Thursday, November 05, 2015

Bell 206B JetRanger, N22743, registered to and operated by Applebee Aviation: Accident occurred November 02, 2015 in Dallas, Polk County, Oregon

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entities:

Federal Aviation Administration / Flight Standards District Office; Hillsboro, Oregon
Rolls Royce; Indianapolis, Indiana
Bell Helicopter; Euless, Texas

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf


Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms


http://registry.faa.gov/N22743

Location: Dallas, OR
Accident Number: WPR16LA020
Date & Time: 11/02/2015, 1424 PST
Registration: N22743
Aircraft: BELL 206B
Aircraft Damage: Substantial
Defining Event: Loss of engine power (partial)
Injuries: 1 Minor
Flight Conducted Under: Part 133: Rotorcraft Ext. Load

Analysis

The commercial pilot of the helicopter reported that, after he released the external load of trees in the loading zone and about 50 ft above ground level, it seemed like the engine experienced a partial loss of power. The pilot stated that he heard an abnormal noise as the helicopter began to spin to the right, and the low rotor rpm warning light illuminated. The pilot jettisoned the external load line and rolled the throttle toward a closed position in order to counteract the yawing motion, with no response noted. The pilot then initiated an autorotation; during the landing sequence, the helicopter impacted a tree and came to rest upright in a nose-high position. The pilot further stated that, after the helicopter came to rest, he noted that the engine was at a "very slow idle" and he had to shut down the engine. Postaccident examination of the helicopter revealed no evidence of any preexisting mechanical anomalies that would have precluded normal operation. The engine was removed and installed in an engine test cell and ran throughout various power settings.

The airframe fuel filter was removed. The filter element was almost black. The fuel removed was dark, and debris was observed within the fuel filter bowl. The fuel sample from the filter housing was tested and found to be within Jet A specifications. The debris noted within the sample contained various metals, the source of which could not be determined. Given that fuel was found throughout the fuel system, it is unlikely that the debris in the filter resulted in a blockage and restriction of fuel flow; however, the reason for the partial loss of engine power could not be determined. 

Probable Cause and Findings

The National Transportation Safety Board determines the probable cause(s) of this accident to be:
A loss of engine power for reasons that could not be determined based on the available information. 

Findings

Not determined
Not determined - Unknown/Not determined (Cause)

Factual Information 

On November 2, 2015, about 1424 Pacific standard time, a Bell 206B, N22743, was substantially damaged during an autorotation landing following a partial loss of engine power near Dallas, Oregon. The helicopter was registered to and operated by Applebee Aviation under the provisions of 14 Code of Federal Regulations Part 133. The commercial pilot, sole occupant of the helicopter, sustained minor injuries. Visual meteorological conditions prevailed, and no flight plan was filed for the external load flight. The local flight originated from a staging area about 15 minutes prior to the accident.

The pilot reported that prior to the accident flight; the helicopter was refueled with 30 gallons of Jet-A fuel. The pilot departed from a staging area and began lifting Christmas trees from a field to a nearby loading zone. The pilot stated that after about 5 or 10 loads, he released a load of trees in the loading zone and shortly after, it seemed like the engine went to a reduced power setting at an altitude of about 50 feet above ground level. He further stated that he heard an abnormal noise originate from the helicopter as the helicopter began to spin to the right along with an illumination of a low rotor RPM light. The pilot jettisoned the external load line and rolled the throttle towards a closed position in order to counteract the yawing motion, with no response noted. The pilot initiated an autorotation and during the landing sequence, the helicopter impacted a tree. Subsequently, the helicopter came to rest upright in a nose high position. The pilot further stated that after the helicopter came to rest, he noted that the engine was at a "very slow idle" and he had to shut off the engine.

Postaccident examination of the helicopter by a Federal Aviation Administration inspector revealed that the tailboom forward of the tailrotor gearbox was twisted about 90o. The helicopter was recovered to a secure location for further examination.

On December 2, 2015, the recovered helicopter was examined at the facilities of AvTech Inc., Auburn, Washington, by the National Transportation Safety Board (NTSB) investigator-in-charge and representatives from Rolls Royce and Bell Helicopters. The examination revealed that the skids were removed to facilitate wreckage transport. Flight control continuity was established throughout the airframe to the main rotor head and aft to the tailrotor. An area of impact damage was observed just forward of the tailrotor gearbox. Continuity of the engine controls was established from the cockpit controls to the engine. The airframe fuel filter was removed. The filter element was dark, almost black in color. The fuel removed was dark in color (charcoal looking). Debris was observed within the fuel filter bowl. Samples of the debris and fuel were retained. Power was applied to the helicopter, and the fuel boost pumps were turned on. Fuel expelled out of the engine supply fuel lines. A sample was taken, and the fuel appeared to be fairly clear in color with no debris noted. Visual inspection of the fuel tanks revealed that about 10 to 20 gallons of fuel was present.

The engine was visually intact and all fuel and air lines appeared to be secure. N1 and N2 rotated freely and continuity was established throughout the engine to the gearbox. The engine fuel filter was removed from its housing, and a fuel sample was collected. The fuel was dark in color and contained an unknown sediment inside. The filter was dark in color. The fuel from the fuel nozzle supply line was captured and was found clear in color.

The engine was removed and subsequently shipped to Rolls Royce for further inspection. Fuel samples were retained and sent for subsequent testing.

On April 6, 2016, the engine was further examined at the facilities of Rolls Royce, Indianapolis, Indiana. The engine was placed on an engine stand, and visually examined. Compressed air was applied to the port where the PC Line connects to the compressor scroll. Air was found leaking from the PC line that connects to the fuel control unit. The engine was subsequently installed in an engine test cell and run for about 90 minutes throughout various power settings. During a governor droop test, when the load was removed from the engine to test the governor's ability to maintain RPM, N2 RPM increased to the limit for the test cell. Throughout the engine run, the engine produced rated power at cruise flight and takeoff power settings.

The power turbine governor and fuel control unit were removed and subsequently examined at the facilities of Honeywell, Inc., South Bend, Indiana, under the supervision of an NTSB investigator. The investigator reported that the bench tests of the power turbine governor revealed the unit was "sluggish" however, would not result in a loss of engine power. The fuel control unit was placed on a test bench and functioned normally.

The fuel sample from the fuel filter housing from the accident helicopter was submitted to a third-party laboratory for analysis. There was a small amount of unknown debris visible in the sample. Three tests, including Freezing Point; Flashpoint and Distillation were performed on the fuel sample. All tests were found to be within specification for Jet A fuel. The debris was retained and sent to the NTSB Materials Laboratory for further examination. The testing results for the debris found higher elemental levels of calcium (Ca), copper (Cu), iron (Fe), magnesium (Mg), nickel (Ni), potassium (K), silver (Ag) and zinc (Zn). The source of the debris could not be determined.

History of Flight

Maneuvering-low-alt flying
Loss of engine power (partial) (Defining event)

Autorotation
Collision with terr/obj (non-CFIT) 

Pilot Information

Certificate: Commercial
Age: 26, Male
Airplane Rating(s): None
Seat Occupied: Right
Other Aircraft Rating(s): Helicopter
Restraint Used: 3-point
Instrument Rating(s): None
Second Pilot Present: No
Instructor Rating(s): None
Toxicology Performed: No
Medical Certification: Class 2 With Waivers/Limitations
Last FAA Medical Exam: 10/29/2015
Occupational Pilot: Yes
Last Flight Review or Equivalent: 08/29/2015
Flight Time:  800 hours (Total, all aircraft), 600 hours (Total, this make and model), 750 hours (Pilot In Command, all aircraft), 78 hours (Last 90 days, all aircraft), 6 hours (Last 30 days, all aircraft), 3 hours (Last 24 hours, all aircraft)

Aircraft and Owner/Operator Information

Aircraft Manufacturer: BELL
Registration: N22743
Model/Series: 206B B
Aircraft Category: Helicopter
Year of Manufacture:
Amateur Built: No
Airworthiness Certificate:  Normal
Serial Number: 3624
Landing Gear Type: Skid;
Seats:
Date/Type of Last Inspection: 09/25/2015, 100 Hour
Certified Max Gross Wt.: 3201 lbs
Time Since Last Inspection: 55 Hours
Engines: 1 Turbo Shaft
Airframe Total Time: 18443.3 Hours as of last inspection
Engine Manufacturer: Rolls Royce
ELT: Installed, not activated
Engine Model/Series: 250-C20B
Registered Owner: APPLEBEE AVIATION INC
Rated Power: hp
Operator: APPLEBEE AVIATION INC
Operating Certificate(s) Held: Rotorcraft External Load (133) 

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light: Day
Observation Facility, Elevation: KMMV, 159 ft msl
Observation Time: 2228 UTC
Distance from Accident Site: 16 Nautical Miles
Direction from Accident Site: 45°
Lowest Cloud Condition:
Temperature/Dew Point: 14°C / 8°C
Lowest Ceiling: Broken / 6500 ft agl
Visibility:  4 Miles
Wind Speed/Gusts, Direction: 5 knots, 230°
Visibility (RVR):
Altimeter Setting: 29.93 inches Hg
Visibility (RVV):
Precipitation and Obscuration:  Light - Rain; No Obscuration; No Precipitation
Departure Point: Dallas, OR
Type of Flight Plan Filed: None
Destination: Dallas, OR
Type of Clearance: None
Departure Time: 1411 PST
Type of Airspace: Class G 

Wreckage and Impact Information

Crew Injuries: 1 Minor
Aircraft Damage: Substantial
Passenger Injuries: N/A
Aircraft Fire: None
Ground Injuries: N/A
Aircraft Explosion: None
Total Injuries: 1 Minor

Latitude, Longitude: 45.006944, -123.401944 (est)



NTSB Identification: WPR16LA020
14 CFR Part 133: Rotorcraft Ext. Load
Accident occurred Monday, November 02, 2015 in Dallas, OR
Aircraft: BELL 206B, registration: N22743
Injuries: 1 Minor.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On November 2, 2015, about 1424 Pacific standard time, a Bell 206B, N22743, was substantially damaged during an autorotation landing following a partial loss of engine power near Dallas, Oregon. The helicopter was registered to and operated by Applebee Aviation, Banks, Oregon, under the provisions of Title 14 Code of Federal Regulations Part 133. The commercial pilot, sole occupant of the helicopter, sustained minor injuries. Visual meteorological conditions prevailed and no flight plan was filed for the external load operations flight. The local flight originated from a staging area nearby the accident site about 15 minutes prior to the accident.

The pilot reported that prior to the accident flight the helicopter was refueled with 30 gallons of Jet-A fuel. The pilot departed from a staging area and began lifting Christmas trees from a field to a nearby loading zone. The pilot stated that after about 5 or 10 loads, he released a load of trees in the loading zone and shortly after, it seemed like the engine went to a reduced power setting at an altitude of about 50 feet above ground level. He further stated that he heard an abnormal noise originate from the helicopter as the helicopter began to spin to the right along with an illumination of a low rotor RPM light. The pilot jettisoned the external load line and rolled the throttle towards a closed position in order to counteract the yawing motion, with no response noted. The pilot initiated an autorotation and during the landing sequence, the helicopter impacted a tree. Subsequently, the helicopter came to rest upright in a nose high position. 

Postaccident examination of the helicopter by a Federal Aviation Administration inspector revealed that the tailboom forward of the tailrotor gearbox was twisted about 90-degrees. The helicopter was recovered to a secure location for further examination. The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entities: 
Federal Aviation Administration / Flight Standards District Office; Hillsboro, Oregon
Rolls Royce; Indianapolis, Indiana
Bell Helicopter; Euless, Texas 

Aviation Accident Factual Report - National Transportation Safety Board:  https://app.ntsb.gov/pdf

Registered Owner: Applebee Aviation


Operator:  Applebee Aviation

http://registry.faa.gov/N22743

NTSB Identification: WPR16LA020 
14 CFR Part 133: Rotorcraft Ext. Load
Accident occurred Monday, November 02, 2015 in Dallas, OR
Aircraft: BELL 206B, registration: N22743
Injuries: 1 Minor.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On November 2, 2015, about 1424 Pacific standard time, a Bell 206B, N22743, was substantially damaged during an autorotation landing following a partial loss of engine power near Dallas, Oregon. The helicopter was registered to and operated by Applebee Aviation under the provisions of 14 Code of Federal Regulations Part 133. The commercial pilot, sole occupant of the helicopter, sustained minor injuries. Visual meteorological conditions prevailed, and no flight plan was filed for the external load flight. The local flight originated from a staging area about 15 minutes prior to the accident.

The pilot reported that prior to the accident flight; the helicopter was refueled with 30 gallons of Jet-A fuel. The pilot departed from a staging area and began lifting Christmas trees from a field to a nearby loading zone. The pilot stated that after about 5 or 10 loads, he released a load of trees in the loading zone and shortly after, it seemed like the engine went to a reduced power setting at an altitude of about 50 feet above ground level. He further stated that he heard an abnormal noise originate from the helicopter as the helicopter began to spin to the right along with an illumination of a low rotor RPM light. The pilot jettisoned the external load line and rolled the throttle towards a closed position in order to counteract the yawing motion, with no response noted. The pilot initiated an autorotation and during the landing sequence, the helicopter impacted a tree. Subsequently, the helicopter came to rest upright in a nose high position. The pilot further stated that after the helicopter came to rest, he noted that the engine was at a "very slow idle" and he had to shut off the engine.

Postaccident examination of the helicopter by a Federal Aviation Administration inspector revealed that the tailboom forward of the tailrotor gearbox was twisted about 90o. The helicopter was recovered to a secure location for further examination. 

On December 2, 2015, the recovered helicopter was examined at the facilities of AvTech Inc., Auburn, Washington, by the National Transportation Safety Board (NTSB) investigator-in-charge and representatives from Rolls Royce and Bell Helicopters. The examination revealed that the skids were removed to facilitate wreckage transport. Flight control continuity was established throughout the airframe to the main rotor head and aft to the tailrotor. An area of impact damage was observed just forward of the tailrotor gearbox. Continuity of the engine controls was established from the cockpit controls to the engine. The airframe fuel filter was removed. The filter element was dark, almost black in color. The fuel removed was dark in color (charcoal looking). Debris was observed within the fuel filter bowl. Samples of the debris and fuel were retained. Power was applied to the helicopter, and the fuel boost pumps were turned on. Fuel expelled out of the engine supply fuel lines. A sample was taken, and the fuel appeared to be fairly clear in color with no debris noted. Visual inspection of the fuel tanks revealed that about 10 to 20 gallons of fuel was present.

The engine was visually intact and all fuel and air lines appeared to be secure. N1 and N2 rotated freely and continuity was established throughout the engine to the gearbox. The engine fuel filter was removed from its housing, and a fuel sample was collected. The fuel was dark in color and contained an unknown sediment inside. The filter was dark in color. The fuel from the fuel nozzle supply line was captured and was found clear in color. 

The engine was removed and subsequently shipped to Rolls Royce for further inspection. Fuel samples were retained and sent for subsequent testing.

On April 6, 2016, the engine was further examined at the facilities of Rolls Royce, Indianapolis, Indiana. The engine was placed on an engine stand, and visually examined. Compressed air was applied to the port where the PC Line connects to the compressor scroll. Air was found leaking from the PC line that connects to the fuel control unit. The engine was subsequently installed in an engine test cell and run for about 90 minutes throughout various power settings. During a governor droop test, when the load was removed from the engine to test the governor's ability to maintain RPM, N2 RPM increased to the limit for the test cell. Throughout the engine run, the engine produced rated power at cruise flight and takeoff power settings. 

The power turbine governor and fuel control unit were removed and subsequently examined at the facilities of Honeywell, Inc., South Bend, Indiana, under the supervision of an NTSB investigator. The investigator reported that the bench tests of the power turbine governor revealed the unit was "sluggish" however, would not result in a loss of engine power. The fuel control unit was placed on a test bench and functioned normally.


The fuel sample from the fuel filter housing from the accident helicopter was submitted to a third-party laboratory for analysis. There was a small amount of unknown debris visible in the sample. Three tests, including Freezing Point; Flashpoint and Distillation were performed on the fuel sample. All tests were found to be within specification for Jet A fuel. The debris was retained and sent to the NTSB Materials Laboratory for further examination. The testing results for the debris found higher elemental levels of calcium (Ca), copper (Cu), iron (Fe), magnesium (Mg), nickel (Ni), potassium (K), silver (Ag) and zinc (Zn). The source of the debris could not be determined.

NTSB Identification: WPR16LA020
14 CFR Part 133: Rotorcraft Ext. Load
Accident occurred Monday, November 02, 2015 in Dallas, OR
Aircraft: BELL 206B, registration: N22743
Injuries: 1 Minor.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On November 2, 2015, about 1424 Pacific standard time, a Bell 206B, N22743, was substantially damaged during an autorotation landing following a partial loss of engine power near Dallas, Oregon. The helicopter was registered to and operated by Applebee Aviation, Banks, Oregon, under the provisions of Title 14 Code of Federal Regulations Part 133. The commercial pilot, sole occupant of the helicopter, sustained minor injuries. Visual meteorological conditions prevailed and no flight plan was filed for the external load operations flight. The local flight originated from a staging area nearby the accident site about 15 minutes prior to the accident.

The pilot reported that prior to the accident flight the helicopter was refueled with 30 gallons of Jet-A fuel. The pilot departed from a staging area and began lifting Christmas trees from a field to a nearby loading zone. The pilot stated that after about 5 or 10 loads, he released a load of trees in the loading zone and shortly after, it seemed like the engine went to a reduced power setting at an altitude of about 50 feet above ground level. He further stated that he heard an abnormal noise originate from the helicopter as the helicopter began to spin to the right along with an illumination of a low rotor RPM light. The pilot jettisoned the external load line and rolled the throttle towards a closed position in order to counteract the yawing motion, with no response noted. The pilot initiated an autorotation and during the landing sequence, the helicopter impacted a tree. Subsequently, the helicopter came to rest upright in a nose high position. 

Postaccident examination of the helicopter by a Federal Aviation Administration inspector revealed that the tailboom forward of the tailrotor gearbox was twisted about 90-degrees. The helicopter was recovered to a secure location for further examination.



This photograph of a helicopter spraying herbicides is among hundreds whistleblower Darryl Ivy released after a month working for Applebee Aviation driving trucks and handling pesticides on Seneca Jones Timber Company sites. 

Buxton-based Applebee Aviation got more bad news Tuesday, Nov. 3, when the Oregon Department of Agriculture (ODA) revoked its commercial pesticide operator license and fined the company $160,000 after an investigation revealed it had continued aerial pesticide applications even after the license was suspended by ODA Sept. 25.

“Mr. Applebee has demonstrated that he will ignore or fail to comply with any or all pesticide application requirements if compliance would cost him money,” stated an official notice from ODA to Applebee.

The new civil penalty of $160,000 against the company is in addition to a civil penalty of $20,000 issued to company owner Michael Applebee, who is a licensed pesticide applicator. ODA is suspending both the company’s operator license and Michael Applebee’s applicator license for five years.

ODA initially suspended Applebee’s license Sept. 25, 2015, for performing aerial herbicide application activities in a faulty, careless or negligent manner. It also gave the company a $1,100 civil penalty at the same time.

But Applebee continued to conduct application activities after Sept. 25, despite the suspended license, prompting ODA to get a temporary restraining order from Washington County Circuit Court on Oct. 11, and to issue a $40,000 civil penalty and a one-year license suspension.

The latest ODA investigation revealed the company performed 16 separate pesticide applications on private, state and federal forest lands between Sept. 26 and Oct. 2, in violation of its suspended license.

Applications took place on private forest land in Douglas and Lane counties, on state forest land in Clatsop County and on Bureau of Land Management land in Lake County, according to the ODA’s notice to Applebee.

The applications on BLM land on Oct. 1 and 2 took place after Mike Applebee and Applebee Aviation’s operation manager Warren Howe asked for and were denied permission from the ODA to perform the operation.

“Mr. Applebee stated that the contract [with BLM] was worth three million dollars and that he felt pressure to complete the job despite the fact that the Applebee Aviation’s CPO [Commercial Pesticide Operator] license was suspended,” the ODA’s notice said.

Although company owner Michael Applebee did not conduct any of the applications, ODA has moved to suspend his applicator’s license and issue a $20,000 civil penalty because of his lead role in making the decision to conduct application with a suspended license.

“Issuing $180,000 in civil penalties and five-year license revocations against Applebee Aviation underscores how serious the Oregon Department of Agriculture considers the violations that have taken place,” says ODA Director Katy Coba.

“We take all violations of the state’s pesticide law seriously. The fact that this operator knowingly and willfully continued to conduct pesticide applications 16 times after receiving a suspended license shows contempt for state regulations and our department. We cannot and will not tolerate such disregard for the law by which all pesticide operators are expected to live by.”

ODA’s regulatory action is being appealed by Applebee Aviation, which has the right to contest it through an administrative hearing.

Applebee Aviation’s week began poorly with a with a helicopter crash in Polk County Monday, Nov. 2, during a tree harvesting operation. According to witnesses, the helicopter suffered engine failure. The pilot, identified as Blaine Hayes, was uninjured. He refused medical care and left the scene, according to the Polk County Sheriff’s Office.

“The employees from Applebee Aviation who were at the scene then loaded into two vehicles and left prior to deputies from Polk County Sheriff’s Office arriving on scene,” the release said.

“At this point it is unknown why employees of the aviation company left the scene of the accident so quickly after refusing medical assistance.”

The crash — the fifth in as many years involving Applebee Aviation aircraft — is under investigation by the Federal Aviation Administration and the National Transportation Safety Board.

Original article can be found here:   http://www.pamplinmedia.com

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