Wednesday, July 12, 2017

Evolution Trikes REVO, N9912S: Fatal accident occurred July 09, 2016 at Cushing Field (0C8), Newark, Illinois and accident occurred May 24, 2014 near Williamsburg-Jamestown Airport (KJGG), Williamsburg, Virginia

Randy E. Atkinson 


The National Transportation Safety Board did not travel to the scene of this accident. 

Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; DuPage, Illinois

Aviation Accident Final Report - National Transportation Safety Board:http://app.ntsb.gov/pdf 


Investigation Docket - National Transportation Safety Board: http://dms.ntsb.gov/pubdms

Aviation Accident Data Summary - National Transportation Safety Board: http://app.ntsb.gov/pdf

http://registry.faa.gov/N9912S


NTSB Identification: CEN16LA263 
14 CFR Part 91: General Aviation
Accident occurred Saturday, July 09, 2016 in Newark, IL
Probable Cause Approval Date: 05/01/2017
Aircraft: EVOLUTION TRIKES REVO, registration: N9912S
Injuries: 1 Fatal.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

The student pilot was conducting his fourth solo flight in the weight-shift aircraft and was landing on a private turf runway in light wind conditions. A witness stated that the aircraft initially appeared to track straight down the runway after landing; however, shortly thereafter, it started to oscillate to the left and right. The oscillations increased until the aircraft rolled over and came to rest on its side. An examination of the aircraft did not reveal any preimpact malfunctions or anomalies that would have precluded normal operation. Although the pilot only had a total of 16.75 flight hours and less than 2 hours solo, it could not be determined why he lost control of the aircraft after landing.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The student pilot's failure to maintain directional control on landing. Contributing to the accident was the pilot's lack of flight experience.

HISTORY OF FLIGHT

On July 9, 2016, about 0915 central daylight time, an Evolution Trikes Revo, weight-shift aircraft, N9912S, impacted terrain at the Cushing Field Ltd Airport (0C8), Newark, Illinois. The student rated pilot, sole occupant, was fatally injured and the aircraft was substantially damaged. The aircraft was registered to and operated by a private individual, under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Day visual meteorological conditions prevailed at the time.

A witness who was in an airplane positioned in the traffic pattern observed the accident. The witness stated that the accident aircraft landed on runway 36. Initially, the aircraft appeared to track straight down the runway, when the aircraft started to oscillate left and right. The oscillations then increased until the aircraft rolled over. The pilot was taken to a local hospital and was initially listed in critical condition before he succumbed to his injuries.

The responding Federal Aviation Administration (FAA) inspector reported that the aircraft came to rest on its side. The aircraft sustained substantial damage to the wing and fuselage; the examination of the aircraft did not reveal any pre-impact malfunctions.

PILOT INFORMATION

The pilot held a student pilot certificate and was operating under the sport pilot medical rules. A review of the pilot's logbook revealed he had accumulated 16.75 total flight hours, with 1.75 solo, in the accident aircraft. The logbook revealed three solo flights before the accident flight.

AIRCRAFT INFORMATION

The accident aircraft was an Evolution Trikes Revo. The aircraft has a strut-braced hang glider-style high-wing, weight-shift controls, two-seats-in-tandem, tricycle landing gear, and a single-engine in the pusher configuration. The aircraft was powered by a reciprocating Rotax four cylinder 912ULS engine and a fixed pitch propeller. A review of the aircraft's maintenance records revealed the last condition inspection was completed on February 8, 2016 with an aircraft total time of 93.5 hours. A review of FAA records revealed the aircraft received its Special Airworthiness Certificate in the Special Light Sport – Weight Shift Control Aircraft category on February 7, 2011. The student pilot purchased the aircraft in March 2016; however, at the time of the accident, the aircraft registration had not been updated in the FAA's database.

METEOROLOGICAL INFORMATION

At 0915, the automated weather observation facility located at the Morris Municipal Airport – James R. Washburn Field (C09), about 10 miles southeast of the accident site recorded; wind calm, 10 mile visibility, broken clouds at 1,900 ft, temperature 71 degrees Fahrenheit (F), dew point 62 degrees F, and a barometric pressure of 30.02 inches of mercury.

AIRPORT INFORMATION
The Cushing Field Ltd Airport (0C8), is a privately owned airport, open to the public, located 2 miles southwest of Newark, Illinois. Pilots are to use the CTAF (Common Traffic Advisory Frequency) for communications. The airport has a single turf runway 18/36; 2,831 ft by 180 ft. The airport is at an elevation of 640 ft mean sea level.

WRECKAGE AND IMPACT INFORMATION

The wreckage came to rest on its right side, on the grass runway. Substantial damage was noted to the aircraft fiberglass fuselage/fairing. Several tubing members for the wing were either bent or broken during the collision with the ground. The fabric wing was also torn.

MEDICAL AND PATHOLOGICAL INFORMATION

The Office of the Coroner, DuPage County, Illinois conducted an autopsy on the pilot. The cause of death was determined to be "cervical spinal injuries".

The FAA Bio Aeronautical Sciences Research Laboratory, Oklahoma City, Oklahoma, conducted toxicological testing on the pilot. The specimens were not tested for cyanide. The test was negative for carbon monoxide and ethanol. The test was positive for Fentanyl in lung and blood.

Fentanyl is an opioid medication. Fentanyl is used as part of anesthesia to help prevent pain after surgery or other medical procedure. A review of medical records revealed that the fentanyl was administered during medical treatment, after the accident.

NTSB Identification: CEN16LA263
14 CFR Part 91: General Aviation
Accident occurred Saturday, July 09, 2016 in Newark, IL
Aircraft: EVOLUTION TRIKES REVO, registration: N9912S
Injuries: 1 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On July 9, 2016, about 1940 central daylight time, an Evolution Trikes Revo, weight-shift aircraft, N9912S, experienced a hard landing at the Cushing Field LTD Airport (0C8), Newark, Illinois. The student rated pilot, sole occupant, was seriously injured and the aircraft was substantially damaged. The aircraft was registered to and operated by a private individual, under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Day visual meteorological conditions prevailed at the time.

An initial report from the responding Federal Aviation Administration (FAA) inspector stated that student rated pilot had little flight experience, but was endorsed for solo flight. The aircraft landed hard and flipped over, coming to rest upside down.   The aircraft was retained for further examination.








NTSB Identification: ERA14CA262 
14 CFR Part 91: General Aviation
Accident occurred Saturday, May 24, 2014 in Williamsburg, VA
Probable Cause Approval Date: 07/30/2014
Aircraft: EVOLUTION TRIKES REVO, registration: N9912S
Injuries: 2 Minor.

NTSB investigators used data provided by various entities, including, but not limited to, the Federal Aviation Administration and/or the operator and did not travel in support of this investigation to prepare this aircraft accident report.

The pilot stated that he was flying the weight-shift control aircraft over a river while the passenger took photos. As he slowed and descended the aircraft near a bird's nest in order for the passenger to capture a photo, the aircraft entered an aerodynamic stall. The pilot applied full engine power to recover, but the aircraft continued to sink before impacting the river, resulting in substantial damage. The pilot and passenger subsequently egressed and swam to the shore. The pilot stated that there were no mechanical malfunctions or anomalies of the aircraft or engine that would have precluded normal operation of the airplane.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:

The pilot's failure to maintain airspeed while maneuvering at low altitude, which resulted in an aerodynamic stall and impact with water.

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