Wednesday, January 13, 2016

Cessna 172N Skyhawk, N737EZ: Fatal accident occurred January 12,2016 near Fox Stephens Field - Gilmer Municipal Airport ( KJXI) Gilmer, Upshur County, Texas

The National Transportation Safety Board traveled to the scene of this accident.

Additional Participating Entities:

Federal Aviation Administration / Flight Standards District Office; Irving, Texas
Textron Aviation; Wichita, Kansas
Lycoming Engines; Williamsport, Pennsylvania

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf 

Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms


Aviation Accident Data Summary - National Transportation Safety Board:  https://app.ntsb.gov/pdf

http://registry.faa.gov/N737EZ

NTSB Identification: CEN16FA083
14 CFR Part 91: General Aviation
Accident occurred Tuesday, January 12, 2016 in Gilmer, TX
Probable Cause Approval Date: 07/20/2017
Aircraft: CESSNA 172N, registration: N737EZ
Injuries: 1 Fatal, 1 Uninjured.

NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

The private pilot and one passenger departed on the approximate 35-minute personal flight with an unknown quantity of fuel onboard. Later that evening, they departed to return to their home airport in night visual meteorological conditions without adding additional fuel during their stop. While on final approach to their home airport, the engine lost total power and the airplane impacted trees and terrain. The passenger stated that the engine did not sound any different during the accident flight than on any of the previous flights and that there was no indication of a problem with the airplane when the engine lost power. Postaccident examination of the wreckage revealed no usable fuel within the airplane's fuel system, and no mechanical anomalies that would have precluded normal operation; therefore, it is likely that the airplane experienced a total loss of engine power as a result of fuel exhaustion. While it is unknown what preflight fuel planning the pilot performed and the extent of his preflight inspection, it is apparent that both were inadequate; had he performed both properly, he likely would not have run out of fuel.

Recorded GPS data showed that the pilot flew the traffic pattern 400-600 ft lower than the recommended 1,000-ft above airport elevation and turned to the base leg of the traffic pattern farther from the runway than recommended. Had the pilot flown the traffic pattern at the recommended altitude and distance from the runway, it may have been possible for the airplane to glide to the runway following the loss of engine power.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

The pilot's inadequate preflight planning and inspection, which resulted in a total loss of engine power due to fuel exhaustion. Contributing to the accident was the pilot's failure to maintain an appropriate traffic pattern altitude and distance from the runway, which may have allowed the airplane to glide to the runway following the loss of engine power.


Samuel Oliver Lucky 




HISTORY OF FLIGHT

On January 12, 2016, about 1954 central standard time, a Cessna 172N, N737EZ, was substantially damaged when it impacted wooded terrain following a loss of engine power about 0.5 nautical mile south/southwest of Fox Stephens Field-Gilmer Municipal Airport (JXI), Gilmer, Texas. The private pilot was fatally injured and the passenger sustained serious injuries. The airplane was privately owned and operated by the pilot under 14 Code of Federal Regulations Part 91 as a personal flight. No flight plan was filed and the flight was not receiving any air traffic control services. Night visual meteorological conditions (VMC) prevailed for the flight that departed from Sulphur Springs Municipal Airport (SLR), Sulphur Springs, Texas, about 1916 and was returning to JXI.

The passenger, who was the pilot's wife, stated that the pilot filled both of the airplane's wing fuel tanks a couple of days before the flight to SLR. The tanks were fueled from three gas cans that had a capacity of 5 gallons each and one that had a capacity of 6 gallons. However, the investigation could not determine how much total fuel was onboard the airplane following the refueling. The passenger said that she obtained the fuel from the airport in Gladewater, Texas, 1 or 1 1/2 weeks before the accident because the fuel there was cheaper than at JXI. The gas cans had been used solely for fueling the airplane. She said that the flight departed from JXI to SLR, was 33-34 minutes long, and there were no stops. 

The pilot's brother, who had dinner with the pilot and his wife near SLR, stated that he did not see the airplane depart from SLR. He said that when he left, the pilot was still getting the airplane warmed up, it was kind of cold outside, and the pilot's wife was already sitting in the airplane. The pilot's brother said that the airplane was tied down, and the pilot untied the tie downs and checked the airplane wings. The pilot then got into the airplane, turned the lights on, had the instrument lights on, and was "looking at things." He said that "he doesn't know how much looking around" at the airplane the pilot was doing and he said that he did not see the pilot reach up and shake the wings because he, the pilot's brother, was not paying attention. 

The passenger stated that the return flight was 29-32 minutes long with no stops. The cruise altitude for both legs of the flight was 3,500-3,700 ft. She said that the engine did not sound any different during the accident flight than from previous flights. There was no indication of a problem with the airplane when the engine lost power. She said that there were no alarms, and the pilot did not say anything was wrong before the engine quit. 

The airplane was located by law enforcement on January 13, 2016, about 0105, after it was reported overdue by a family member.

PERSONNEL INFORMATION

The pilot, age 73, held a private pilot certificate with a rating for airplane single-engine land. The pilot was issued a Federal Aviation Administration (FAA) third-class medical certificate on July 7, 2014, with no limitations. 

Review of the pilot's logbook showed that the pilot had accumulated 259.15 total hours of flight experience, of which 202.55 hours were in the accident airplane. The pilot's total flight experience at night was 13.5 hours. The two most recent entries for flight at night were 1.6 hours in February 2014 and 0.8 hours in December 2015. 

The pilot's most recent flight review was completed on September 22, 2015, in the accident airplane. 

AIRCRAFT INFORMATION

The airplane, S/N 17269373, was registered to the pilot in July 2008. It was equipped with a Lycoming O-320-H2AD reciprocating engine, S/N L-3869-76. The airplane's most recent annual inspection was completed on December 9, 2015, about 3 flight hours before the accident. 

The airplane was equipped with standard capacity tanks, which held 21.5 gallons each and provided a total capacity of 43 gallons and 40 gallons of usable fuel.

METEOROLOGICAL INFORMATION

The 1955 automated weather observation at JXI included calm wind, clear skies, 10 statute miles visibility, temperature 6°C, dew point 2°C, and an altimeter setting of 30.24 inches of mercury.

According to data from the US Naval Observatory, sunset occurred at 1734 on the evening of the accident, and the end of civil twilight was at 1800. Moonset occurred at 2039. The phase of the moon was a waxing crescent, with 9% of the moon's visible disk illuminated. 




WRECKAGE AND IMPACT INFORMATION

The airplane came to rest on a heading of about 040° about 0.5 nautical mile south/southwest of runway 36 in a wooded area. A wreckage path measured about 197 ft in length and was oriented on an approximate 050° heading. The airplane was resting on its left side and on top of the left wing, which was folded over and oriented along the length of the fuselage. The wings, flight control surfaces, and stabilizers were attached to the airframe. The wing flap cockpit control and the flap actuator were in the 20° positions. Flight control continuity from the control surfaces to the cockpit controls was confirmed. 

There was no fuel smell or leakage at the accident site. Both wing fuel tank caps and the auxiliary fuel tank cap were intact and secure. There was no usable fuel in the wing fuel tanks. About 8 oz of blue-colored liquid consistent in color with 100 low-lead aviation fuel was drained from the auxiliary fuel tank, and about 1 oz was drained from the airframe fuel strainer assembly. The fuel strainer did not contain debris. Removal and disassembly of the carburetor showed that the carburetor bowl contained about 2 oz of a liquid consistent in color with a mixture of oil and fuel. The remaining fuel from the auxiliary fuel tank, airframe fuel strainer, and carburetor bowl was tested for water using water sensing paste; the test showed no indication for the presence of water.

The propeller was attached to the propeller hub and engine. Neither propeller blade exhibited S-shaped bending or chordwise scratching. 

The cockpit master/alternator switch was in the off positon, and the magneto key switch was in the both positon.

Throttle and mixture control continuity was confirmed from the cockpit controls to the carburetor. Examination of the engine confirmed the suction and expulsion of air through the top spark plug holes after removal of the spark plugs and when the engine was rotated through by hand using the propeller. Continuity of engine to the accessory section and of the valve train to the accessory section was confirmed during engine rotation. Rotation of both magnetos produced electrical spark through each magneto lead.

An Adventure Pilot iFly multifunction display was recovered from the wreckage and sent to the NTSB Vehicle Recorder Division for download.




MEDICAL AND PATHOLOGICAL INFORMATION

The Dallas County Medical Examiner's Office conducted an autopsy of the pilot on January 14, 2016. The autopsy report stated that the pilot died as a result of blunt force injuries. The manner of death was accident.

The FAA Bioaeronautical Sciences Research Laboratory, Oklahoma City, Oklahoma performed toxicology testing. Testing was negative for carbon monoxide and ethanol. Losartan, an antihypertensive medication, was detected in the liver, and pravastatin, a high cholesterol medication, was detected in the blood and liver. Neither medication is noted to adversely affect pilot performance.

TESTS AND RESEARCH

An Adventure Pilot iFly was recovered from the wreckage. The iFly unit is an externally-powered, multi-function display and GPS receiver with a high resolution, LCD touchscreen display. The unit included a built-in navigational database and was optionally capable of receiving inflight ADS-B information, including weather radar, airport weather reports, weather forecasts, and traffic advisories. The navigational and information features included terrain warnings, airspace alerts, and display of en route visual flight rule and instrument flight rule (IFR) navigational information and IFR approach charts.

Download of the recovered iFly unit showed two log files that corresponded to the date of the accident flight. The most recent log, the accident flight, spanned from 19:16:21 to 19:53:53, which captured the accident flight from JXI to SLR. The second log file spanned from 16:42:46 to 17:26:59 and captured the previous flight from SLR to JXI. 

During the last minute of flight, the airplane's speed steadily decreased from 79 knots to the last recorded speed of 29 knots. The GPS altitude also steadily decreased from 832 ft to 425 ft. At 19:53:16 the airplane was at 649 ft GPS altitude, 74 kts, and about 35 degrees past and .43 miles from the approach end of runway 36 at JXL. At 19:53:27 the airplane was at 583 ft GPS altitude, 70 kts, and about 55 degrees past and .62 miles from the approach end of runway 36. 

Figure 1 shows the flight track the airplane followed, which is consistent with a left downwind and a left base leg for runway 36 at JXI, which had an airport elevation of 415 feet. The GPS track indicated the airplane began a turn for the left base when the airplane reached about 55 degrees past abeam the approach end of runway 36, as depicted in Figure 1.

Plot of recorded data points for the accident flight showing the accident location near JXI. 

ADDITIONAL INFORMATION

Title 14 Code of Federal Regulations 61.57 Recent flight experience: Pilot in command, states in part:

(b)Night takeoff and landing experience. 

(1) Except as provided in paragraph (e) of this section, no person may act as pilot in command of an aircraft carrying passengers during the period beginning 1 hour after sunset and ending 1 hour before sunrise, unless within the preceding 90 days that person has made at least three takeoffs and three landings to a full stop during the period beginning 1 hour after sunset and ending 1 hour before sunrise, and – 

(i) The person acted as the sole manipulator of the flight controls; and 

(ii) The required takeoffs and landings were performed in an aircraft of the same category, class, and type (if a type rating is required), and, if the aircraft to be flown is an airplane with a tailwheel, the takeoffs and landings must have been made to a full stop in an airplane with a tailwheel.

Advisory Circular 90-66A - Recommended Standards Traffic Patterns for Aeronautical Operations at Airports without Operating Control Towers, stated in part:

c. It is recommended that airplanes observe a 1,000-foot above ground level (AGL) traffic pattern altitude. Large and turbine-powered airplanes should enter the traffic pattern at an altitude of 1,500 feet AGL or 500 feet above the established pattern altitude. A pilot may vary the size of the traffic pattern depending on the aircraft's performance characteristics.

d. The traffic pattern altitude should be maintained until the aircraft is at least abeam the approach end of the landing runway on the downwind leg.

e. The base leg turn should commence when the aircraft is at a point approximately 45 degrees relative bearing from the runway threshold.

The Cessna 172N airplane flight manual, Section 3, Amplified Emergency Procedures, Engine Failure, contained a chart of maximum glide distance, which is shown in Figure 2. 


The Cessna 172N flight manual chart for maximum glide distance shows an approximate glide distance of 1 nautical mile at an altitude of 500 ft above ground level with a speed of 65 knots indicated airspeed, propeller windmilling, flaps up, and zero wind.










NTSB Identification: CEN16FA083 
14 CFR Part 91: General Aviation
Accident occurred Wednesday, January 13, 2016 in Gilmer, TX
Aircraft: CESSNA 172N, registration: N737EZ
Injuries: 1 Fatal, 1 Uninjured.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

On January 13, 2016, about 0105 central standard time, a Cessna 172N, N737EZ, was located in a wooded area about 0.5 nautical miles south/southwest of runway 36 at Fox Stephens Field - Gilmer Municipal Airport (JXI), Gilmer, Texas. The airplane was found by a Texas Department of Public Safety Officer during a search with the Gilmer Police Department for an airplane that was reported by a family member to be overdue. The private non-instrument rated pilot was fatally injured and a passenger sustained serious injuries. The airplane received substantial damage to the wings, fuselage, and empennage. The airplane was registered to and operated by the pilot under 14 Code of Federal Regulations Part 91 as a personal flight that was not operating on a flight plan nor receiving any air traffic control services. Night instrument meteorological conditions prevailed for the flight that departed from Sulphur Springs Municipal Airport, Sulphur Springs, Texas on January 12, 2016 about 1915 and was returning to JXI. The National Transportation Safety Board traveled to the scene of this accident.

Additional Participating Entities:
Federal Aviation Administration / Flight Standards District Office; Irving, Texas
Textron Aviation; Wichita, Kansas
Lycoming Engines; Williamsport, Pennsylvania

Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

http://registry.faa.gov/N737EZ

NTSB Identification: CEN16FA083
14 CFR Part 91: General Aviation
Accident occurred Tuesday, January 12, 2016 in Gilmer, TX
Aircraft: CESSNA 172N, registration: N737EZ
Injuries: 1 Fatal, 1 Uninjured.

NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

HISTORY OF FLIGHT

On January 12, 2016, about 1954 central standard time, a Cessna 172N, N737EZ, was substantially damaged when it impacted wooded terrain following a loss of engine power about 0.5 nautical mile south/southwest of Fox Stephens Field-Gilmer Municipal Airport (JXI), Gilmer, Texas. The private pilot was fatally injured and the passenger sustained serious injuries. The airplane was privately owned and operated by the pilot under 14 Code of Federal Regulations Part 91 as a personal flight. No flight plan was filed and the flight was not receiving any air traffic control services. Night visual meteorological conditions (VMC) prevailed for the flight that departed from Sulphur Springs Municipal Airport (SLR), Sulphur Springs, Texas, about 1916 and was returning to JXI.

The passenger, who was the pilot's wife, stated that the pilot filled both of the airplane's wing fuel tanks a couple of days before the flight to SLR. The tanks were fueled from three gas cans that had a capacity of 5 gallons each and one that had a capacity of 6 gallons. However, the investigation could not determine how much total fuel was onboard the airplane following the refueling. The passenger said that she obtained the fuel from the airport in Gladewater, Texas, 1 or 1 1/2 weeks before the accident because the fuel there was cheaper than at JXI. The gas cans had been used solely for fueling the airplane. She said that the flight departed from JXI to SLR, was 33-34 minutes long, and there were no stops. 

The pilot's brother, who had dinner with the pilot and his wife near SLR, stated that he did not see the airplane depart from SLR. He said that when he left, the pilot was still getting the airplane warmed up, it was kind of cold outside, and the pilot's wife was already sitting in the airplane. The pilot's brother said that the airplane was tied down, and the pilot untied the tie downs and checked the airplane wings. The pilot then got into the airplane, turned the lights on, had the instrument lights on, and was "looking at things." He said that "he doesn't know how much looking around" at the airplane the pilot was doing and he said that he did not see the pilot reach up and shake the wings because he, the pilot's brother, was not paying attention. 

The passenger stated that the return flight was 29-32 minutes long with no stops. The cruise altitude for both legs of the flight was 3,500-3,700 ft. She said that the engine did not sound any different during the accident flight than from previous flights. There was no indication of a problem with the airplane when the engine lost power. She said that there were no alarms, and the pilot did not say anything was wrong before the engine quit. 

The airplane was located by law enforcement on January 13, 2016, about 0105, after it was reported overdue by a family member.

PERSONNEL INFORMATION

The pilot, age 73, held a private pilot certificate with a rating for airplane single-engine land. The pilot was issued a Federal Aviation Administration (FAA) third-class medical certificate on July 7, 2014, with no limitations. 

Review of the pilot's logbook showed that the pilot had accumulated 259.15 total hours of flight experience, of which 202.55 hours were in the accident airplane. The pilot's total flight experience at night was 13.5 hours. The two most recent entries for flight at night were 1.6 hours in February 2014 and 0.8 hours in December 2015. 

The pilot's most recent flight review was completed on September 22, 2015, in the accident airplane. 

AIRCRAFT INFORMATION

The airplane, S/N 17269373, was registered to the pilot in July 2008. It was equipped with a Lycoming O-320-H2AD reciprocating engine, S/N L-3869-76. The airplane's most recent annual inspection was completed on December 9, 2015, about 3 flight hours before the accident. 

The airplane was equipped with standard capacity tanks, which held 21.5 gallons each and provided a total capacity of 43 gallons and 40 gallons of usable fuel.

METEOROLOGICAL INFORMATION

The 1955 automated weather observation at JXI included calm wind, clear skies, 10 statute miles visibility, temperature 6°C, dew point 2°C, and an altimeter setting of 30.24 inches of mercury.

According to data from the US Naval Observatory, sunset occurred at 1734 on the evening of the accident, and the end of civil twilight was at 1800. Moonset occurred at 2039. The phase of the moon was a waxing crescent, with 9% of the moon's visible disk illuminated. 

WRECKAGE AND IMPACT INFORMATION

The airplane came to rest on a heading of about 040° about 0.5 nautical mile south/southwest of runway 36 in a wooded area. A wreckage path measured about 197 ft in length and was oriented on an approximate 050° heading. The airplane was resting on its left side and on top of the left wing, which was folded over and oriented along the length of the fuselage. The wings, flight control surfaces, and stabilizers were attached to the airframe. The wing flap cockpit control and the flap actuator were in the 20° positions. Flight control continuity from the control surfaces to the cockpit controls was confirmed. 

There was no fuel smell or leakage at the accident site. Both wing fuel tank caps and the auxiliary fuel tank cap were intact and secure. There was no usable fuel in the wing fuel tanks. About 8 oz of blue-colored liquid consistent in color with 100 low-lead aviation fuel was drained from the auxiliary fuel tank, and about 1 oz was drained from the airframe fuel strainer assembly. The fuel strainer did not contain debris. Removal and disassembly of the carburetor showed that the carburetor bowl contained about 2 oz of a liquid consistent in color with a mixture of oil and fuel. The remaining fuel from the auxiliary fuel tank, airframe fuel strainer, and carburetor bowl was tested for water using water sensing paste; the test showed no indication for the presence of water.

The propeller was attached to the propeller hub and engine. Neither propeller blade exhibited S-shaped bending or chordwise scratching. 

The cockpit master/alternator switch was in the off positon, and the magneto key switch was in the both positon.

Throttle and mixture control continuity was confirmed from the cockpit controls to the carburetor. Examination of the engine confirmed the suction and expulsion of air through the top spark plug holes after removal of the spark plugs and when the engine was rotated through by hand using the propeller. Continuity of engine to the accessory section and of the valve train to the accessory section was confirmed during engine rotation. Rotation of both magnetos produced electrical spark through each magneto lead.

An Adventure Pilot iFly multifunction display was recovered from the wreckage and sent to the NTSB Vehicle Recorder Division for download.

MEDICAL AND PATHOLOGICAL INFORMATION

The Dallas County Medical Examiner's Office conducted an autopsy of the pilot on January 14, 2016. The autopsy report stated that the pilot died as a result of blunt force injuries. The manner of death was accident.

The FAA Bioaeronautical Sciences Research Laboratory, Oklahoma City, Oklahoma performed toxicology testing. Testing was negative for carbon monoxide and ethanol. Losartan, an antihypertensive medication, was detected in the liver, and pravastatin, a high cholesterol medication, was detected in the blood and liver. Neither medication is noted to adversely affect pilot performance.

TESTS AND RESEARCH

An Adventure Pilot iFly was recovered from the wreckage. The iFly unit is an externally-powered, multi-function display and GPS receiver with a high resolution, LCD touchscreen display. The unit included a built-in navigational database and was optionally capable of receiving inflight ADS-B information, including weather radar, airport weather reports, weather forecasts, and traffic advisories. The navigational and information features included terrain warnings, airspace alerts, and display of en route visual flight rule and instrument flight rule (IFR) navigational information and IFR approach charts.

Download of the recovered iFly unit showed two log files that corresponded to the date of the accident flight. The most recent log, the accident flight, spanned from 19:16:21 to 19:53:53, which captured the accident flight from JXI to SLR. The second log file spanned from 16:42:46 to 17:26:59 and captured the previous flight from SLR to JXI. 

During the last minute of flight, the airplane's speed steadily decreased from 79 knots to the last recorded speed of 29 knots. The GPS altitude also steadily decreased from 832 ft to 425 ft. At 19:53:16 the airplane was at 649 ft GPS altitude, 74 kts, and about 35 degrees past and .43 miles from the approach end of runway 36 at JXL. At 19:53:27 the airplane was at 583 ft GPS altitude, 70 kts, and about 55 degrees past and .62 miles from the approach end of runway 36. 

Figure 1 shows the flight track the airplane followed, which is consistent with a left downwind and a left base leg for runway 36 at JXI, which had an airport elevation of 415 feet. The GPS track indicated the airplane began a turn for the left base when the airplane reached about 55 degrees past abeam the approach end of runway 36, as depicted in Figure 1.

Plot of recorded data points for the accident flight showing the accident location near JXI. ADDITIONAL INFORMATION

Title 14 Code of Federal Regulations 61.57 Recent flight experience: Pilot in command, states in part:

(b)Night takeoff and landing experience. 

(1) Except as provided in paragraph (e) of this section, no person may act as pilot in command of an aircraft carrying passengers during the period beginning 1 hour after sunset and ending 1 hour before sunrise, unless within the preceding 90 days that person has made at least three takeoffs and three landings to a full stop during the period beginning 1 hour after sunset and ending 1 hour before sunrise, and – 

(i) The person acted as the sole manipulator of the flight controls; and 

(ii) The required takeoffs and landings were performed in an aircraft of the same category, class, and type (if a type rating is required), and, if the aircraft to be flown is an airplane with a tailwheel, the takeoffs and landings must have been made to a full stop in an airplane with a tailwheel.

Advisory Circular 90-66A - Recommended Standards Traffic Patterns for Aeronautical Operations at Airports without Operating Control Towers, stated in part:

c. It is recommended that airplanes observe a 1,000-foot above ground level (AGL) traffic pattern altitude. Large and turbine-powered airplanes should enter the traffic pattern at an altitude of 1,500 feet AGL or 500 feet above the established pattern altitude. A pilot may vary the size of the traffic pattern depending on the aircraft's performance characteristics.

d. The traffic pattern altitude should be maintained until the aircraft is at least abeam the approach end of the landing runway on the downwind leg.

e. The base leg turn should commence when the aircraft is at a point approximately 45 degrees relative bearing from the runway threshold.

The Cessna 172N airplane flight manual, Section 3, Amplified Emergency Procedures, Engine Failure, contained a chart of maximum glide distance, which is shown in Figure 2. 


The Cessna 172N flight manual chart for maximum glide distance shows an approximate glide distance of 1 nautical mile at an altitude of 500 ft above ground level with a speed of 65 knots indicated airspeed, propeller windmilling, flaps up, and zero wind.

NTSB Identification: CEN16FA083 
14 CFR Part 91: General Aviation
Accident occurred Wednesday, January 13, 2016 in Gilmer, TX
Aircraft: CESSNA 172N, registration: N737EZ
Injuries: 1 Fatal, 1 Uninjured.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

On January 13, 2016, about 0105 central standard time, a Cessna 172N, N737EZ, was located in a wooded area about 0.5 nautical miles south/southwest of runway 36 at Fox Stephens Field - Gilmer Municipal Airport (JXI), Gilmer, Texas. The airplane was found by a Texas Department of Public Safety Officer during a search with the Gilmer Police Department for an airplane that was reported by a family member to be overdue. The private non-instrument rated pilot was fatally injured and a passenger sustained serious injuries. The airplane received substantial damage to the wings, fuselage, and empennage. The airplane was registered to and operated by the pilot under 14 Code of Federal Regulations Part 91 as a personal flight that was not operating on a flight plan nor receiving any air traffic control services. Night instrument meteorological conditions prevailed for the flight that departed from Sulphur Springs Municipal Airport, Sulphur Springs, Texas on January 12, 2016 about 1915 and was returning to JXI.





TYLER, TX (KLTV) -

An East Texas woman is sharing her story of survival.

Pamela Lucky survived a plane crash Tuesday in Upshur County that killed her husband and stranded her for hours. 

She invited our cameras into her hospital room to tell us about her husband and the reason she knew she had to survive. 

“I held his hand until they found us. Five hours it took them to find us and I never left his side. I held his hand. I talked to him the whole time because that was my baby. My baby," Lucky said.

Lucky said she still struggles to remember all of the details of the plane crash. But some moments she said she'll never forget.

"Every time I close my eyes I see a picture of him. Because this man loved me with everything he had," she said.

Lucky said she and her husband Samuel spent the day in Sulphur Springs with family. 

She said at least once a month they would take a trip in his Cessna 172 Skyhawk. 

They were just a quarter mile away from the Gilmer Municipal Airport runway before the crash. 

"We were making a loop around the airport and it happened so fast neither one of us had time to say anything. He didn't know what happened I didn't know what happened," Lucky said.

Lucky said she was able to get out her seatbelt, hopeful that she could call for help. 

"Is it going to kill me because I'm falling real far? But I didn't care I wanted to call 911 so I could find the phone and get help for him," Lucky said.

Lucky said  they would have been married for two years this Valentine’s Day.

"I was his sweetheart. And he wanted everybody to know that I was his sweetheart that's why we got married on Feb. 14," Lucky said.

While she's grateful to be among friends and family, she said that "If I could change places with him I would, because he was just that kind of man."

She believes her love for him and their family gave her the strength she needed to survive the unthinkable. 

"I really thought I was going to die out there, I really did. But I knew he didn't want me out there," Lucky said.

The cause of the plane crash has not been determined.

A preliminary report from the NTSB could be available as early as next week.


Story, video and photo gallery: http://www.kltv.com





UPSHUR COUNTY (KYTX) - One person is dead and another person was hospitalized after the plane they were on went down in Upshur County. 

DPS identified the pilot as 73-year-old Samuel Oliver Lucky of Gladewater. He was pronounced dead at the scene. His passenger, 57-year-old Pamela Rickman Lucky also of Gladewater was sent to ETMC in Tyler in ICU where her condition has been upgraded to fair.

According to DPS Troopers on the scene, Gilmer Police heard a woman screaming when they drove by the area. Pamela’s screams led them to the crash site around 1:30 a.m. It’s been determined Pamela had been sitting stuck in the plane for hours in the cold before she was found.

Troopers determined the plane went down around 7:45 p.m. Tuesday after it was overdue at Fox Stephens Airport Gilmer Airport.

The single-engine Cessna 172 went down in a field off of Hwy 271 near Eagle Road, just south of Gilmer, according to DPS officials. The plane is registered out of Gregg County, according to FAA records.

The FAA had notified Upshur County of a missing plane earlier Tuesday evening that had left the airport in Sulphur Springs en route to Gilmer that had not shown up.

The National Transportation Safety Board has also been notified of the crash and will lead the investigation.
 
In September 2013, Pilot Samuel Oliver received top honors when he was recognized by the FAA for exceeding safety standards.


Source:  http://www.cbs19.tv








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