Wednesday, July 22, 2020

Cessna 140A, N140AB: Accident occurred July 18, 2020 at Arlington Municipal Airport (KGKY), Tarrant County, Texas

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:

Federal Aviation Administration / Flight Standards District Office; Irving, Texas

Aviation Accident Preliminary Report - National Transportation Safety Board:

Location: Arlington, TX
Accident Number: CEN20LA291
Date & Time: 07/18/2020, 0745 CDT
Registration: N140AB
Aircraft: CESSNA 140
Injuries: 2 None
Flight Conducted Under: Part 91: General Aviation - Instructional

On July 18, 2020, about 0745 central daylight time, a Cessna 140 airplane, N140AB, was substantially damaged when it was involved in an accident near Arlington, Texas. The flight instructor and student pilot were uninjured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 instructional flight.

According to the flight instructor, the purpose of this flight was to fly the airplane cross-country for tire repairs, and at the same time, to train the student pilot on the airplane. The student pilot started the engine about 0715. The recorded weather indicated the temperature was 26° C and the dew point was 23° C. The flight instructor mentioned that since the outside air temperature was close to the dew point, they would have to be careful and cautious about carburetor icing, even if there was no visible moisture in the air.

The flight instructor related a previous occurrence when he flew this airplane for the first time with another instructor. The condition was almost 100% relative humidity and the carburetor heat was kept on about "10%" during the flight when at cruise power setting and full carburetor heat at lower than cruise power. However, a rough engine or any sign of carburetor ice was not encountered during that flight.

During the accident flight, the airplane's engine performed as expected during the run up. The student pilot set the carburetor heat on cold for takeoff and departed without issues. The flaps were retracted and the airplane was accelerated to best climb airspeed. The rate of climb was about 250 ft per minute and the engine was running at full power.

About 2 minutes into the flight, the engine started to run a "little bit rough and shaky." The instructor pulled the carburetor heat on about 10% hot and left it in this position in accordance with his training for this airplane. The engine roughness disappeared, and the airplane kept climbing at the same rate.

About 1 minute after this event, the roughness came back more severe this time. The instructor pulled the carburetor heat all the way on to full hot and waited. The roughness continued and the power available was not allowing the airplane to continue the climb at the same rate.

The airplane's pitch attitude was progressively lowered to maintain the airspeed and full power was not sufficient to keep the level flight attitude at 1,200 ft. There was no suitable area ahead for about the next 8 to 10 miles to perform an off-field emergency landing.

The instructor elected to turn back to the departure airport. He was not confident that the airplane could maintain altitude in the traffic pattern, so he elected to conduct a landing on a closer runway with a quartering tailwind. During the landing roll, as the airplane slowed down, he retracted the flaps to remove any residual lift and applied the yoke "slightly diving" away from the wind. While the airplane was still moving forward at a low ground speed, the nose "suddenly" yawed very "quickly and strongly" to the right. Application of the ailerons, elevators, and full left rudder and full left brake did not remedy the yaw. The airplane subsequently ground looped and came to rest in the grass.

Using the pilot's reported departure weather, the plotted relative humidity at this temperature and dewpoint spread was about 80%. Review of the icing probability chart contained in Federal Aviation Administration Special Airworthiness Information Bulletin CE-09-35 revealed that the weather conditions at the time of the accident were "conducive to serious icing at glide power."

The operator of the airplane was asked to run the engine after the accident. The engine started and operated "normally."

Aircraft and Owner/Operator Information

Aircraft Make: CESSNA
Registration: N140AB
Model/Series: 140 A
Aircraft Category:Airplane
Amateur Built: No
Operator: On file
Operating Certificate(s) Held: None

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light:Day
Observation Facility, Elevation: KGKY, 630 ft msl
Observation Time: 0653 CDT
Distance from Accident Site: 0 Nautical Miles
Temperature/Dew Point: 26°C / 23°C
Lowest Cloud Condition: Clear
Wind Speed/Gusts, Direction: 6 knots / , 150°
Lowest Ceiling: None
Visibility: 10 Miles
Altimeter Setting: 30.03 inches Hg
Type of Flight Plan Filed: None
Departure Point: Arlington, TX (GKY)
Destination: Fort Worth, TX (FWS)

Wreckage and Impact Information

Crew Injuries: 2 None
Aircraft Damage: Substantial
Passenger Injuries: N/A
Aircraft Fire: None
Ground Injuries: N/A
Aircraft Explosion:None
Total Injuries: 2 None
Latitude, Longitude: 32.663889, -97.094167 (est)

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