The three people on board had moderate injuries, including bumps and bruises and perhaps some broken bones, according to Bachman. No fatalities were reported.

“I’m told they are in fair condition right now,” said Ponder. “Their vital signs are stable and within normal limits. The outcome is likely going to be favorable. The patients are conscious and may or may not be comfortable.”



Big Bear Lake, CA - Multiple people were injured Thursday afternoon in a plane crash reported near Big Bear Lake, according to the San Bernardino County Fire Department.

It happened around 2 p.m. about 12 miles west of Big Bear City Airport  near State Route 15 and Glory Ridge. The San Bernardino County Sheriff's Department referred to the plane as a "light aircraft" and stated there were a total of three injuries.

The victims were hoisted onto responding medical helicopters.

Both the fire and sheriff's departments responded to the scene and were posting updates on Twitter.

Coincidentally, a second plane was located near Thursday's scene from an accident that happened 8 to 10 years ago, according to emergency responders.























NTSB Identification: WPR13LA346 
14 CFR Part 91: General Aviation
Accident occurred Sunday, July 28, 2013 in Lone Pine, CA
Aircraft: BEECH 35-B33, registration: N82182
Injuries: 4 Minor.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On July 28, 2013, about 1516 Pacific daylight time, a Beech 35-B33, N82182, experienced a loss of engine power immediately after departing Lone Pine Airport, Lone Pine, California. The pilot executed a forced landing into desert terrain. All four occupants egressed the airplane with minor injuries, and a post accident fire ensued causing substantial damage. The airplane was registered to Sohail Air Ventures LLC, and operated by the private pilot, under the provisions of Title 14 Code of Federal Aviation, Part 91. Visual meteorological conditions prevailed for the flight, and a visual flight plan had not been filed. The flight originated at 1515 from Lone Pine Airport, and was destined for Corona, California.

The pilot stated that he diverted to Lone Pine Airport to wait out a weather system that was on their route of flight. About 1.5 hours after landing he decided to proceed on the planned route. He performed a full preflight and engine run up prior to departure. After takeoff he retracted the landing gear, and he noticed that the airplane was not climbing normally, and in fact, was in a slight descent. The engine started to sputter. The pilot performed a gear up forced landing. After the airplane stopped, he noticed a fire emanating from the left wing. His three passengers egressed through the right cabin door, and he followed. The fire spread and soon engulfed most of the airplane's cabin before firefighters arrived to put out the flames.


Beech 35-B33 Bonanza, SOHAIL AIR VENTURES LLC, N82282

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