Sunday, September 22, 2019

Powerplant System / Component Malfunction / Failure: Titan T-51 Mustang, N51FB; accident occurred June 04, 2017 at Goodyear Airport (KGYR), Maricopa County, Arizona


The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entities:

Federal Aviation Administration / Flight Standards District Office; Scottsdale, Arizona
Transport Accident Investigation Commission; Wellington, FN 
 
Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf


Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms


http://registry.faa.gov/N51FB




Location: Goodyear, AZ
Accident Number: WPR17LA121
Date & Time: 06/04/2017, 0917 MST
Registration: N51FB
Aircraft: Bob Frederick Titan T-51
Aircraft Damage: Substantial
Defining Event: Powerplant sys/comp malf/fail
Injuries: 1 None
Flight Conducted Under: Part 91: General Aviation - Personal 

On June 4, 2017, at 0917 mountain standard time, an experimental amateur-built Titan T-51 Mustang, N51FB, lost thrust to the propeller during the initial takeoff climb from Phoenix Goodyear Airport, Goodyear, Arizona. The pilot was not injured, and the airplane sustained substantial damage to the left wing and aft fuselage during the forced landing. The airplane was registered to a private individual and the pilot was operating the airplane as a Title 14 Code of Federal Regulations Part 91 personal flight. Visual meteorological conditions prevailed for the local flight, and no flight plan had been filed.

The pilot reported that immediately after takeoff, the airplane began to vibrate. He stated that it felt like one of the wheels was still spinning, so he applied the brakes, but the vibration continued. As he transitioned the airplane to the downwind leg, the vibration increased, and the engine then experienced an overspeed and lost all power. As the pilot initiated a return to runway 21, the cockpit filled with smoke, and unable to reach the runway, the airplane landed short in a dirt area, where the landing gear collapsed (See Figure 1).


Figure 1 – Airplane at the Accident Site 


Pilot Information


Certificate: Airline Transport; Flight Instructor
Age: 67, Male
Airplane Rating(s): Single-engine Land
Seat Occupied: Front
Other Aircraft Rating(s): None
Restraint Used:
Instrument Rating(s): Airplane
Second Pilot Present: No
Instructor Rating(s): Airplane Multi-engine; Airplane Single-engine
Toxicology Performed: No
Medical Certification: Class 1 With Waivers/Limitations
Last FAA Medical Exam: 03/16/2017
Occupational Pilot: Yes
Last Flight Review or Equivalent: 05/04/2016
Flight Time:  10377 hours (Total, all aircraft), 183 hours (Total, this make and model), 8823 hours (Pilot In Command, all aircraft), 6 hours (Last 24 hours, all aircraft)

Aircraft and Owner/Operator Information

Aircraft Make: Bob Frederick
Registration: N51FB
Model/Series: Titan T-51
Aircraft Category:Airplane 
Year of Manufacture: 2015
Amateur Built: Yes
Airworthiness Certificate: Experimental
Serial Number: MO4XXXS0HK0052
Landing Gear Type: Retractable - Tailwheel
Seats:2 
Date/Type of Last Inspection: 10/26/2016, Condition
Certified Max Gross Wt.: 1850 lbs
Time Since Last Inspection: 20 Hours
Engines: 1 Reciprocating
Airframe Total Time: 43.4 Hours at time of accident
Engine Manufacturer: Suzuki
ELT: C91A installed, not activated
Engine Model/Series:H27A 
Registered Owner: Robert Frederick Jr.
Rated Power: 183 hp
Operator:On file 
Operating Certificate(s) Held: None

The airplane kit was manufactured by Titan Aircraft in the United States, and the kit was assembled by the owner, who completed construction in July 2015.

The most recent conditional inspection was completed on October 26, 2016, and at the time of the accident the airplane and engine had accrued 43.4 hours of total flight time.

The airplane was equipped with a Suzuki H27A six-cylinder, 2.7-liter automobile engine. The engine was one of the types recommended by Titan Aircraft for installation in the T51. The pilot purchased the engine used, and reported that it had accrued about 2,000 miles of use in its donor automobile prior to installation.

A Whirl Wind four-blade 100-4-84D hydraulically-controlled constant-speed composite propeller was driven by a reduction gearbox manufactured in New Zealand by Autoflight Ltd. The propeller was supplied to the owner by Titan Aircraft, and was the type recommended by Titan Aircraft and Autoflight for the airframe, engine, and gearbox combination.

Representatives from Titan Aircraft did not respond to multiple requests for technical support by NTSB investigators, and did not provide any information or assistance during the investigation. Autoflight provided summary information regarding basic gearbox specifications.




Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light: Day
Observation Facility, Elevation: KGYR, 968 ft msl
Distance from Accident Site: 1 Nautical Miles
Observation Time: 1620 UTC
Direction from Accident Site: 218°
Lowest Cloud Condition: Clear
Visibility:  10 Miles
Lowest Ceiling: None
Visibility (RVR):
Wind Speed/Gusts: Calm /
Turbulence Type Forecast/Actual:
Wind Direction:
Turbulence Severity Forecast/Actual:
Altimeter Setting: 29.84 inches Hg
Temperature/Dew Point: 33°C / 5°C
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: GOODYEAR, AZ (GYR)
Type of Flight Plan Filed: None
Destination: GOODYEAR, AZ (GYR)
Type of Clearance: VFR
Departure Time: 0915 MST
Type of Airspace: Class D

Airport Information

Airport: PHOENIX GOODYEAR (GYR)
Runway Surface Type: Asphalt
Airport Elevation: 968 ft
Runway Surface Condition: Dry
Runway Used: 21
IFR Approach: None
Runway Length/Width: 8500 ft / 150 ft
VFR Approach/Landing: Forced Landing 

Wreckage and Impact Information

Crew Injuries: 1 None
Aircraft Damage: Substantial
Passenger Injuries: N/A
Aircraft Fire: In-Flight
Ground Injuries: N/A
Aircraft Explosion: None
Total Injuries: 1 None
Latitude, Longitude: 33.433889, -112.366944 (est) 

Engine

Post-accident examination revealed two holes in the lower left side of the engine crankcase, adjacent to the cylinder number 4 crankshaft journal. The oil sump was removed, and contained dark colored oil. The oil level was above the oil pickup tube inlet, and the sump contained significant quantities of metallic shards and remnants of connecting rod components. The engine exhibited evidence of a catastrophic internal failure, with the connecting rods of cylinders number 1 and 4 separating from the crankshaft, and extensive peening and gouging of the internal surfaces of the crankcase.

The oil cooler contained oil, and the internal gear and cavity of the oil pump was intact and free of damage.

Propeller Speed Reduction Gearbox


The propeller speed reduction gearbox was composed of a two-piece cast aluminum case, mounted directly to the engine flywheel bell housing, and oriented with the input shaft at the bottom. The input shaft was connected to the engine crankshaft via a "CENTAFLEX" flexible rubber coupling, manufactured by CENTA Antriebe Kirschey GmbH. The gearbox drivetrain consisted of the input drive gear and shaft, an idler gear, and an output drive gear fitted to the propeller flange.

According to the gearbox manufacturer, the gear ratios were designed as a "hunting tooth set", to minimize gear tooth wear, and distribute propeller blade passage across different engine strokes. Lubricant was shared with the propeller governor via an external oil sump mounted on the right side of the gearbox. The recommended lubricant was Synthetic 75W-90 gear oil, and the airplane builder reported that this was the oil he used.

Gearbox Examination

Initial gearbox disassembly was performed by the builder after he drained the oil from the sump and gearbox. He reported that the oil in the gearbox appeared dark in color, and full of black fragments.


Figure 2 – Input Drive Gear




Figure 3 – Idler Gear

Follow-up NTSB examination of the gearbox components revealed that the input drive gear had shed all of its teeth at its contact area with the idler gear (See Figure 2). The idler gear teeth were all deformed and rounded, with numerous sections of their tips and faces missing (See Figure 3). Both damaged gears exhibited a dark surface tint. The inner and outer rings of the input drive gear bearing on the forward side were intact, but its polymer cage had disintegrated and/or melted. The balls were round and intact, and remained within the bearing, and the ring-to-ball contact faces were free of damage. All remaining drive gear bearings were intact and were free of damage.

The bottom of the gearbox case contained crushed slivers of gear teeth coated in oil. The failure surfaces of the input drive gear teeth were obliterated and smeared, preventing a detailed examination of their fracture surfaces.

The input and idler gears were sent to the NTSB Materials Laboratory for hardness and microstructure evaluation. A complete report is contained within the public docket.

As part of the Materials Laboratory evaluation, the drive gear was cross-sectioned at an undamaged location adjacent to the damaged teeth. Because all teeth of the idler gear were damaged, a cross-section could only be taken at a damaged location. Hardness testing of each gear was performed at a tooth face, tooth root, and the inside diameter of the gear case. Micrographs for 100X, 200X and 500X magnification were also taken at a tooth face, tooth core, and inside diameter of the gear case.

The results for the drive gear indicated maximum hardness values of between 49.3, and 49.7 Rockwell C (HRC), with case depths of between 0.029in and 0.034in.

The results for the idler gear indicated maximum hardness values of between 42.5 and 54.6 HRC, with a case depth of 0.025in for the inside diameter edge (case depth is typically defined as the depth of hardness where the hardened layer reaches the same hardness and properties as the base or core material). Damage prevented an accurate assessment of the case depth at the other locations.

The effective case depth for both gears (the depth where a hardness measurement drops below a specified point - such as 50 HRC for high carbon steel) could not be determined because almost all the hardness values were below 50 HRC.

According to the gearbox manufacturer, the gears were made of EN39B steel, case hardened to 58/60 Rockwell.

Other T-51 Accident

Another accident involving a Titan T-51 Mustang equipped with the same speed reduction gearbox occurred in New Zealand on August 23, 2010. A Safety investigation report provided by the Transport Accident Investigation Commission of New Zealand revealed that the input, idler, and output gears had suffered complete gear tooth failure and severe overheating damage. The idler gear had experienced heavy wear on the teeth to such an extent that they had worn to a knife edge, and the drive gear had shed all of its teeth in a similar manner to that observed in the gearbox of N51FB. The investigation determined that the builder had been using an oversized propeller, and that while other failure modes could not be definitively ruled out, it was likely that the failure was caused by harmonics associated with the untested propeller, gearbox, and engine combination.

2 comments:

  1. Yikes ! a used automobile engine used in aircraft,I know they are used but the quality of this engine seems a bit suspect ?

    ReplyDelete
  2. It sounds like the initial point of failure was the gear reduction. That seems to be a major weakness of auto conversions. The engine damage was probably overspeed related.

    ReplyDelete