Sunday, March 02, 2014

Sonex, N732SX: Fatal accident occurred February 17, 2014 in Wellington, Florida

NTSB Identification: ERA14FA123 
14 CFR Part 91: General Aviation
Accident occurred Monday, February 17, 2014 in Wellington, FL
Probable Cause Approval Date: 12/09/2015
Aircraft: WILLIAMS CHRISTOPHER T SONEX, registration: N732SX
Injuries: 1 Fatal.

NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

The airplane had just departed the airport; one witness reported that during the initial climb the engine “sputtered,” and another reported that it “backfired.” The pilot then made a steep turn back toward the airport, but the airplane stalled and spiraled to the ground. The airplane was equipped with an electronic flight instrument system that recorded numerous engine and flight parameters. Review of the downloaded data revealed that, initially, the engine was operating normally and within design parameters. However, toward the end of the recorded data, the No. 1 cylinder head and exhaust gas temperatures had begun to decrease while the other cylinder temperature parameters remained fairly constant. The engine data then recorded a decrease in engine rpm followed by a steep 180-degree turn toward the airport. A witness who assisted the pilot with the airplane’s oil change 2 days earlier stated that the pilot had cross-threaded a spark plug in the No. 1 cylinder and attempted a helicoil repair. During examination after the accident, the No. 1 sparkplug was easily removed by hand. This was likely the cause of the power loss that preceded the pilot’s attempt to return to the airport. The pilot’s steep, 180-degree turn exceeded the airplane’s critical angle of attack, which resulted in a stall at low altitude and collision with terrain. A review of the pilot’s toxicology revealed that even though he tested positive for antidepressants, they were not a factor in the accident.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot's failure to maintain adequate airspeed following a partial loss of engine power during initial climb, which led to the airplane exceeding its critical angle of attack and experiencing an aerodynamic stall. Contributing to the accident was the pilot's improper repair of a stripped spark plug hole, which led to a partial loss of engine power during initial climb.

HISTORY OF FLIGHT

On February 17, 2014, about 1250 eastern standard time, an experimental, amateur-built Sonex, N732SX, collided with terrain shortly after departing the Wellington Aero Club (FD38), West Palm Beach, Florida. The airline transport pilot/owner was fatally injured, and the airplane was destroyed. Visual meteorological conditions prevailed, and no flight plan was filed for the personal flight conducted under the provisions of 14 Code of Federal Regulations Part 91. The flight was originating at the time of the accident.

Witnesses stated that during the initial climb, the engine "back- fired" and made a "sputtering" sound. The pilot entered a steep 180 degree turn back towards the airport. The airplane then stalled and entered a nose-down spiral, descended into a canal.

PERSONNEL INFORMATION

The pilot, age 58, held an airline transport pilot certificate for airplane multiengine land, airplane single-engine land, rotorcraft-helicopter, instrument helicopter, which was issued February 16, 2008, and a first-class airman medical certificate issued February 6, 2012, with no limitations. On the pilot's most recent application for a Federal Aviation Administration (FAA) medical certificate, he reported a total of 13,000 flight hours. The pilot's logbook was not recovered; therefore, his total flight experience could not be determined.

AIRCRAFT INFORMATION

The single engine airplane was manufactured in 2007, and was powered by an AeroVee series engine and equipped with a Sensenich model W54JV544G-AC9751, fixed-pitch propeller. The maintenance logbooks were not located; therefore, the maintenance history of the airplane could not be reconciled.

METEOROLOGICAL INFORMATION

At 1253, the recorded weather at Palm Beach International Airport (PBI), West Palm Beach, Florida, about 10 miles east of the accident site, included variable wind 6 knots, 10 statute miles visibility, few clouds at 4,300 feet above ground level. The temperature was 21 degrees Celsius (C), the dew point was 11 degrees C, and the altimeter setting was 30.19 inches of mercury.

WRECKAGE AND IMPACT INFORMATION

The wreckage was located partially submerged in a pond, about 200 yards from the departure end of runway 15. The airplane came to rest on a 109 degree magnetic heading, and was 3 feet from the pond's edge. The airplane was removed from the pond for examination, and all major components of the airplane were accounted for at the accident site.

The forward portion of the fuselage, firewall and cockpit were deformed and displaced aft. Both wings remained attached to the fuselage and were crushed along the leading edge aft. The vertical stabilizer, elevators and rudder remained attached to the empennage. Control continuity was traced from the cockpit control stick to the elevators and ailerons and from the rudder pedals to the rudder control horn. The examination of the flight control system components revealed no evidence of preimpact mechanical malfunction.

Examination of the engine revealed that it was separated from the firewall with sections of engine mount still attached and bent. The engine revealed impact damage on multiple areas on the external surface. Further examination revealed that the ignition lead wires were all attached to the respective sparkplugs and separated from the coil packs on the firewall. Examination of the wires revealed no breaks or chaffed sparkplug wires.

Examination of the sparkplugs revealed that the top spark plug on cylinder No. 1 was not seated in the cylinder head and finger tight within the cylinder head threads. The lower sparkplug was found seated to the cylinder and secure. The engine cylinders revealed that the top sparkplug, associated with cylinder No. 4, top sparkplug was seated and finger tight. All other sparkplugs were found seated within the cylinders and secure. All of the spark plugs were removed and the cylinders were checked for blockage. No blockage was noted and the crankshaft was rotated freely by hand. Engine valve train continuity and thumb compression was observed on all cylinders.

The throttle body revealed that it was still attached to the throttle cables, but broken away from the manifold. The throttle body lever actuated when the throttle control was manipulated. The air filter was found crushed and impact damaged. The fuel line was connected to the throttle body and was impact damaged and separated from the electric fuel pump attached to the firewall. Examination of the accessory plate revealed that it was impact damaged. The oil cooler was crushed and the oil flow input and output lines remained attached. The oil lines were broken away from the oil pump and oil was within the lines and the oil sump can.

The propeller remained attached to the propeller hub and the hub remained attached to the crankshaft. The wooden propeller revealed that one propeller blade was splintered, and the other propeller blade displayed span-wise cracks across the forward face.

MEDICAL AND PATHOLOGICAL INFORMATION

An autopsy was performed on the pilot on February 18, 2014, by Office of the District Medical Examiner, District 15 State of Florida, West Palm Beach, Florida.

Toxicological testing was performed on the pilot by the FAA Bioaeronautical Science Research Laboratory, Oklahoma City, Oklahoma.

Review of the toxicology report revealed, no carbon monoxide was detected in the cavity blood. No ethanol was detected in the vitreous. The following drugs were detected in the blood cavity; 0.091 (ug/ml, ug/g) Citalopram and 0.04 (ug/mL, ug/g) N-Desmethylcitalopram detected in blood cavity. Citalopram and Desmethylcitalopram is an antidepressant drug used to treat depression.

ADDITIONAL INFORMATION

According to a friend of the pilot, he assisted the pilot during an oil change two days prior to the accident. He stated that while conducting the oil change the pilot attempted to change the sparkplugs and cross-threaded the upper sparkplug on the No. 1 cylinder; and made an attempt to helicoil the cylinder thread. The friend further stated that he inspected the sparkplug and noted that the sparkplug along with the helicoil were able to be pulled out of the cylinder head. The pilot continued to work on the engine but the friend did not know if the pilot eventually repaired the cylinder head or if the pilot had flown the airplane after the repair, prior to the accident flight. During the examination of the engine a helicoil was not observed within the cylinder head threads of the No. 1 sparkplug.

The airplane was equipped with a Stratomaster Enigma electronic flight instrument system (EFIS) that is capable of recording primary flight data, GPS positions and engine monitor data. The device supports data recording to a secured digital (SD) card. The SD card was recovered and sent to the NTSB Vehicle Recorder Division for data recovery. Review of the data revealed that all engine parameters were normal during the initial climb. Further review revealed that the No. 1 cylinder head and exhaust gas temperature dropped approximately 100 degrees, followed by a loss in rpm and a loss in airspeed. GPS data then showed the airplane making a banking left turn as described by witnesses.


The Palm Beach Post has given the recent experimental aircraft accident an inordinate amount of coverage. However, it was never mentioned that veteran airline pilots crash experimental airplanes at an inordinate rate. The lay public has the misconception that a Boeing 777 pilot with 15,000-20,000 hours of total flight time will automatically be a good pilot in a small propeller-driven airplane. Jet pilots crashing small prop planes is not an anomaly.

I am a retired commercial pilot with 18,000 hours of flight time, including 11,000 as a Boeing 727 captain. I would be totally unsafe even attempting to taxi a Cessna 172. My experience as a veteran jet pilot transitioning to small propeller airplanes is documented in my book, “The Rogue Aviator” (therogueaviator.com), with an entire chapter dedicated to that theme. The title of that chapter is: “An Accident Looking for a Place to Happen — Jet Pilots in Prop Planes.” Very succinctly, in most regards, it is easier flying “the big jet” than the “puddle-jumper.” The crash rate of the little prop plane, particularly home-builts or experimentals, is off-the-scale unqualifiedly higher than the airline jet — even with an airline or ex-airline pilot at the controls.

ALLEN MORRIS

Delray Beach


Source:    http://www.palmbeachpost.com


http://registry.faa.gov/N732SX

NTSB Identification: ERA14FA123 
14 CFR Part 91: General Aviation
Accident occurred Monday, February 17, 2014 in Wellington, FL
Aircraft: WILLIAMS CHRISTOPHER T SONEX, registration: N732SX
Injuries: 1 Fatal.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

On February 17, 2014, about 1250 eastern standard time, an experimental, amateur built, Williams Sonex, N732SX, collided with terrain during an uncontrolled descent after departing the Wellington Aero Club (FD38), West Palm Beach, Florida. The airline transport pilot was fatally injured, and the airplane was destroyed. The airplane was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed, and no flight plan was filed. The flight was originating from FD38 at the time of the accident.

According to witnesses, as the airplane climbed after takeoff the engine backfired and began to sputter. The airplane made a steep 180 degree left turn, back towards the airport and went into a nose down attitude. The airplane began to spiral downward and collided with a pond. Witnesses attempted to assist the pilot and reported the downed airplane to the local 911 operator at 1255.

The wreckage was located partially submerged in a pond 3 feet deep, 200 yards from the departure end of runway 15. The airplane was on a 109 degree magnetic heading, and was 3 feet from the ponds edge. The airplane was removed from the pond for examination, and all major components of the airplane were accounted for at the accident site. Examination of the airplane revealed that the engine was separated from the firewall, impact damaged, and still attached to the engine mounts. The cockpit, fuselage, wings, and empennage were impact damaged. Flight control continuity from the cockpit controls to the flight control surfaces was confirmed. A cursory examination of the engine confirmed valve train continuity and compression on all cylinders.

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