Saturday, September 19, 2015

Cessna 172E Skyhawk, N3647S: Fatal accident occurred September 19, 2015 in Gettysburg, Adams County, Pennsylvania

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:

Federal Aviation Administration / Flight Standards District Office; Harrisburg, Pennsylvania

Aviation Accident Final R
eport - National Transportation Safety Board: https://app.ntsb.gov/pdf


Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms


http://registry.faa.gov/N3647S

Location: Gettysburg, PA
Accident Number: ERA15LA363
Date & Time: 09/19/2015, 1043 EDT
Registration: N3647S
Aircraft: CESSNA 172E
Aircraft Damage: Substantial
Defining Event: Loss of engine power (total)
Injuries: 2 Serious
Flight Conducted Under: Part 91: General Aviation - Personal

Analysis 

The private pilot, who was also the airplane owner, was conducting a local personal flight. About 30 minutes after takeoff, during a descent from 3,000 to 1,500 ft mean sea level, the airplane experienced a total loss of engine power; the pilot then attempted a forced landing to a grass field. The airplane's approach speed was too fast for landing and the airplane overflew the selected field, eventually impacting trees at the edge of an adjacent field.

Subsequent examination of the airframe and engine revealed no evidence of any preimpact mechanical anomalies that would have precluded normal operation. Before the accident flight, the airplane had been stored for an extended period with automotive fuel in the tanks. Although long-term storage with automotive fuel can lead to varnish or gum deposits that may block or restrict fuel flow, the newly-replaced carburetor was found full of fuel with no foreign material or deposits present, and fuel was observed to flow freely from the fuel tanks to the carburetor during postaccident testing. The weather conditions at the time of the accident were conducive to the formation of serious carburetor icing at glide engine power settings when using aviation-grade gasoline. Given that the use of automotive gasoline is known to result in the formation of carburetor icing at higher ambient temperature and lower humidity conditions than aviation gasoline, it is likely that the loss of engine power was the result of carburetor icing. 

Probable Cause and Findings

The National Transportation Safety Board determines the probable cause(s) of this accident to be:

The total loss of engine power due to carburetor icing. Contributing to the accident was the pilot's failure to maintain a proper approach speed during the forced landing, which resulted in impact with trees.

Findings

Aircraft

Fuel - Fluid type

Personnel issues
Decision making/judgment - Pilot (Factor)

Environmental issues
Conducive to carburetor icing - Effect on equipment (Cause)

Factual Information 

On September 19, 2015, at 1043 eastern daylight time, a privately owned and operated Cessna 172E, N3647S, was substantially damaged during a forced landing to a soybean field after a total loss of engine power near Gettysburg, Pennsylvania. The private pilot and pilot-rated passenger received serious injuries. Visual meteorological conditions prevailed and no flight plan was filed for the local personal flight that departed from Waltz Field (34PA), Gettysburg, Pennsylvania about 1015. The airplane was being operated under the provisions of Title 14 Code of Federal Regulations Part 91.

The pilot-rated passenger stated that prior to departure, during the engine run-up, the engine ran "a little rough" when operated on one of the two magnetos. The pilot continued the run up until the engine operated smoothly on the left, right, and both magnetos. He recalled that the engine operated "remarkably smooth" for takeoff, climb and while performing various maneuvers. After descending from 3,000 feet to about 1,500 feet above mean sea level, the engine started to "shake, rumble, spit, and sputter and then just quit." The passenger further recalled that the pilot did not reduce engine power from its previous setting of around 2,400 rpm during the descent, nor did he apply carburetor heat. After the engine lost power, the pilot attempted to land in a nearby grass field, however the approach was too fast. He overflew the grass field, then touched down in an adjacent soybean field, the airplane bounced, veered left, and collided with the tree line at the edge of the field.

According to Federal Aviation Administration (FAA) records, the pilot held a private pilot certificate with ratings for airplane single-engine land and instrument airplane. His most recent FAA third-class medical certificate had expired, it was issued on December 29, 2010, at which time he reported a total of 2,096 hours of flight experience.

The four-seat, single-engine, high-wing airplane was manufactured in 1963, and was equipped with a Continental O-300D, 145-horsepower reciprocating engine. The maintenance logbooks were not recovered. FAA airworthiness records showed that the airplane had been modified to operate with automotive gasoline in accordance with a supplemental type certificate. According to a mechanic, an annual inspection of the airplane was completed in July 2013, after which the airplane had accrued about 1 hour of flight prior to the next annual inspection, which was completed by him on September 11, 2015. During the interval between the two inspections, automotive fuel remained in the fuel tanks. Maintenance documents provided by the mechanic revealed that the carburetor had been replaced, seals in the fuel selector valve and gascolator were replaced, the automotive fuel was drained and 15 gallons of 100 low-lead aviation fuel was added to the fuel tanks, just prior to the September 2015 annual inspection. Afterwards, the engine operated satisfactorily during ground tests. The accident flight was the first flight after the maintenance and inspection.

Examination of the airplane revealed that the left wing was partially separated from the fuselage, rotated about 45 degrees aft, and exhibited leading edge crush damage. The right wing remained attached, exhibited leading edge crush damage, and the right aileron was separated from the wing. The empennage was partially separated from the fuselage near the aft bulkhead of the cargo compartment. Flight control cable continuity was confirmed for pitch and yaw from the cockpit controls to the respective control surfaces, while the aileron control cables exhibited fractures in each wing consistent with tension overload.

The left fuel tank was breached, and about 2 gallons of fuel were drained from it during recovery operations. An unknown amount of fuel had leaked from the right wing after the accident. The gascolator and carburetor were full of a yellowish-amber fluid similar in color and odor as automotive fuel. The fuel inlet screen was unobstructed, and no water was present. Air pressure was applied to the gascolator outlet and fluid was observed flowing through the fractured fuel lines at the door pillars near the wing attach points. The carburetor needle valve and seat were clean with no debris found. When manually operated, fluid was observed exiting out of the carburetor accelerator pump. The carburetor main fuel nozzle was absent of debris. The fluid observed throughout the fuel system was yellowish-amber in color with an odor consistent with automotive fuel.

One of the propeller blades was bent aft at its tip. Neither blade exhibited a pattern of chordwise scratching or leading edge damage. The propeller was rotated by hand and thumb suction and compression was observed on all cylinders. Continuity of the crankshaft was confirmed to the rear accessory pad. The top spark plugs were removed and appeared grey to slightly black in color with normal wear when checked against the Champion Check-A-Plug chart. Both magnetos produced spark on all towers when rotated by hand. The air inlet box was clean and free of obstructions. The throttle, mixture, and carburetor heat controls were securely attached to the engine and moved freely. The oil quantity dipstick indicated 6 quarts.

A weather observation recorded at Fountain Dale Heliport (RYT), Fountain Dale, Pennsylvania, at 1053 included: temperature 23 degrees C (73 F), dew point 18 degrees C (64 F), and an altimeter setting of 29.95 inches of mercury.

According to an FAA Special Airworthiness Information Bulletin, these weather conditions are conducive to serious carburetor icing at glide power settings.
FAA Advisory Circular (AC) 91-33A, Use of Alternate Grades of Aviation for Grade 80/87, and Use of Automotive Gasoline, provided operational information regarding the use of automotive fuels in aircraft. According to the AC, "Long-term fuel storage of automotive gasoline in aircraft fuel tanks should be avoided. Although automotive gasolines have lower maximum existent gum specification requirements than aviation gasoline, either fuel can form undesirable gum deposits over long-term storage under particularly severe conditions, such as in barrels and at high temperature. Gum deposits thus formed could result in engine malfunctions." The AC further stated, "FAA Technical Center testing indicates that carburetor icing will occur in less time and at higher ambient temperatures with automotive gasoline than with aviation gasoline. Therefore, pilots using automotive gasoline should be familiar with the induction system icing prevention procedures of the FAA Advisory Circular AC 20-113 and be prepared to use these procedures at higher ambient temperatures and lower humidities than when using aviation gasolines." 

History of Flight

Maneuvering

Loss of engine power (total) (Defining event)

Landing
Off-field or emergency landing

Landing-flare/touchdown
Collision with terr/obj (non-CFIT) 

Pilot Information

Certificate: Private
Age: 85, Male
Airplane Rating(s): Single-engine Land
Seat Occupied: Left
Other Aircraft Rating(s): None
Restraint Used: Unknown
Instrument Rating(s): Airplane
Second Pilot Present: Yes
Instructor Rating(s): None
Toxicology Performed: No
Medical Certification: Class 3 With Waivers/Limitations
Last FAA Medical Exam: 12/29/2010
Occupational Pilot: No
Last Flight Review or Equivalent:
Flight Time: 2096 hours (Total, all aircraft) 

Pilot-Rated Passenger Information

Certificate:
Age: 64, Male
Airplane Rating(s): Single-engine Land
Seat Occupied: Right
Other Aircraft Rating(s):
Restraint Used: Lap Only
Instrument Rating(s): None
Second Pilot Present: Yes
Instructor Rating(s):
Toxicology Performed: No
Medical Certification: Class 2 With Waivers/Limitations
Last FAA Medical Exam: 04/27/2012
Occupational Pilot:
Last Flight Review or Equivalent:
Flight Time: 438 hours (Total, all aircraft) 

Aircraft and Owner/Operator Information

Aircraft Manufacturer: CESSNA
Registration: N3647S
Model/Series: 172E E
Aircraft Category: Airplane
Year of Manufacture: 1963
Amateur Built: No
Airworthiness Certificate: Normal
Serial Number: 17250847
Landing Gear Type: Tricycle
Seats: 4
Date/Type of Last Inspection: 09/11/2013, Annual
Certified Max Gross Wt.:
Time Since Last Inspection:  1 Hours
Engines: 1 Reciprocating
Airframe Total Time: 2181 Hours at time of accident
Engine Manufacturer: CONT MOTOR
ELT: C91  installed, not activated
Engine Model/Series: O-300-D6
Registered Owner: On file
Rated Power: 145 hp
Operator: On file
Operating Certificate(s) Held: None 

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light: Day
Observation Facility, Elevation: RYT, 902 ft msl
Observation Time: 1053 EDT
Distance from Accident Site: 9 Nautical Miles
Direction from Accident Site: 236°
Lowest Cloud Condition: Clear
Temperature/Dew Point: 23°C / 18°C
Lowest Ceiling: None
Visibility:  10 Miles
Wind Speed/Gusts, Direction: 5 knots, 10°
Visibility (RVR): 
Altimeter Setting: 29.95 inches Hg
Visibility (RVV): 
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: GETTYSBURG, PA (34PA)
Type of Flight Plan Filed: None
Destination: GETTYSBURG, PA (34PA)
Type of Clearance: None
Departure Time:
Type of Airspace:  Class G

Wreckage and Impact Information


Crew Injuries: 1 Serious
Aircraft Damage: Substantial
Passenger Injuries: 1 Serious
Aircraft Fire: None
Ground Injuries: N/A
Aircraft Explosion: None
Total Injuries: 2 Serious
Latitude, Longitude:  39.813056, -77.277222 (est)


Walter Miller Trostle, 85, passed away on October 27, 2015, at York Hospital in York, Pennsylvania.



NTSB Identification: ERA15LA363
14 CFR Part 91: General Aviation
Accident occurred Saturday, September 19, 2015 in Gettysburg, PA
Aircraft: CESSNA 172E, registration: N3647S
Injuries: 2 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On September 19, 2015, at 1043 eastern daylight time, a Cessna 172E, N3647S, was substantially damaged during a forced landing to a soybean field after a total loss of engine power near Gettysburg, Pennsylvania. The private pilot and pilot-rated passenger received serious injuries. Visual meteorological conditions prevailed and no flight plan was filed for the local personal flight that departed from Waltz Field (34PA), Gettysburg, Pennsylvania at an unknown time. The airplane was registered to and operated by a private individual under the provisions of Title 14 Code of Federal Regulations Part 91.

The pilot-rated passenger stated that prior to departure, during the engine run-up, the engine ran "a little rough" when operated on one of the two magnetos. The pilot continued the run up until the engine operated smoothly on the left, right, and both magnetos. He recalled that the engine operated "remarkably smooth" for takeoff, climb and while performing various maneuvers. After descending from 3,000 feet to about 1,500 feet above mean sea level, the engine started to "shake, rumble, spit, and sputter and then just quit." The pilot attempted to land in a nearby field and on touchdown the airplane bounced, veered left, and collided with the tree line at the edge of the field.

According to a mechanic, an annual inspection of the airplane was completed in July 2013, after which the airplane had accrued about 1 hour of flight prior to the next annual inspection which was completed on September 11, 2015. During the interval between the two inspections, automotive fuel remained in the fuel tanks. Maintenance records of the most recent annual inspection revealed that the carburetor and seals in both the fuel selector valve and the gascolator were replaced, fuel was drained from the fuel tanks, and the fuel tanks were refueled with 15 gallons of 100LL aviation fuel. The engine was then operated satisfactorily during ground tests.

The airplane came to rest upright in a tree line at the edge of a soybean field. The left wing was partially separated from the fuselage, rotated about 45 degrees aft, and exhibited leading edge crush damage. The right wing remained attached, exhibited leading edge crush damage, and the right aileron was separated from the wing. The empennage was partially separated from the fuselage near the aft bulkhead of the cargo compartment. Flight control continuity was confirmed from the cockpit controls to the respective control surfaces. The aileron cables exhibited fractures in each wing consistent with overload.

The left fuel tank was breached, and about 2 gallons of fuel were drained from it during recovery operations. An unknown amount of fuel had leaked from the right wing after the accident. The gascolator and carburetor were full of a yellowish-amber fluid similar in color and odor as automotive fuel. The fuel inlet screen was unobstructed, and no water was present. Air pressure was applied to the gascolator outlet and fluid was observed flowing through the fractured fuel lines at the door pillars near the wing attach points. The carburetor needle valve and seat were clean with no debris found. When manually operated, fluid was observed exiting out of the carburetor accelerator pump. The fluid observed throughout the fuel system was yellowish-amber in color with an odor consistent with automotive fuel.

The propeller was rotated by hand and thumb suction and compression was observed on all cylinders. Continuity of the crankshaft was confirmed from the propeller to the rear accessory pad. The top spark plugs were removed and appeared grey to slightly black in color with normal wear when checked against the Champion Check-A-Plug chart. Both magnetos produced spark on all towers when rotated by hand. The air inlet box was clean and free of obstructions. The throttle, mixture, and carburetor heat controls were securely attached to the engine and moved freely. The oil quantity dipstick indicated 6 quarts.

The engine was retained for further examination.

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; Harrisburg, Pennsylvania 

Aviation Accident Factual Report - National Transportation Safety Board:  https://app.ntsb.gov/pdf

Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

http://registry.faa.gov/N3647S

NTSB Identification: ERA15LA363
14 CFR Part 91: General Aviation
Accident occurred Saturday, September 19, 2015 in Gettysburg, PA
Aircraft: CESSNA 172E, registration: N3647S
Injuries: 2 Serious.

NTSB investigators may have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On September 19, 2015, at 1043 eastern daylight time, a privately owned and operated Cessna 172E, N3647S, was substantially damaged during a forced landing to a soybean field after a total loss of engine power near Gettysburg, Pennsylvania. The private pilot and pilot-rated passenger received serious injuries. Visual meteorological conditions prevailed and no flight plan was filed for the local personal flight that departed from Waltz Field (34PA), Gettysburg, Pennsylvania about 1015. The airplane was being operated under the provisions of Title 14 Code of Federal Regulations Part 91.

The pilot-rated passenger stated that prior to departure, during the engine run-up, the engine ran "a little rough" when operated on one of the two magnetos. The pilot continued the run up until the engine operated smoothly on the left, right, and both magnetos. He recalled that the engine operated "remarkably smooth" for takeoff, climb and while performing various maneuvers. After descending from 3,000 feet to about 1,500 feet above mean sea level, the engine started to "shake, rumble, spit, and sputter and then just quit." The passenger further recalled that the pilot did not reduce engine power from its previous setting of around 2,400 rpm during the descent, nor did he apply carburetor heat. After the engine lost power, the pilot attempted to land in a nearby grass field, however the approach was too fast. He overflew the grass field, then touched down in an adjacent soybean field, the airplane bounced, veered left, and collided with the tree line at the edge of the field.

According to Federal Aviation Administration (FAA) records, the pilot held a private pilot certificate with ratings for airplane single-engine land and instrument airplane. His most recent FAA third-class medical certificate had expired, it was issued on December 29, 2010, at which time he reported a total of 2,096 hours of flight experience.

The four-seat, single-engine, high-wing airplane was manufactured in 1963, and was equipped with a Continental O-300D, 145-horsepower reciprocating engine. The maintenance logbooks were not recovered. FAA airworthiness records showed that the airplane had been modified to operate with automotive gasoline in accordance with a supplemental type certificate. According to a mechanic, an annual inspection of the airplane was completed in July 2013, after which the airplane had accrued about 1 hour of flight prior to the next annual inspection, which was completed by him on September 11, 2015. During the interval between the two inspections, automotive fuel remained in the fuel tanks. Maintenance documents provided by the mechanic revealed that the carburetor had been replaced, seals in the fuel selector valve and gascolator were replaced, the automotive fuel was drained and 15 gallons of 100 low-lead aviation fuel was added to the fuel tanks, just prior to the September 2015 annual inspection. Afterwards, the engine operated satisfactorily during ground tests. The accident flight was the first flight after the maintenance and inspection.

Examination of the airplane revealed that the left wing was partially separated from the fuselage, rotated about 45 degrees aft, and exhibited leading edge crush damage. The right wing remained attached, exhibited leading edge crush damage, and the right aileron was separated from the wing. The empennage was partially separated from the fuselage near the aft bulkhead of the cargo compartment. Flight control cable continuity was confirmed for pitch and yaw from the cockpit controls to the respective control surfaces, while the aileron control cables exhibited fractures in each wing consistent with tension overload.

The left fuel tank was breached, and about 2 gallons of fuel were drained from it during recovery operations. An unknown amount of fuel had leaked from the right wing after the accident. The gascolator and carburetor were full of a yellowish-amber fluid similar in color and odor as automotive fuel. The fuel inlet screen was unobstructed, and no water was present. Air pressure was applied to the gascolator outlet and fluid was observed flowing through the fractured fuel lines at the door pillars near the wing attach points. The carburetor needle valve and seat were clean with no debris found. When manually operated, fluid was observed exiting out of the carburetor accelerator pump. The carburetor main fuel nozzle was absent of debris. The fluid observed throughout the fuel system was yellowish-amber in color with an odor consistent with automotive fuel.

One of the propeller blades was bent aft at its tip. Neither blade exhibited a pattern of chordwise scratching or leading edge damage. The propeller was rotated by hand and thumb suction and compression was observed on all cylinders. Continuity of the crankshaft was confirmed to the rear accessory pad. The top spark plugs were removed and appeared grey to slightly black in color with normal wear when checked against the Champion Check-A-Plug chart. Both magnetos produced spark on all towers when rotated by hand. The air inlet box was clean and free of obstructions. The throttle, mixture, and carburetor heat controls were securely attached to the engine and moved freely. The oil quantity dipstick indicated 6 quarts.

A weather observation recorded at Fountain Dale Heliport (RYT), Fountain Dale, Pennsylvania, at 1053 included: temperature 23 degrees C (73 F), dew point 18 degrees C (64 F), and an altimeter setting of 29.95 inches of mercury.

According to an FAA Special Airworthiness Information Bulletin, these weather conditions are conducive to serious carburetor icing at glide power settings.

FAA Advisory Circular (AC) 91-33A, Use of Alternate Grades of Aviation for Grade 80/87, and Use of Automotive Gasoline, provided operational information regarding the use of automotive fuels in aircraft. According to the AC, "Long-term fuel storage of automotive gasoline in aircraft fuel tanks should be avoided. Although automotive gasolines have lower maximum existent gum specification requirements than aviation gasoline, either fuel can form undesirable gum deposits over long-term storage under particularly severe conditions, such as in barrels and at high temperature. Gum deposits thus formed could result in engine malfunctions." The AC further stated, "FAA Technical Center testing indicates that carburetor icing will occur in less time and at higher ambient temperatures with automotive gasoline than with aviation gasoline. Therefore, pilots using automotive gasoline should be familiar with the induction system icing prevention procedures of the FAA Advisory Circular AC 20-113 and be prepared to use these procedures at higher ambient temperatures and lower humidities than when using aviation gasolines."

NTSB Identification: ERA15LA363
14 CFR Part 91: General Aviation
Accident occurred Saturday, September 19, 2015 in Gettysburg, PA
Aircraft: CESSNA 172E, registration: N3647S
Injuries: 2 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On September 19, 2015, at 1043 eastern daylight time, a Cessna 172E, N3647S, was substantially damaged during a forced landing to a soybean field after a total loss of engine power near Gettysburg, Pennsylvania. The private pilot and pilot-rated passenger received serious injuries. Visual meteorological conditions prevailed and no flight plan was filed for the local personal flight that departed from Waltz Field (34PA), Gettysburg, Pennsylvania at an unknown time. The airplane was registered to and operated by a private individual under the provisions of Title 14 Code of Federal Regulations Part 91.

The pilot-rated passenger stated that prior to departure, during the engine run-up, the engine ran "a little rough" when operated on one of the two magnetos. The pilot continued the run up until the engine operated smoothly on the left, right, and both magnetos. He recalled that the engine operated "remarkably smooth" for takeoff, climb and while performing various maneuvers. After descending from 3,000 feet to about 1,500 feet above mean sea level, the engine started to "shake, rumble, spit, and sputter and then just quit." The pilot attempted to land in a nearby field and on touchdown the airplane bounced, veered left, and collided with the tree line at the edge of the field.

According to a mechanic, an annual inspection of the airplane was completed in July 2013, after which the airplane had accrued about 1 hour of flight prior to the next annual inspection which was completed on September 11, 2015. During the interval between the two inspections, automotive fuel remained in the fuel tanks. Maintenance records of the most recent annual inspection revealed that the carburetor and seals in both the fuel selector valve and the gascolator were replaced, fuel was drained from the fuel tanks, and the fuel tanks were refueled with 15 gallons of 100LL aviation fuel. The engine was then operated satisfactorily during ground tests.

The airplane came to rest upright in a tree line at the edge of a soybean field. The left wing was partially separated from the fuselage, rotated about 45 degrees aft, and exhibited leading edge crush damage. The right wing remained attached, exhibited leading edge crush damage, and the right aileron was separated from the wing. The empennage was partially separated from the fuselage near the aft bulkhead of the cargo compartment. Flight control continuity was confirmed from the cockpit controls to the respective control surfaces. The aileron cables exhibited fractures in each wing consistent with overload.

The left fuel tank was breached, and about 2 gallons of fuel were drained from it during recovery operations. An unknown amount of fuel had leaked from the right wing after the accident. The gascolator and carburetor were full of a yellowish-amber fluid similar in color and odor as automotive fuel. The fuel inlet screen was unobstructed, and no water was present. Air pressure was applied to the gascolator outlet and fluid was observed flowing through the fractured fuel lines at the door pillars near the wing attach points. The carburetor needle valve and seat were clean with no debris found. When manually operated, fluid was observed exiting out of the carburetor accelerator pump. The fluid observed throughout the fuel system was yellowish-amber in color with an odor consistent with automotive fuel.

The propeller was rotated by hand and thumb suction and compression was observed on all cylinders. Continuity of the crankshaft was confirmed from the propeller to the rear accessory pad. The top spark plugs were removed and appeared grey to slightly black in color with normal wear when checked against the Champion Check-A-Plug chart. Both magnetos produced spark on all towers when rotated by hand. The air inlet box was clean and free of obstructions. The throttle, mixture, and carburetor heat controls were securely attached to the engine and moved freely. The oil quantity dipstick indicated 6 quarts.

The engine was retained for further examination.

FAA Flight Standards District Office: FAA Harrisburg FSDO-13

An 85-year-old man died October 27th from injuries sustained in a September plane crash in Cumberland Township, the York County Coroner's Office confirmed. 

Walter M. Trostle, of the 1000 block of Barlow Two Taverns Road, was the operator of a Cessna 172E Skyhawk plane when its engine lost power and it crashed in a field on Sept. 19 by Black Horse Tavern Road outside of Gettysburg.

A passenger in the plane survived the crash, the coroner confirmed.

Trostle's cause of death was multiple blunt force trauma. There will be no autopsy.

The Cumberland Township Police Department is investigating.



 




Two people were transported from the scene of a single-engine Cessna plane crash Saturday in Cumberland Township, outside Gettysburg, officials said. 

York Hospital spokesman Barry Sparks said that Walter Trostle, 85, was in serious condition at the hospital at 4 p.m. Saturday. Robert Beveridge, who runs Trostle's Antiques outside Gettysburg, said Walter Trostle is the store's landlord.

Federal Aviation Administration records indicate that the Cessna 172 plane that crashed is registered to Trostle.

The hospital did not provide any additional information about Trostle's condition. Members of Trostle's family who visited the scene of the crash Saturday afternoon declined to comment

Emergency units responded to the scene of the crash in a field by Black Horse Tavern Road just west of Gettysburg at 10:43 a.m.

Lynn Skopic lives in the 500 block of Black Horse Tavern Road, directly across the street from the soybean field where the plane crashed. She can see the plane from the front of the house.

"I heard the noise when it hit," she said. "It was just a funny bang. I was inside the house, but I knew something had happened. I went outside and saw two cars parked along the road but they didn't look like they had crashed. I went down to ask if everything was okay and that's when I saw the plane had hit the fence."

She said the woman who called 911 saw the crash, and told her that the plane appeared as if it was going to hit Skopic's house, but swerved to avoid it.

The FAA is investigating. Gary Martin of the FAA said it's not clear what caused the crash. He said the plane will be taken from the site and that the FAA will work with the National Transportation Safety Board to figure out what happened.

Emergency responders and investigating officials have not released information on the second person in the plane.Martin said his agency responded to the call for the plane crash, but said they don't know where the flight came from or who was on it.

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