Sunday, September 23, 2012

Cessna 150G, N8465J: Accident occurred September 21, 2012 in Corinth, Mississippi

http://registry.faa.gov/N8465J

NTSB Identification: ERA12LA574
 14 CFR Part 91: General Aviation
Accident occurred Friday, September 21, 2012 in Corinth, MS
Probable Cause Approval Date: 09/12/2013
Aircraft: CESSNA 150G, registration: N8465J
Injuries: 2 Minor.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

According to the pilot, after about 2 hours of uneventful flight, a loud noise came from the engine compartment, the engine cowling shook violently, and the engine experienced a total loss of power. During the subsequent descent, the pilot attempted to restart the engine. The propeller continued to windmill, but the engine did not restart. The pilot selected a field for a forced landing, and during the landing roll, the landing gear became entangled with the crop. The airplane then nosed over and came to rest inverted, and the pilot and his wife egressed with minor injuries.

Examination of the engine revealed that the crankshaft gear bolt locking tab washer and the alignment dowel for the gear mounting flange were fractured due to fatigue. This allowed the gear to rotate on the crankshaft. The fatigue resulted from improper torque application on the crankshaft gear bolt during overhaul, which had been completed 26 years and 643 total airplane flight hours before the accident. In service bulletins and service instructions, the engine manufacturer warned that improper installation of the crankshaft gear may result in "complete engine stoppage" and recommended that engines be overhauled after 12 years in service, even if the engine had not accumulated the manufacturer-specified 2,000-hour time-between-overhaul during that period.

The National Transportation Safety Board determines the probable cause(s) of this accident to be:

The improper torque application on the crankshaft gear bolt by maintenance personnel during an engine overhaul, which resulted in the fatigue failure of the locking tab washer and gear alignment dowel and subsequent engine stoppage. Contributing to the accident was the operator’s exceedence of the engine overhaul calendar year limits recommended by the engine manufacturer.

On September 21, 2012, about 1515 central daylight time, a Cessna 150G, N8465J, was substantially damaged during a forced landing following a total loss of engine power in cruise flight near Corinth, Mississippi. The certificated commercial pilot and a passenger received minor injuries. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight, which was conducted under the provisions of Title 14 Code of Federal Regulations Part 91.

According to the pilot/owner, the purpose of the flight was to return the airplane to his home in Oregon after he purchased it in Georgia. After receiving 2 hours of dual instruction in the airplane, the pilot and his wife departed Paulding Northwest Atlanta Airport (PUJ) and leveled the airplane in cruise flight at 4,500 feet. After approximately 2 hours of flight, with "everything perfect," a loud report came from the engine compartment, the engine cowling shook violently, and the engine experienced a total loss of power.

During the subsequent descent, the pilot attempted to restart the engine. The propeller continued to windmill, but the engine did not restart. The pilot selected a soy bean field for a forced landing, and during the landing roll, the landing gear became entangled with the crop. The airplane then nosed over and came to rest inverted, and the pilot and his wife egressed with minor injuries.

The pilot held a commercial pilot certificate with ratings for airplane single engine land and instrument airplane. He reported 960 total hours of flight experience, of which 60 hours were in the accident airplane make and model.
The airplane was manufactured in 1967, and a review of the maintenance records by a Federal Aviation Administration (FAA) maintenance inspector revealed that the most recent annual inspection was completed April 12, 2012, at 3,968 total aircraft hours. A major overhaul on the engine was completed November 12, 1986, and the engine was installed in the airplane July 22, 1988. The engine had accrued 643 total hours since that date, and 5 hours since the annual inspection.

On October 17, the engine was examined by an FAA inspector. The examination revealed that the crankshaft gear bolt locking tab washer and the alignment dowel for the gear mounting flange were fractured. The gear bolt and its associated components were examined in the NTSB Materials Laboratory in Washington, DC. The examination revealed that the locking tab and the alignment dowel displayed fracture surfaces consistent with fatigue. The bolt, the gear, and the gear mounting flange all displayed evidence of working and impact marks consistent with movement between the parts, indicative of insufficient clamping or pressure force at installation.

According to Lycoming Service Bulletin 475C, "Damage to the crankshaft gear and the counterbored recess in the rear of the crankshaft, as well as badly worn or broken gear alignment dowels are the result of improper assembly techniques or the reuse of worn or damaged parts during reassembly. Since a failure of the gear or the gear attaching parts would result in complete engine stoppage, the proper inspection and reassembly of these parts is very important."

According to Lycoming Service Instruction 1009AU, the recommended time between overhaul for the O-320 series engines was 2,000 hours. It further stated, "…all engines that do not accumulate the hourly period of time between overhauls specified in this publication are recommended to be overhauled in the twelfth year."


NTSB Identification: ERA12LA574 
14 CFR Part 91: General Aviation
Accident occurred Friday, September 21, 2012 in Corinth, MS
Aircraft: CESSNA 150G, registration: N8465J
Injuries: 2 Minor.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On September 21, 2012, about 1515 central daylight time, a Cessna 150G, N8465J, was substantially damaged during a forced landing following a total loss of engine power in cruise flight near Corinth, Mississippi. The certificated commercial pilot and a passenger received minor injuries. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight, which was conducted under the provisions of Title 14 Code of Federal Regulations Part 91.


According to the pilot/owner, the purpose of the flight was to return the airplane to his home in Oregon after he purchased it in Georgia. After receiving 2 hours of dual instruction in the airplane, the pilot and his wife departed Paulding Northwest Atlanta Airport (PUJ) and leveled the airplane in cruise flight at 4,500 feet. After approximately 2 hours of flight, with "everything perfect," a loud report came from the engine compartment, the engine cowling shook violently, and the engine experienced a total loss of power.

During the subsequent descent, the pilot attempted to restart the engine. The propeller continued to windmill, but the engine did not restart. The pilot selected a soy bean field for a forced landing, and during the landing roll, the landing gear became entangled with the crop. The airplane then nosed over and came to rest inverted, and the pilot and his wife egressed with minor injuries.

The pilot held a commercial pilot certificate with ratings for airplane single engine land and instrument airplane. He reported 960 total hours of flight experience, of which 60 hours were in the accident airplane make and model.
The airplane was manufactured in 1967, and a review of the maintenance records by a Federal Aviation Administration (FAA) maintenance inspector revealed that the most recent annual inspection was completed April 12, 2012, at 3,968 total aircraft hours. A major overhaul on the engine was completed November 12, 1986, and the engine was installed in the airplane July 22, 1988. The engine had accrued 643 total hours since that date, and 5 hours since the annual inspection.

On October 17, the engine was examined by an FAA inspector. The examination revealed that the crankshaft gear bolt locking tab washer and the alignment dowel for the gear mounting flange were fractured. The gear bolt and its associated components were examined in the NTSB Materials Laboratory in Washington, DC. The examination revealed that the locking tab and the alignment dowel displayed fracture surfaces consistent with fatigue. The bolt, the gear, and the gear mounting flange all displayed evidence of working and impact marks consistent with movement between the parts, indicative of insufficient clamping or pressure force at installation.

According to Lycoming Service Bulletin 475C, "Damage to the crankshaft gear and the counterbored recess in the rear of the crankshaft, as well as badly worn or broken gear alignment dowels are the result of improper assembly techniques or the reuse of worn or damaged parts during reassembly. Since a failure of the gear or the gear attaching parts would result in complete engine stoppage, the proper inspection and reassembly of these parts is very important."

According to Lycoming Service Instruction 1009AU, the recommended time between overhaul for the O-320 series engines was 2,000 hours. It further stated, "…all engines that do not accumulate the hourly period of time between overhauls specified in this publication are recommended to be overhauled in the twelfth year."



IDENTIFICATION
  Regis#: 8465J        Make/Model: C150      Description: 150, A150, Commuter, Aerobat
  Date: 09/21/2012     Time: 2115

  Event Type: Incident   Highest Injury: None     Mid Air: N    Missing: N
  Damage: Unknown

LOCATION
  City: CORINTH   State: MS   Country: US

DESCRIPTION
  AIRCRAFT FORCE LANDED IN A FIELD AND FLIPPED OVER, NEAR CORINTH, MS

INJURY DATA      Total Fatal:   0
                 # Crew:   2     Fat:   0     Ser:   0     Min:   0     Unk:    
                 # Pass:   0     Fat:   0     Ser:   0     Min:   0     Unk:    
                 # Grnd:         Fat:   0     Ser:   0     Min:   0     Unk:    


OTHER DATA
  Activity: Unknown      Phase: Landing      Operation: OTHER


  FAA FSDO: JACKSON, MS  (SW31)                   Entry date: 09/24/2012 







 
A couple walks away virtually unscathed after a plane crash in Alcorn County Friday afternoon. (Wayne Hereford, WTVA)


ALCORN COUNTY, Miss. (WTVA) -- An Oregon couple walks away virtually unscathed after their plane crashed in Alcorn County Friday afternoon. 

 Authorities say the Cessna 150 went down in a soybean field located in the Hinkle community.

The pilot, 63-year-old Ron Noland, and his wife Cindy were flying from Atlanta to Memphis when he told authorities the engine quit.

The crash remains under investigation by the National Transportation Safety Board.

http://www.wtva.com
 


ALCORN COUNTY, Miss. - Federal Aviation officials are investigating a plane crash in Alcorn County, Mississippi. 

 Officials with the Pisgah Community Volunteer Fire Department told 7 Eyewitness News they responded to the scene of the crash around 4:30 p.m. Friday.

They said a small plane began to have engine trouble as it was heading toward Memphis.

The pilot tried to make an emergency landing, but the plane flipped and landed upside down in a soybean field near County Road 518 near Rienzi, Mississippi.

Fortunately, no one was injured.

Officials have not released the names of the pilot and passenger.

7 Eyewitness News was told a representative with the Federal Aviation Administration was on the scene of the crash Saturday afternoon, and is making plans to bring the plane to a local airport by Monday.