Monday, September 01, 2014

Team Tango Foxtrot 4, N729AR: Fatal accident occurred August 31, 2014 in Abilene, Texas

The National Transportation Safety Board traveled to the scene of this accident. 

Federal Aviation Administration Flight Standards District Office: FAA Lubbock FSDO-13

Aviation Accident Final Report  -   National Transportation Safety Board: http://app.ntsb.gov/pdf

Docket And Docket Items   -   National Transportation Safety Board:   http://dms.ntsb.gov/pubdms

Aviation Accident Data Summary -   National Transportation Safety Board: http://app.ntsb.gov/pdf

RICK W.  SCHAFER :   http://registry.faa.gov/N729AR 


NTSB Identification: CEN14FA468 
14 CFR Part 91: General Aviation
Accident occurred Sunday, August 31, 2014 in Abilene, TX
Probable Cause Approval Date: 10/24/2016
Aircraft: SCHAFER RICK W FOXTROT 4, registration: N729AR
Injuries: 2 Fatal, 1 Serious, 1 Minor.

NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

The airplane had departed to the south for a short local flight. When it was about 400 ft above ground level, the pilot declared an emergency and reported to the tower controller that he needed to return to the airport. Witnesses saw the southbound airplane in a steep left bank and then descend into the trees. Evidence at the scene showed that the airplane was moving to the north-northwest when it impacted trees and terrain in a slightly nose-down, right-wing-low attitude. The impact resulted in the complete separation of the wing from the fuselage, and the complete separation of the forward fuselage, engine and propeller. All three adult occupants were ejected or partially ejected. The fourth occupant, a child restrained by a 4-point child safety seat in a rear seating position, sustained minor injuries and was removed from the wreckage by emergency responders shortly after the crash. 

Both fuel tanks were breached, fuel spilled from the tanks, but there was no postimpact fire. The examination of the wreckage revealed no evidence of preimpact mechanical malfunctions or failures that would have precluded normal operation. The reason for the emergency reported by the pilot could not be determined. Flat, cultivated agricultural fields south of the accident location would have provided a more suitable emergency landing area rather than to attempt a steep turn to return to the airport.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot's decision to attempt a steep turn to return to the airport after reporting an emergency. The reason for the emergency could not be determined because postaccident examination of the airframe and engine did not reveal any mechanical anomalies that would have precluded normal operation.

HISTORY OF FLIGHT

On August 31, 2014, about 1834 central daylight time, a Schafer Foxtrot 4, experimental, amateur-built, single-engine airplane, N729AR, was destroyed after impacting terrain during initial climb near Abilene Regional Airport (ABI), Abilene, Texas. The pilot and one passenger were fatally injured, a second passenger was seriously injured, and a 2-year old child sustained minor injuries. The airplane was registered to and operated by the pilot. Day visual meteorological conditions (VMC) prevailed and a flight plan had not been filed for the 14 Code of Federal Regulations (C.F.R.) Part 91 personal flight. At the time of the accident the airplane was departing ABI for a local flight.

The airplane had departed ABI runway 17R to the south and was about 400 feet above ground level (agl) when the pilot declared an emergency and reported to the tower controller that he needed to return. Witnesses saw the southbound airplane in a steep left bank and several witnesses heard the sounds of impact. The airplane was generally northbound when it impacted mesquite trees and terrain about one mile south of the airport. The impact resulted in the complete separation from the fuselage of the forward fuselage, engine and propeller. The wing was also completely separated from the fuselage and both wing fuel tanks were compromised. All three adult occupants were ejected or partially ejected. The child in the rear seat remained restrained by a 4-point safety harness and was removed from the wreckage by emergency responders who arrived quickly. There was a fuel spill at the scene, but no postimpact fire.

PERSONNEL INFORMATION

The pilot, age 35, was a career active duty officer in the United States Air Force (USAF). He was rated as a Senior Pilot and was then assigned on active flight status as a military instructor pilot. He held a Federal Aviation Administration (FAA) commercial pilot certificate with a rating in airplane multiengine land limited to center thrust, a rating in instrument airplane, and a rating in airplane single engine land limited to private pilot privileges. The pilot also held a current FAA instructor pilot certificate with a rating in only instrument airplane.

Complete copies of the pilot's personal flight records were not available for examination by the NTSB during the course of the investigation. The investigator-in-charge was able to review six selected pages of the pilot's personal logbook, the aircraft logbook, the engine logbook, FAA and USAF documents and other records. The pilot's flight experience on August 31, 2014, was estimated as a total of 2,594 hours of flight experience in all airplanes, with an assumed total of more than 2,000 hours in military airplanes. The pilot's flight experience in a Foxtrot 4 airplane was estimated as a total of 23 hours, with all of that experience being within the previous three months.

AIRCRAFT INFORMATION

The low wing, fixed tricycle landing gear, single-engine airplane, serial number (s/n) F-008, was powered by a 300-horsepower Lycoming IO-540-K1H3 fuel injected engine, s/n L-22038-48, which drove a McCauley model B3D36C431-C, 3-blade aluminum alloy controllable pitch propeller, s/n 040071.

The airplane had a cantilever low-wing with conventional tail surfaces, and a four-seat enclosed cockpit which was accessed through "gull-wing" doors on both the left and right sides of the front cockpit seats. The aircraft structure was made mostly from composites with the fuselage halves molded as single pieces. The kit manufacturer's website described the airplane as having an expected empty weight of about 1,750 pounds, a maximum gross weight of 3,200 pounds, and an expected stall speed in the landing configuration of about 58 knots.

FAA records show the airplane was completed by the pilot, with assistance from the kit-builder, as a kit-built airplane. On June 10, 2014, it was issued an FAA special airworthiness certificate in the experimental category as an amateur built airplane with a requirement for the next annual condition inspection due on June 30, 2015.

Entries in the aircraft logbook showed that the first recorded flight in N729AR was by a Team Tango employee on June 11, 2014, at a beginning aircraft total time of 0.0 hours. Based on a review of entries in the aircraft logbook, the engine logbook, pilot logbook entries and other records, the IIC estimated the total flight times on August 31, 2014, as: aircraft total time 53.0 hours; engine total time 1,498.5 hours; and engine total time since major overhaul 362.5 hours.

Records show that N729AR flew from Golden Triangle Regional Airport (GTR), Columbus, Mississippi to San Marcos Municipal Airport (HYI), San Marcos, Texas, on August 29, 2014. Refueling records at HYI showed the airplane was refueled on that day with 65.80 gallons of 100LL aviation gasoline.

METEOROLOGICAL INFORMATION

At 1752 the Automated Surface Observation System at ABI reported wind from 150 degrees at 12 knots, visibility 10 miles, few clouds at 7,500 feet, temperature 36 degrees Celsius (C), dew point 17 degrees C, and an altimeter setting of 29.87 inches of mercury.

Data from the National Oceanic and Atmospheric Administration showed that, at the accident location, at 1834, the altitude of the sun was about 18 degrees above the horizon and the azimuth of the sun was about 269 degrees. Apparent sunset occurred at 2006.

COMMUNICATIONS AND RADAR

Following is a timeline of selected communications between the pilot of N729AR and FAA Air Traffic Control (ATC), including a summary of selected FAA ATC radar contacts.

1755 N729AR landed at ABI after a flight from HYI. All ATC services with the inbound flight appeared to be normal and N729AR taxied to Abilene Aero, the general aviation fixed base operator, located east of taxiway C2 and west of the control tower.

1827:33 N729AR requested taxi instructions from Abilene Aero, to runway 17R at taxiway C3 for an intersection takeoff. The controller instructed the pilot to taxi via taxiway C. The pilot correctly read back the instructions and advised he would be operating west of the airfield in the local area for about 15 minutes before returning to ABI.

1832:01 N729AR was at taxiway C3 and runway 17R and advised he was ready for departure.

1832:19 The controller cleared N729AR for takeoff; the pilot read back the takeoff clearance and repeated that he would be staying in the local before returning to ABI.

1833:03 Radar showed a primary target over the runway abeam taxiway C2.

1833:22 Radar showed the primary target was southbound.

1833:27 Radar showed the primary target was southbound.

1833:32 Radar began receiving the Mode 3 code of 0322 and showed N729AR was southbound at a transponder reported altitude of 2,100 feet mean sea level (msl).

1833:37 Radar showed N729AR was southbound at a transponder reported altitude of 2,100 feet msl.

1833:41 Radar showed N729AR was beginning a left turn at a transponder reported altitude of 2,200 feet msl.

1833:42 N729AR transmitted: "tower experimental seven two nine alpha romeo ah emergency landing one seven right opposite direction".

There were no further communications from N729AR.

1833:46 Radar showed N729AR was in a left turn at a transponder reported altitude of 2,100 feet msl.

1833:51 Radar showed N729AR was in a left turn at a transponder reported altitude of 2,000 feet msl.

Radar contact was then lost.

AIRPORT INFORMATION

The FAA Airport/ Facility Directory, South Central U. S., indicated that ABI was a towered airport with a field elevation of 1,790 feet msl. The longest runway was 17R/35L, which was a grooved asphalt runway 7,203 feet long by 150 feet wide. Runway 17R was oriented to 180 degrees true and 172 degrees magnetic. Records show that runway 17R had a 0.4 percent upslope gradient to the south. Other runways at ABI were also listed.

WRECKAGE AND IMPACT INFORMATION

The airplane impacted 15 to 20-foot-tall mesquite trees and terrain on flat ranch lands at an estimated terrain elevation of about 1,755 feet msl. The impact location was about 2,500 feet south from the departure end of runway 17R.

Evidence at the scene showed that the airplane was moving to the north-northwest when it impacted terrain in a slightly nose down attitude with the right wing low. The first impact was to an upper branch of a mesquite tree at about 11 feet agl. The next impact was a ground scar about 16 feet away at an estimated angle of about 35 degrees from the horizontal. An uprooted mesquite tree about 28 feet from the initial tree impact showed evidence of a nearly vertical slice in its trunk at an angle to the first tree impact estimated about 12 degrees from the horizontal. The separated propeller spinner was found nearby. Other ground scars, wreckage debris and numerous broken branches littered the area on a wreckage distribution path of about 330 degrees. Several trees were completely uprooted by the impact. The main wreckage came to rest about 140 feet from the initial tree impact. The completely separated forward part of the fuselage, including the attached engine and propeller, came to rest about 195 feet from the initial tree impact.

The instrument panel and forward cockpit, including both front cockpit seats, were completely separated from the main fuselage and fragmented parts littered the wreckage distribution path leading to the main wreckage. The entire wing was completely separated from the fuselage and came to rest inverted with the left wing tip oriented to the south. Both integral wing fuel tanks were completely breached. The main part of the fuselage came to rest upright on top of the separated wing. The tail surfaces and aft empennage remained attached to each other, but were completely separated from the fuselage behind the rear cabin bulkhead and came to rest about 45 feet southeast from the main wreckage. Parts of the engine cowling, other fragmented parts, and a noticeable amount of engine oil littered the paved road in the path leading to the separated engine.

The upper skin on both wings was completely separated and both fuel tank caps remained securely fastened. Each fuel port was marked "AV GAS 60 GAL 100LL".

Impact damage prevented an assessment of the position of the flaps.

All flight control surfaces, and all major components of the airplane were accounted for.

The USAF Air Force Rescue Coordination Center reported that they had not monitored any emergency locator transmitter (ELT) beacon signals in the area on the day of the accident. An ACK E-04 ELT installed in the airplane's tail was examined. The 406 MHz ELT was marked with a 15-digit hex number: 2DC86 A42C2 FFBFF and the manufacture date code was: "23 AUG 2013". Investigators opened the case to the ELT and observed that no batteries were installed.

Parts of the four foot tall barbed wire fence in the debris path on the south side of the east-west paved road were destroyed. The electric power lines, about 35 feet above the fence, were undamaged.

Emergency responders reported they did not see evidence of liquid fuel and did not smell fuel when they first arrived at the accident scene. The investigative team arrived on the following day and did not see evidence of liquid fuel and no evidence of a vegetation kill was evident. Other investigative team members returned to the scene on the third day following the accident and they then observed clear evidence of a significant fuel blight of vegetation which showed a fuel spray pattern on the leaves of the mesquite trees in the accident debris field.

While on-scene, the investigative team observed that many of the large areas of flat cultivated agricultural fields to the south appeared to be a more adequate emergency forced landing area than the wooded area of the accident location.

MEDICAL AND PATHOLOGICAL INFORMATION

An autopsy was performed on the pilot by the Tarrant County Office of the Chief Medical Examiner in Fort Worth, Texas.

Forensic toxicology was performed on specimens from the pilot by the FAA Civil Aerospace Medical Institute (CAMI), Oklahoma City, Oklahoma. The toxicology report stated that no carbon monoxide was detected in blood. Tests for cyanide were not performed. No ethanol was detected in vitreous. Diphenhydramine was detected in urine and femoral blood. No other listed drugs were detected. The amount of diphenhydramine detected was too low to quantify and thus is considered to have not been impairing.

The pilot's most recent FAA medical certificate was an unrestricted third class certificate issued on January 17, 2001. USAF investigators reported that the pilot's most recent military flight-check as an instructor pilot was completed on October 5, 2013. A USAF "Medical Recommendation for Flying or Special Operational Duty" (form AF IMT 1041) showed that the pilot completed a USAF flight physical exam on January 24, 2014, and was then medically cleared for military instructor pilot duties. Under the provisions of 49 C.F.R. 61.23 (b) (9), the pilot's current military medical clearance met the FAA's equivalent requirements for operations requiring an FAA third class medical certificate.

TESTS AND RESEARCH

The wreckage was moved to another location and examined.

Examination of the separated wing showed the right wing was almost unrecognizable and highly fragmented. The fuel tank in the right wing was completely impact breached. The only section of the right wing remaining was a largely broomstrawed spar cap and impact damaged and fragmented spar web. The right hand wing ribs, wing skins and flight controls were all of fiberglass construction and were broken, most of them being completely separated from the adjacent structural members. The right landing gear fitting was completely separated from the wing. The left side of the wing still retained the shape of a wing, with the exception that the leading edge was fragmented, the entire upper skin of the left wing was separated, and the integral fuel tank was breached. The bond quality of the left wing skin bond line exhibited process issues that resulted in decent adherence to spars and ribs, but poor adhesion resulted in a clean separation of the bond to the attaching wing skin surface. The adhesive was not consistently applied on the whole bond surface and in some areas the adhesive had a very thick bond line.

The flight control linkage and engine control linkage were examined. Severe impact damage prevented a confirmation of preimpact control continuity, however all of the control linkage separations examined appeared to be a result of impact damage.

The engine mount remained attached to the firewall and the separated section of forward fuselage and was partially collapsed just to the engine mount's point of contact with the firewall. The impact vector was primarily rearward with an upward component. The main cabin area of the fuselage was largely intact and consisted of the barrel section from a plane just behind the front spar and instrument panel back to the empennage break. This remaining fuselage cabin area was laterally flexible due to compromise of the aft cabin bulkhead. The forward fuselage from the firewall and below the windscreen to just aft of the front spar was fragmented and separated.

The two front seat lap belt anchorages were adhesively bonded to the interior structure. The front seats and the inboard lap belt attachments and shoulder harness reel attachments were impact separated. Most of the fuselage shell around the front seat occupants had disintegrated into small pieces. The forward lap belt anchor locations consisted of large hex head bolts placed adjacent to the airplane structure with the fastener head covered with a generous mound of structural filler. On top of this filler the assembly was then covered with what appeared to be two four inch diameter circular wet-layup plies of glass cloth. The lap belt attachments were not otherwise mechanically attached. The shoulder harness inertia reels for the front seat occupants were anchored to the floor of the airplane and were not attached to the ceiling or the upper side of the door jamb. Both inboard lap belt attachments and both shoulder harness inertial reel attachments for the front seat occupants were impact separated.

The right passenger seat in the rear cabin was separated from its attach points. The left passenger seat in the rear cabin remained attached. The individual inertia reels for the two rear seat occupants were mechanically bolted to the top of a platform common to the aft cabin bulkhead, and both remained attached. The rear seat lap belt attachments were mechanically bolted through the adjacent fuselage for the outboard belts, and were bolted through the control cable tunnel sidewall for the inboard lap belts. The inboard lap belt attachment for the right rear occupant was impact separated and had pulled completely through the composite sidewall. The other lap belt attachments for both rear seat occupants remained attached.

Impact damage prevented an assessment of the position of the fuel selector valve.The airframe fuel system, from the suction screens in the fuel tanks to the fuel line to the engine driven fuel pump in the engine compartment, was broken and completely separated in several different locations. Selected airframe fuel system components were removed from the wreckage and further examined.

The engine and propeller were examined.

The engine driven diaphragm fuel pump was impact damaged and could not be tested. The left magneto was secure on its mount, it was removed and examined. The right magneto was impact separated from the accessory case. Both magnetos were rotated using an electric drill and both furnished spark at all outlet points. The spark plugs were removed and examined. The plugs that were not impact damaged all showed undamaged electrodes with "normal" wear and exhibited a low service life with color consistent with normal combustion. The starter, generator, and vacuum pump were examined, but were not further tested. Oil was observed on the engine at the engine examination and there was no evidence of lubrication distress or heat distress. The engine fuel system, including fuel screens, flow divider, and injector nozzles were examined. The fuel suction screen was visually examined and observed clear of contaminants. The induction air box was impact destroyed.

The engine was rotated by hand from the propeller and thumb suction and compression was obtained on all cylinders. Valve train and crankshaft continuity was verified and the accessory gears were observed rotating. All cylinders were examined using a lighted bore scope with no defects noted.

The propeller governor was secure on its mount. The actuating cable was impact broken. The unit was removed and inspected. No defects were observed and the gasket screen was free of debris.

The propeller assembly remained attached to the engine driveshaft propeller flange. All three propeller blades remained attached to the propeller hub. One of the blades exhibited ripples along the span of the trailing edge. All three blades exhibited chordwise smearing on their faces, and some blades had leading edge gouges. The outboard tips of two propeller blades were bent slightly aft.

The examination of the wreckage revealed no evidence of preimpact mechanical malfunctions or failures that would have precluded normal operation.

Other Examinations:

Two Dynon SV-D1000 electronic displays were removed from the wreckage and were examined at the NTSB Vehicle Recorder Laboratory in Washington, D. C. Examination of the devices showed they were both severely impact damaged. The disk storage modules were removed from the devices and evaluated for a potential chip-level recovery of any recorded information. The memory chips from both units were found to exhibit exterior cracking which was visible under magnification and X-ray. The chips were removed and tested. Both chips were found to be damaged beyond recovery and no data could be extracted from either device.

Airframe fuel system components were removed from the wreckage and were examined under the direct supervision of an FAA Inspector at the manufacturing facilities of Weldon Pump in Oakwood Village, Ohio. The sealed box was opened in the presence of the FAA Inspector and the components including the fuel selector valve, Weldon C8100-E electric fuel boost pump, Racor fuel filter/water separator, Jegs inline fuel filter, firewall bulkhead fitting, and airframe fuel plumbing components were flow tested. The examination showed that the flow was adequate, the electric fuel boost pump was operational, and the entire fuel system did not show evidence of a preaccident anomaly that would have prevented normal operation.

ADDITIONAL INFORMATION

According to the FAA "Airplane Flying Handbook", FAA-H-8083-3A, Page 16-5, "… If an actual engine failure should occur immediately after takeoff and before a safe maneuvering altitude is attained, it is usually inadvisable to attempt to turn back to the field from where the takeoff was made. Instead, it is safer to immediately establish the proper glide attitude, and select a field directly ahead or slightly to either side of the takeoff path."

"The decision to continue straight ahead is often difficult to make unless the problems involved in attempting to turn back are seriously considered. In the first place, the takeoff was in all probability made into the wind. To get back to the takeoff field, a downwind turn must be made. This increases the groundspeed and rushes the pilot even more in the performance of procedures and in planning the landing approach. Secondly, the airplane will be losing considerable altitude during the turn and might still be in a bank when the ground is contacted, resulting in the airplane cartwheeling (which would be a catastrophe for the occupants, as well as the airplane). After turning downwind, the apparent increase in groundspeed could mislead the pilot into attempting to prematurely slow down the airplane and cause it to stall."

NTSB Identification: CEN14FA468 
14 CFR Part 91: General Aviation
Accident occurred Sunday, August 31, 2014 in Abilene, TX
Aircraft: SCHAFER RICK W FOXTROT 4, registration: N729AR
Injuries: 2 Fatal,1 Serious,1 Minor.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigativ
e work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

On August 31, 2014, about 1834 central daylight time, a Schafer Foxtrot 4, experimental, amateur-built, single-engine airplane, N729AR, was destroyed after impacting terrain during initial climb near Abilene Regional Airport (ABI), Abilene, Texas. The pilot and one passenger were fatally injured, a second passenger was seriously injured, and a 2-year old child sustained minor injuries. The airplane was registered to and operated by the pilot. Day visual meteorological conditions (VMC) prevailed at the time of the accident and a flight plan had not been filed for the 14 Code of Federal Regulations Part 91 personal flight. At the time of the accident the airplane was departing ABI for a local flight.

The airplane was taking off to the south and was about 200 feet above ground level when the pilot declared an emergency and reported to the tower controller that he needed to return. A witness saw the southbound airplane in a steep left bank and several witnesses heard the sounds of impact. The airplane was generally northbound when it impacted mesquite trees and terrain about one mile south of the airport. The impact resulted in the complete separation from the fuselage of the forward fuselage, engine and propeller. The wing was also completely separated from the fuselage and both wing fuel tanks were compromised. All three adult occupants were ejected or partially ejected. The child in the rear seat remained restrained by a 4-point safety harness and was removed from the wreckage by emergency responders who arrived quickly. There no postimpact fire.


Previous Incident:  August 01, 2014 in Oshkosh, Wisconsin 

AIRCRAFT EXPERIMENTAL TEAM TANGO FOXTROT 4, ON TAXI NOSE GEAR COLLAPSED, OSHKOSH, WI 

Federal Aviation Administration Flight Standards District Office:  FAA Milwaukee FSDO-13
 

 
Richard and Matthew Schafer died on Sunday evening when the small airplane they were flying in crashed in Abilene. 
Submitted photo


 Remember Matthew Taylor Schafer by donating to his spouse and 2 young sons 


Major Richard Schafer and wife Major Richard W. "Tracer" Schafer III, 49th Fighter Training Squadron Instructor Pilot, poses for a photo with his wife Ashley Schafer in the cockpit of a T-38C Talon. 




Update 11:52 a.m. (9/4/14):

Sunday plane crash victim Victoria Schafer was released from Hendrick Medical Center Wednesday night.

Above is a photo of her along with her two sons and her husband, Matthew, who was killed in the crash. Her 2-year-old son Wyatt Schafer was also in the crash and was released from the hospital Tuesday.

An account has been set up for the Schafer family at Abilene Teachers Federal Credit Union.

The branches are located at 3849 Antilley Road, 2801 N. 6th Street, 2555 Buffalo Gap Road, and 1181 E.N. 10th Street.

Update 9:54 a.m. (9/4/14):

Funeral services have been scheduled for 35-year-old United States Air Force Maj. Richard W. “Tracer” Schafer III and his brother 28-year-old Matthew Schafer.

The two were killed Sunday in a plane crash near Diamondback Golf Club on Sunday, August 31.

The services will be held at Hillcrest Church of Christ at 2 p.m. on Friday, September 5.

Update 10:08 a.m. (9/2/14):

2-year-old Wyatt Schafer has been released from Hendrick Medical Center after a plane crash on Sunday, August 31, near Diamondback Golf Club.

31-year-old Victoria Schafer, the second crash victim transported to Hendrick, remains there in fair condition.

Update 7:38 p.m. (9/1/14):

The National Transportation Safety Board has revealed new details on what happened in the moments just before Sunday's crash.

According to the NTSB, the pilot, 35-year-old Richard W. “Tracer” Schafer III, had flown to San Marcos, Texas from Mississippi before flying to Abilene to pick up his family members.

Shortly after taking off from Abilene Regional Airport to the south, someone from the aircraft reported an emergency to Abilene tower control, saying the plane needed to land.

The aircraft turned left and crashed about one mile south of the control tower.

NTSB will send electronic components from the plane to the NTSB headquarters in Washington, D.C. for examination.

The NTSB says its preliminary report is expected to be released next week.  The full report could take six months to one year to complete.

Update 4:47 p.m. (9/1/14):

More information has been released about the pilot in Sunday's fatal plane crash. The pilot was former Airman at Columbus Air Force Base in Mississippi. Columbus AFB gives more information in the release below:

COLUMBUS AIR FORCE BASE, Miss. – An instructor pilot assigned to Columbus Air Force Base died in a general aviation plane crash Sunday night at approximately 6:30 p.m. near Abilene Regional Airport, Texas.

The pilot, United States Air Force Maj. Richard W. “Tracer” Schafer III, 35, and his brother, were pronounced dead by local authorities. Two other passengers were transported to a local hospital.

Schafer was flying his private aircraft, licensed in Mississippi, while on vacation with his family in Texas. The cause of the crash is under investigation by the National Transportation Safety Board.

"This is a tragic event that affects not only Team BLAZE, but our community partners both here and in Abilene," reflects Col John Nichols, commander, 14th Flying Training Wing. "Our thoughts and prayers are with Maj Schafer's family as they cope with this painful tragedy."

Additional details will be provided as soon as they become available from the NTSB.

Update 9:00 a.m. (9/1/14):
The Abilene Fire Department released the following information regarding the plane crash that took place near Abilene Regional Airport:

At approximately 6:36 p.m. yesterday evening Abilene 911 dispatch received a call that a plane had crashed south of the Airport.  Abilene police, Airport fire, and Abilene fire responded to the scene (just off Industrial Blvd.)  A single engine experimental plane had crashed into the trees and brush just South of Industrial Blvd.  There were 4 passengers on board at the time of the crash.  Two of the passengers were immediately transported to Hendrick Medical Center, neither appeared to have life threatening injuries.  The pilot and his other passenger were deceased.

The FAA will be en route Monday morning to investigate the crash site.  In the meantime, Abilene Police have the scene secured.  At this time it is unknown as to what caused the accident.

The plane was registered to Rick W. Schafer (35) out of Columbus Mississippi.  He and his passenger, Matthew Schafer (28) from Abilene, died at the scene.  Their bodies will be taken to Tarrant County for a medical examination.  Victoria (31) and Wyatt (2) Schafer were transported to Hendrick Medical Center.  The investigation is ongoing at this time.

Update 8:30 p.m. (8/31/14):

Two people are dead following a small plane crash near the Abilene Regional Airport early Sunday evening, according to the Abilene Fire Department.

The victims were the pilot and his brother. A female passenger and a child on board the plane were injured and taken to Hendrick Medical Center.

Abilene police will be staying at the scene to guard the site. The Federal Aviation Administration will be conducting an investigation to determine the cause of the crash on Labor Day.

The names of the victims have yet to be released.

ORIGINAL STORY

Emergency units have been called to a scene of a small plane crash near Diamondback Golf Club, just west of the Abilene Regional Airport.

The crash happened shortly after 6:30 p.m. Sunday on a wooded area. Initial reports say four people were on board the plane when the crash occurred.

As of 7 p.m., two have been transported to the hospital. No word on their names and extent of injuries.

Our crews are currently on the scene gathering the latest information.


Matthew Taylor Schafer (left) and Richard W. “Tracer” Schafer III


Abilene police blocked off Industrial Boulevard Monday in anticipation of the National Transportation Safety Board arriving on the scene of a fatal small plane crash.




Published on July 9, 2014: N729AR First flight


4 comments:

  1. I just saw on another page that this same aircraft had an incident at Oshkosh a month before, where it's left main gear collapsed during taxi. Interesting!

    http://aviation-safety.net/wikibase/wiki.php?id=168253

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  2. Another Air Force pilot dies: Cirrus SR22, N401SC, fatal accident occurred January 25, 2017 near Municipal Airport (KSSF), San Antonio, Texas
    http://www.kathrynsreport.com/2017/01/fatal-accident-occurred-january-25-2017.html

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  3. It has now been a little over 5 years that this accident took the lives of these young men. I think about it every day, and wonder what really happened. It was not very well reported from the NTSB, in my opinion. The NTSB finally submitted their report two years after the accident. I made numerous calls to inquire about the status of the NTSB report, which is supposedly due within a year of an accident. If I am beginning to sound a bit bitter, it is because I am bitter.

    I offer the following comments that were known by the NTSB, but were not considered in assessing what happened. First, and most ignorant in my opinion, is the comment by the investigator who retired before I could talk to him, stating he could not determine why an emergency had been declared. However, witnesses on the golf course stated they heard the aircraft engine sputtering as it was departing the airport. They saw it turn (the always dangerous 180) before it went down behind the trees. I wonder what a fighter pilot is going to do with his brand new airplane, or any pilot for that matter. In this case the engine was trying to run, perhaps declaring an emergency and executing a downwind landing without causing danger to other aircraft was a reasonable decision. Secondly, parts they could not test because of extensive damage were not considered in the cause of the crash.

    I am very proud of these two young men, they were my sons. I know the plane did not tip-stall, because I visited the site the next day and saw the crash site. I trust our government, yet the evaluations of some of these bureaucrats continue to be so subjective and opinionated, instead of being backed up with cognitive data.

    ReplyDelete