Thursday, August 23, 2012

Piper PA-32R-301T, N362DM: Accident occurred August 23, 2012 in Riverview, Florida

http://registry.faa.gov/N362DM

NTSB Identification: ERA12LA524  
14 CFR Part 91: General Aviation
Accident occurred Thursday, August 23, 2012 in Riverview, FL
Probable Cause Approval Date: 08/13/2013
Aircraft: PIPER PA-32R-301T, registration: N362DM
Injuries: 3 Uninjured.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

The airplane experienced an electrical discrepancy shortly after an instrument departure. The pilot advised the air traffic controller that he would be returning to the airport. While en route, the pilot noted a film of oil on the windshield. It became more pronounced, and the engine oil pressure dropped to “0.” The pilot declared an emergency and landed the airplane on an interstate highway median. An 8-foot section of the left wing separated when it collided with a highway traffic sign during the landing roll. The postaccident engine examination revealed that the oil leak was from the propeller governor gasket; specifically, the leak originated from the lower left lock nut area that secures the control cable tube end support bracket to the governor’s engine-mounted stud. The nut and lock washer were not properly seated and anti-tamper putty was present. The disassembly of that area revealed that the lower left corner of the gasket had several cracks promulgating to that lower left section of the gasket, which permitted the oil to escape. The top section of the tube end of the support bracket was missing (broken off), which would not allow for an even mounting torque pressure between the gasket, the propeller governor, and the engine surfaces.

A review of the airplane’s maintenance records revealed no history of any discrepancies that would require the removal of the control cable support bracket tube end. Based on physical damage to the control cable bracket tube end, it is likely that, at an unknown time, the tube end was removed from the stud and damaged during installation. This did not permit a proper seal of the gasket, which created the leak.

The National Transportation Safety Board determines the probable cause(s) of this accident to be:

Damage to the propeller governor gasket during installation by unknown persons, which resulted in a total loss of engine oil in flight and a subsequent forced landing.

On August 23, 2012, about 0905 eastern daylight time, a Piper PA-32R-301T, N362DM, sustained substantial damage during a force landing on a highway near Tampa, Florida. The commercial pilot and two passengers were not injured. Visual meteorological conditions prevailed and an instrument flight rule flight plan was filed for the Title 14 Code of Federal Regulations Part 91, personal flight. The flight originated from the Peter O Knight Airport (TPF), Tampa, Florida, at 0900.

The pilot stated that during his preflight inspection he noted the engine required two quarts of oil, which was added before the flight. The ground run up check and the initial climb was uneventful. At approximately 4,000 feet means sea level the “Low Voltage” warning light on the instrument panel illuminated. He cycled the alternator; however, the warning light continued. The pilot communicated with the air traffic controller of the situation and was vectored back to TPF. During the return, it was noted that the windshield was accumulating a film of oil. At first, it seemed to be nothing more than a fine spray; however, it quickly covered the windshield on the pilot side. A stream of oil coming from the front of the engine cowling was observed. The pilot communicated to the controller of the loss of engine oil and was not sure that the airplane would be able to reach TPF. At this time the engine oil pressure indication was “0”. The pilot declared an emergency and advised his intentions on landing on a section of the interstate highway (I-75). The pilot maneuvered the airplane and landed on the median area between the north and south bound lanes. During the landing roll the left wing made contact with a highway sign before coming to a stop. All onboard were able to exit the airplane on their own.

An examination of the wreckage by the responding Federal Aviation Administration (FAA) inspector revealed an eight foot section of the outer left wing was separated. Engine oil was observed leaking from the forward section of the engine.

A postaccident engine examination by an FAA inspector revealed a noticeable cut on the lower left side of the propeller governor gasket. In addition, the lower left lock nut which secures one of three control cable bracket tube ends and propeller governor did not appear to be properly seated and the anti-tamper putty was present. The engine was serviced with six quarts of engine oil and the spark plugs were removed. The oil residue on the propeller governor was cleaned off to observe of any leaks. The engine was rotated several times with the starter. Fresh engine oil started seeping immediately from the area where the gasket was cut. The bracket, governor, and gasket were removed for examination. The lower left corner of the gasket broke off during removal. Several cracks were observed promulgating down to the lower section of the gasket where the oil leak was concentrated. The control cable support bracket tube end where the oil leak was from was observed with its top section missing (broken off). The other two tube ends were intact.

The airplane’s owner stated to the FAA inspector that the airplane had no history of any discrepancies with the airplane’s engine that would require the removal of that control cable support bracket. He did mention, a few years ago he had a maintenance facility correct an engine oil leak during an overnight stay. The mechanic on duty was not familiar with general aviation piston engines. The work order for that oil leak trouble shooting, dated November 4, 2007, was obtained by the FAA inspector. The replacement of an oil temperature sensor gasket and a repair to the breather tube corrected the leak. The engine has since then accumulated about 650 operational hours before the accident. A review of the airplane’s maintenance logbooks by FAA did not reveal documentation of the work performed on November 4, 2007. In addition, there were no entries that would account for the removal of the control cable support bracket tube ends from the propeller governor attachment engine mounted studs.


NTSB Identification: ERA12LA524 
 14 CFR Part 91: General Aviation
Accident occurred Thursday, August 23, 2012 in Riverview, FL
Aircraft: PIPER PA-32R-301T, registration: N362DM
Injuries: 3 Uninjured.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On August 23, 2012, about 0905 eastern daylight time, a Piper PA-32R-301T, N362DM, sustained substantial damage during a force landing on a highway near Tampa, Florida. The commercial pilot and two passengers were not injured. Visual meteorological conditions prevailed and an instrument flight rule flight plan was filed for the Title 14 Code of Federal Regulations Part 91, personal flight. The flight originated from the Peter O Knight Airport (TPF), Tampa, Florida, at 0900.

The pilot stated during his preflight he noted the engine required two quarts of oil, which was added before the flight. The ground run up check and the initial climb was uneventful. At approximately 4,000 feet means sea level the “Low Voltage” warning light on the instrument panel illuminated. He cycled the alternator; however, the warning light continued. The pilot communicated with the air traffic controller of the situation and was vectored back to TPF. During the return, it was noted that the windshield was accumulating a film of oil. At first, it seemed to be nothing more than a fine spray; however, it quickly covered the windshield on the pilot side. A stream of oil coming from the front of the engine cowling was observed. The pilot communicated to the controller of the loss of engine oil and was not sure that the airplane would be able to reach TPF. At this time the engine oil pressure indication was “0”. The pilot declared an emergency and advised his intentions on landing on a section of the interstate highway (I-75). The pilot maneuvered the airplane and landed on the median area between the north and south bound lanes. During the landing roll the left wing made contact with a highway sign before coming to a stop. All onboard were able to exit the airplane on their own.

The responding Federal Aviation Administration inspector examined the wreckage. The vertical stab and rudder were damaged by electrical wires that crossed the highway. The inspection also revealed that an eight foot section of the outer left wing was separated and oil was observed leaking from the forward section of the engine. The wreckage was retained for further examination of the engine. 


IDENTIFICATION
  Regis#: 362DM        Make/Model: PA32      Description: PA-32 Cherokee Six, Six, Saratoga, Turbo
  Date: 08/23/2012     Time: 1255

  Event Type: Accident   Highest Injury: None     Mid Air: N    Missing: N
  Damage: Substantial

LOCATION
  City: TAMPA   State: FL   Country: US

DESCRIPTION
  AIRCRAFT FORCE LANDED ON A HIGHWAY, STRUCK A POWERLINE AND SIGN, NEAR 
  TAMPA, FL

INJURY DATA      Total Fatal:   0
                 # Crew:   1     Fat:   0     Ser:   0     Min:   0     Unk:    
                 # Pass:   2     Fat:   0     Ser:   0     Min:   0     Unk:    
                 # Grnd:         Fat:   0     Ser:   0     Min:   0     Unk:    


OTHER DATA
  Activity: Pleasure      Phase: Landing      Operation: OTHER


  FAA FSDO: TAMPA, FL  (SO35)                     Entry date: 08/24/2012 




 








































 

GIBSONTON — A small plane made an emergency landing along Interstate 75 Thursday morning, ending up in the median near the Alafia River, according to the Florida Highway Patrol.

Three people were in the plane as it made a hard landing on the northbound shoulder near mile marker 252. No one was injured, according to Hillsborough County Fire Rescue.

The three people on board were pilot Charles Craig Pulliam, 64, of Tampa; Walter Womack, 50, of Spring Hill; and William Sisson, 58, also of Tampa, according to the Florida Highway Patrol.

Pulliam said only that he was headed to Miami on a business trip and declined to comment further.

The men, who were traveling in a black and white 2004 Piper Saratoga II TC, took off at about 8:30 a.m. from Peter O. Knight Airport on Davis Islands. The trio was headed to Opa-Locka Executive Airport in Miami, officials said.

Shortly after takeoff at about 4,000 feet, Pulliam noticed that a low voltage light came on in the cockpit and realized he was losing oil. He was forced to land on I-75, according to an FHP report.

Pulliam first tried to land on the southbound lanes of I-75, according to the report, but he spotted a traffic crash below and decided to land elsewhere. The plane's left wing was damaged after it struck a road sign.

The plane also hit a power line, but no outages were reported, TECO spokeswoman Cherie Jacobs said. 

Traffic was backed up for several miles on both sides of the interstate as officials investigated and removed the plane.