Thursday, October 29, 2020

Dynamic Rollover: Aerospatiale AS 355F2 Ecureuil, N372CA; fatal accident occurred October 30, 2018 in Beekmantown, Clinton County, New York

Robert T. Hoban, Jr.
~

WHITE PLAINS, New York – A lawsuit seeks damages for the death of a South Jersey pilot who fell from a flaming helicopter after it a utility pole in October 2018.

Robert Hoban Jr. of Shamong, who had sought to hover his helicopter so a utility lineman could install equipment atop the pole, plunged about 75 feet after the aircraft struck the tower and flipped onto power lines, the lawsuit says.

The lineman also fell to his death, but two other passengers survived their falls during the accident in Beekmantown, New York, about 20 miles from Canada.

Hoban, 56, was not initially expected to fly the helicopter on a project for the New York Power Authority, according to information provided to the Federal Aviation Administration.

The project called for a helicopter to provide an aerial platform for utility workers who would rewire the towers.

But Hoban was called to the job after utility workers lost confidence in the original pilot’s ability to keep a helicopter steady in adverse wind conditions, according to an FAA interview with a lineman who survived his fall.

Hoban had 17,000 flight hours and experience with power line work, noted the lineman, Bernard McAllister.

The South Jersey man also worked as aviation manager for a Camden-based insurance firm, Conner, Strong & Buckelew, that has a helipad atop its Waterfront office building.

On the day of the accident, Hoban said wind conditions would allow the helicopter to hover for only about 30 seconds during training flights, McAllister told an FAA accident investigator.

But the helicopter “started to sway” after a few seconds and the right skid hit the pole three times, McAllister said.

“On the third hit, the helicopter rolled over onto the power lines,” according to McAllister's account.

Hoban reacted to the accident by helping the helicopter's passengers, the lawsuit says.

It says he "freed McAllister, whose helmet was stuck, and instructed him to jump." Hoban also released a lineman, Jeremy Kearns, from a harness hooked to the burning aircraft.

Kearns, who had been working outside the helicopter, did not survive his fall.

The lawsuit was filed in New York Supreme Court on behalf of Hoban’s estate. The pilot was the father of two daughters and a step-daughter, noted Fredric S. Eisenberg, a Philadelphia attorney for the pilot's family.

The suit accuses the New York Power Authority of negligence and recklessness, among other allegations. It also seeks damages from two New York firms that served as contractors on the project, Northline Utilities and Northline Ventures.

Representatives of the defendants could not be reached for comment.


Robert T. Hoban 

Jeremy P. Kearns

 






The National Transportation Safety Board traveled to the scene of this accident. 

Additional Participating Entities:
Federal Aviation Administration / Flight Standards District Office; Albany, New York
Airbus; Grand Prairie, Texas
Rolls Royce; Indianapolis, Indiana

https://registry.faa.gov/N372CA 

Location: Beekmantown, New York
Accident Number: ERA19FA035
Date & Time: October 30, 2018, 16:11 Local 
Registration: N372CA
Aircraft: Aerospatiale AS 355F2
Aircraft Damage: Destroyed
Defining Event: Dynamic rollover 
Injuries: 2 Fatal, 2 Serious
Flight Conducted Under: Part 133: Rotorcraft ext. load

Analysis

The pilot, pilot-rated passenger, and two linemen were conducting a flight to temporarily install a block (a large pulley used for fiber-optic wire) on a utility pole that was part of a set of high-tension powerlines. The pilot was seated in the front right seat, and one of the linemen was seated outside of the helicopter on a bench that was externally attached to the right side of the landing gear. The pilot-rated passenger, who was observing the flight for training purposes, was seated in the front left seat, and the other lineman was seated in the aft left seat. The power lines were aligned northwest/southeast, which required the pilot to approach the utility pole on a southeasterly heading so that the pole would be to the right of the pilot and lineman. For the lineman to install the block on the utility pole, the pilot had to hover the helicopter next to the pole. The wind conditions about the time of the accident were such that the helicopter would have encountered a tailwind. The pilot-rated passenger, the lineman seated in the aft left seat, and witnesses on the ground all stated that, while the helicopter was hovering next to the utility pole, the helicopter's right skid struck the pole a few times. The helicopter rolled over, became entangled in energized power lines, and caught fire. All four of the occupants survived the impact with the power lines and jumped to the ground to escape the burning wreckage. The pilot and the lineman seated on the bench did not survive the fall.

A postimpact fire consumed most of the helicopter while it was entangled in the power lines, and sections of the helicopter dropped from the power lines as it burned. Examination of the wreckage and both engines revealed no preimpact mechanical deficiencies that would have precluded normal operation.

The surviving lineman stated that he had flown with the pilot earlier that day and that the pilot had difficulty keeping the helicopter steady due to the strong wind, so the lineman temporarily installed a block before the helicopter returned to the base. Before the accident flight, the pilots, linemen, their foreman, the owner and a representative of the helicopter company and representatives of the linemen's employer held a safety meeting and agreed that, although the wind was too strong to fully install a block, the wind was "okay" to temporarily install another block. Given that the pilot had difficulty holding the helicopter steady while hovering with a tailwind on the previous flight the pilot most likely also had difficulty hovering the helicopter with the tailwind that was present about the time of the accident. The helicopter's subsequent impact with the utility pole resulted in a dynamic rollover into the power lines.

Probable Cause and Findings

The National Transportation Safety Board determines the probable cause(s) of this accident to be:

The pilot's failure to keep the helicopter clear of a utility pole while hovering with a tailwind, which resulted in a dynamic rollover into active power lines.

Findings

Personnel issues Aircraft control - Pilot

Environmental issues Tailwind - Response/compensation

Environmental issues Tailwind - Effect on operation

Environmental issues Pole - Response/compensation

Factual Information

History of Flight

Maneuvering-hover Collision with terr/obj (non-CFIT)

Maneuvering-hover Dynamic rollover (Defining event)

Maneuvering-hover Loss of control in flight

Uncontrolled descent Collision with terr/obj (non-CFIT)

On October 30, 2018, about 1611 eastern daylight time, an Aerospatiale AS355F2, N372CA, was destroyed when it collided with a wooden utility pole and power lines while conducting power line construction operations near Beekmantown, New York. The airline transport pilot and a lineman were fatally injured, and the pilot-rated passenger and another lineman sustained serious injuries. The helicopter was registered to and operated by Catalyst Aviation, LLC, and was being operated as a Title 14 Code of Federal Regulations Part 133 external load operation. Visual meteorological conditions prevailed at the time of the accident, and no flight plan was filed for the local flight that departed from a designated landing zone near Plattsburgh, New York, at 1602.

The power lines the crew was working on were supported by two 75-ft-tall wooden utility poles connected by a wooden horizontal bar and two wooden cross bars. The horizontal bar was installed about 6.5 ft below the top of the two poles. The power lines were oriented northwest/southeast.

The helicopter was equipped with a bench (platform) that was attached externally on the right side of the right landing gear. A lineman would sit on the bench while performing his duties. The pilot, who was seated in the front right seat, would position the helicopter on the left side of the utility pole so that the lineman would be able to accomplish work.

The two helicopter occupants who survived the accident, the pilot-rated passenger and one of the lineman, as well as two witnesses on the ground, provided their accounts of the circumstances surrounding the accident to the National Transportation Safety Board (NTSB) and the New York State Police. The pilot-rated passenger, who was seated in the front left seat, was observing the flight for
training purposes. He stated that the pilot was the only one operating the controls at the time of the accident. The pilot-rated passenger recalled that the helicopter approached the utility pole and got caught in the power lines; the helicopter struck the utility pole twice and rolled inverted. The pilot-rated passenger stated that his next memory was that he was upside down, the helicopter was on fire, and he had to unbuckle his harness and jump to the ground.

According to the lineman who was seated in the aft left seat, he had flown earlier that day with the pilot to install a block (a large pulley used for fiber-optic wire) on one of the utility poles. During that flight, as the helicopter approached the pole, the pilot had a hard time keeping the helicopter steady because the "..wind was too strong," so all we did was temporarily place the pulley on the wire" and then returned to the base. During the flight, the lineman sent a text message to his foreman that stated, "[the pilot] is very good. He just has horrible tailwind on the side we actually need to be on." He said that after they landed, two more flights were conducted with different linemen taking turns practicing out on the bench. Once these flights were completed, all the lineman, their foreman, the pilot, pilot rated passenger, and "everyone" from the operator [owner of Catalyst and her husband, a helicopter test pilot, who was assisting in overseeing the operation] held a "tailboard" meeting. He said, "This was a meeting for everyone to discuss the previous flights, review the upcoming flights including a safety briefing. During this meeting, the pilot said it was too windy to fully install a block, which would require him to hover about 5-7 minutes. However, the conditions were okay to just temporarily hang the block, which would take about 30 seconds. The entire team agreed that this would be what they would do. The lineman said they departed with the pilot-rated passenger seated in the front left seat, the pilot in the front right seat, the other lineman was on the bench, and he was seated in the aft left seat. The lineman said he could see everything that occurred during the flight. 

He said that, as the helicopter approached the utility pole, the other lineman on the bench was getting ready to install the block. The helicopter hovered for about 5 seconds so that the lineman could place the block on the line, and then the helicopter skid hit the pole three times. The surviving lineman indicated that the helicopter hit the pole "real hard" the third time and that the helicopter then rolled upside down into the wires and caught fire. The lineman exited the burning helicopter by jumping to the ground.

The linemen's foreman said that at the meeting prior to the accident flight he gave a sheet of all the block sizes to the husband of the owner of the helicopter company, who performed a weight and balance calculation. Once it was determined how many blocks could be taken on the accident flight, the pilot, pilot-rated passenger, and both linemen departed with the purpose to temporarily install the block. The foreman took a picture of the helicopter as it departed (time stamped at 1602) and then drove to the work site to observe the operation. The foreman said he arrived just as the helicopter was making its 45°approach to the power line structure.

As the helicopter got into place, the helicopter's right skid was almost even with the top of the pole. The foreman said the lineman on the bench connected the static line, opened the gate for the block, and placed the block on the power line. As the lineman was trying to close the gate of the block, the helicopter's right skid struck the pole. The helicopter pulled away and then struck the pole harder a second time. The helicopter then struck the pole a third time and immediately rolled over to the right, and the main rotor blades struck the adjacent static line and top of the other pole. The body of the helicopter became entangled in the energized (115 KVA) power lines and caught fire.

The husband of the owner of the helicopter company also witnessed the accident. He stated that the helicopter made a slow approach to the left side of the pole on a southeasterly heading (about 120°) and that the engines were operating normally. As the helicopter got into place near the pole, the lineman on the bench began to install the block. The helicopter then slid to the left and slid back to the right. The witness thought the helicopter's right skid had struck the pole because the helicopter immediately rolled over to the right. The main rotor blades then struck the top of the utility pole, and the helicopter became entangled in the power lines and caught fire. This witness saw all four helicopter occupants jump from the burning wreckage. He was not sure why the helicopter struck the pole and said it may have been the wind or just an overcorrection by the pilot.

Pilot Information

Certificate: Airline transport; Flight instructor 
Age: 56,Male
Airplane Rating(s): Single-engine land
Seat Occupied: Right
Other Aircraft Rating(s): Helicopter 
Restraint Used: 4-point
Instrument Rating(s): Airplane; Helicopter 
Second Pilot Present: Yes
Instructor Rating(s): Airplane single-engine; Helicopter; Instrument helicopter
Toxicology Performed: Yes
Medical Certification: Class 1 With waivers/limitations 
Last FAA Medical Exam: August 22, 2018
Occupational Pilot: Yes 
Last Flight Review or Equivalent: October 16, 2018
Flight Time: 16500 hours (Total, all aircraft)

Pilot-rated passenger Information

Certificate: Commercial 
Age: 34,Male
Airplane Rating(s): None 
Seat Occupied: Left
Other Aircraft Rating(s): Helicopter 
Restraint Used: 4-point
Instrument Rating(s): Helicopter 
Second Pilot Present: Yes
Instructor Rating(s): Helicopter; Instrument helicopter 
Toxicology Performed: No
Medical Certification: Class 2 Without waivers/limitations
Last FAA Medical Exam: January 19, 2018
Occupational Pilot: Yes 
Last Flight Review or Equivalent: January 6, 2018
Flight Time: 2000 hours (Total, all aircraft), 300 hours (Total, this make and model), 1940 hours (Pilot In Command, all aircraft), 34 hours (Last 90 days, all aircraft), 5 hours (Last 30 days, all aircraft), 0 hours (Last 24 hours, all aircraft)

The pilot, who was also the Director of Operations for the operator's Part 135 certificate, held an airline transport pilot certificate with ratings for airplane single-engine land, instrument airplane, rotorcraft helicopter, and rotorcraft-helicopter instrument. A review of the pilot's Federal Aviation Administration (FAA) airman records, revealed that his most recent first-class medical certificate was issued on August 22, 2018. At that time, he reported a total of 16,500 total flight hours. The operator reported that his last flight review occurred on October 16, 2018 in the same make/model helicopter as the accident
helicopter.

The pilot-rated passenger held a commercial pilot certificate with ratings for rotorcraft-helicopter and rotorcraft-helicopter instrument. His most recent FAA second-class medical certificate was issued on January 19, 2018, with no limitations. The operator reported that he had 2,000 hours of total flight experience, of which 300 hours were in the same make and model as the accident helicopter.

Aircraft and Owner/Operator Information

Aircraft Make: Aerospatiale 
Registration: N372CA
Model/Series: AS 355F2 F1 
Aircraft Category: Helicopter
Year of Manufacture: 1981 
Amateur Built: No
Airworthiness Certificate: Restricted (Special) 
Serial Number: 5028
Landing Gear Type: Skid 
Seats: 6
Date/Type of Last Inspection: October 28, 2018 100 hour 
Certified Max Gross Wt.: 5600 lbs
Time Since Last Inspection: 1 Hrs Engines: 2 Turbo shaft
Airframe Total Time: 9905.1 Hrs at time of
accident
Engine Manufacturer: Allison
ELT: C126 installed, not activated 
Engine Model/Series: 250-C20F
Registered Owner:
Rated Power: 420 Horsepower
Operator: 
Operating Certificate(s) Held: Rotorcraft external load (133), Commuter air carrier (135)

The Aerospatiale AS355 was a twin-engine light-utility helicopter equipped with two Rolls-Royce 250-C20F engines. The last 100-hour inspection was completed on October 28, 2018, with a total airframe time of 9,904.3 hours. The left engine had a total time of 11,611.4 hours and 1,640.9 hours since overhaul. The right engine had a total time of 8,114.9 hours and 1,684.2 hours since overhaul.
According to the operator, the helicopter had flown less than 1 hour between the time of the inspection and the time of the accident.

Meteorological Information and Flight Plan 

Conditions at Accident Site: Visual (VMC) 
Condition of Light: Day
Observation Facility, Elevation: PBG,234 ft msl
Distance from Accident Site: 6 Nautical Miles
Observation Time: 15:53 Local 
Direction from Accident Site: 160°
Lowest Cloud Condition: Visibility 10 miles
Lowest Ceiling: Overcast / 3100 ft AGL
Visibility (RVR):
Wind Speed/Gusts: 7 knots / 
Turbulence Type Forecast/Actual: None / None
Wind Direction: 290°
Turbulence Severity Forecast/Actual: N/A / N/A
Altimeter Setting: 30.02 inches Hg 
Temperature/Dew Point: 4°C / -2°C
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: Plattsburgh, NY (None) Type of Flight Plan Filed: None
Destination: Beekmantown, NY 
Type of Clearance: None
Departure Time: 16:02 Local 
Type of Airspace: Unknown

Plattsburgh International Airport, Plattsburgh, New York, which was about 6 miles southeast of the accident site, was the nearest weather reporting station. At 1553, the reported weather was wind from 290° at 7 knots, visibility 10 miles, overcast ceiling at 3,100 ft, temperature 4°C, dew point -2°C, and an altimeter setting of 30.06 inches of mercury.

Wreckage and Impact Information

Crew Injuries: 1 Fatal 
Aircraft Damage: Destroyed
Passenger Injuries:1 Fatal, 2 Serious 
Aircraft Fire: Both in-flight and on-ground
Ground Injuries: N/A 
Aircraft Explosion:Both in-flight and on-ground
Total Injuries: 2 Fatal, 2 Serious Latitude, Longitude: 44.744167,-73.439163(est)

A postimpact fire consumed most of the helicopter after it became entangled in the energized power lines, and sections of the helicopter dropped from the power lines as it burned. Found below the power lines were a portion of the cockpit, including the pilot and copilot seats; the main rotor system and all three main rotor blades; the combiner gearbox, which remained attached to the main transmission gearbox; the tailboom; and both engines.

The pilot and copilot seats were extensively fire damaged, and the aft seating area had been consumed by fire. The pilot's cyclic hand grip was mostly consumed by fire, and the electrical wires were exposed. Collective movement on both the pilot and copilot sides was consistent with corresponding movement with the partially severed control tube below the cabin floor. The left aft sliding doors and the forward windscreen exhibited fire damage.

Examination of the main rotor system revealed that the red and blue pitch change links remained attached to the pitch change horn and rotating swashplate. The yellow blade detached from the rotating swashplate and pitch change horn. A section of the blue blade had separated about three-quarters out from the blade root. The red blade exhibited full-length integrity with separation of the outer skin surface. The yellow blade was separated about five-eighths out from the blade root. The starflex arm sheared from all three rotor blades. The scissor link and collective collar remained attached to the rotating swashplate. All rotor blades were attached to the upper and lower sleeves via their respective attachment bolts. 

The main transmission and the combiner gearbox had separated from the airframe and appeared to be undamaged. The bilateral suspension remained attached, and the left-side combiner gearbox input had sheared. The other end of the sheared section remained attached to the No.1 engine. Two hydraulic reservoirs were found crushed and without fluid, but fluid was observed at the base of the transmission. The hydraulic pumps were attached to the combiner gearbox, and the hydraulic actuators remained attached to the stationary swashplate.

The tailboom separated from the main body of the helicopter and exhibited impact and fire damage. Examination of the tail rotor revealed that both blades were attached to their respective pitch change links, rotor drive shaft, and 90° gearbox. One blade was embedded about 2 inches into the ground, and the other blade appeared undamaged. The vertical fin remained attached and exhibited impact damage. The right horizontal stabilizer was partially embedded in the ground and exhibited impact damage. No fluid was observed in the sight gauge. The magnetic plug was removed and was absent of debris/obstructions. The top portion of the tail rotor drive shaft cover exhibited scuff marks about 4 ft from the aft handling bars.

The helicopter's landing gear remained caught in the power lines and was later removed by the New York Power Authority. The landing gear exhibited fire damage, but the forward and rear airframe mounting sleeves were intact.

Examination of the No. 1 engine revealed that the entire engine bay had been consumed by the postcrash fire, which also melted sections of the auxiliary gearbox and several other smaller components. The engine combustor showed significant impact damage. The power turbine governor was heat damage and was contaminated with melted aluminum. The fuel control unit was intact, but the control arm could not be manually manipulated. The bleed valve was manually operated, and the valve poppet moved smoothly along its normal stroke with no lateral play.

The compressor was heat damaged, and the composite liner had melted and left ashen debris throughout the compressor. No evidence of significant foreign object debris (FOD) was observed on the compressor blades, but the blade tips exhibited some minor bending. Neither the N1 nor the N2 rotor system could be manually rotated.

The No. 2 engine was partially buried in mud and was covered by the burned fuselage debris. The engine was damaged by the postcrash fire. The power turbine governor was partially consumed by fire, and the fuel control unit was impact and fire damaged. The bleed valve was mostly consumed by fire and was liberated from the compressor module. The compressor was heat damaged, and the composite liner had melted and left ashen debris throughout the compressor. The compressor exhibited extensive FOD damage and rotational scoring. Neither the N1 nor the N2 rotor system could be manually rotated. For the turbine module of each engine, visual examination of the fourth stage (power turbine) revealed no evidence of FOD, operational damage, or thermal degradation. Each engine's fuel spray nozzle was removed to permit a borescope examination of the first stage (gas generator turbine). The examination revealed no evidence of FOD or thermal degradation of the first stage nozzle or turbine blades. A small amount of fuel was found in each fuel spray nozzle, which was absent of debris and water. On the No. 2 engine turbine module, shiny metal splatter adhered to the turbine nozzle shield, which was consistent with FOD damage to the compressor (specifically, debris that was melted and deposited within the turbine module). The spray face of the fuel spray nozzle was intact and covered with soot. 

Examination of both turbine engines revealed no mechanical deficiencies that would have precluded normal operation at the time of the accident.

Additional Information

The FAA Helicopter Flying Handbook, FAA-H-8083-21B, states the following on pages 11-11 and -12:

A helicopter is susceptible to a lateral rolling tendency, called dynamic rollover…. For dynamic rollover to occur, some factor must cause the helicopter to roll or pivot around a skid or landing gear wheel until its critical rollover angle is reached…. Then, beyond this point, main rotor thrust continues the roll and recovery is impossible…. If the critical rollover angle is exceeded, the helicopter rolls on its side regardless of the cyclic corrections made. Dynamic rollover begins when the helicopter starts to pivot laterally around its skid or wheel…. This can occur for a variety of reasons, including the failure to remove a tie-down or skid securing device, or if the skid or wheel contacts a fixed object while hovering sideward, or if the gear is stuck in ice, soft
asphalt, or mud…. Once started, dynamic rollover cannot be stopped by application of opposite cyclic control alone.

Medical and Pathological Information

An autopsy of the pilot was conducted by the Champlain Valley Physician Hospital Department of Pathology, Plattsburgh, New York. The pilot's cause of death was determined to be multiple organ trauma due to a fall.

Toxicological testing performed at the FAA Forensic Sciences Laboratory was negative for carbon monoxide, ethanol, and all tested drugs.



Tuesday, October 27, 2020

Lancair 235, N25NL: Fatal accident occurred October 24, 2020 in Cordes Lakes, Yavapai County, Arizona


This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. 

The National Transportation Safety Board traveled to the scene of this accident.

Additional Participating Entity: 
Federal Aviation Administration / Flight Standards District Office; Scottsdale, Arizona


Location: Cordes Lakes, AZ
Accident Number: WPR21FA025
Date & Time: October 24, 2020, 10:28 Local
Registration: N25NL
Aircraft: Lancair 235
Injuries: 2 Fatal
Flight Conducted Under:

On October 24, 2020, about 1028 mountain standard time, a Lancair 235, N25NL, was substantially damaged when it was involved in an accident near Cordes Lakes, Arizona. The pilot and passenger were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

Friends of the pilot reported that he had departed Deer Valley Airport (DVT), Phoenix, Arizona, on October 24, with an intended destination of Page, Arizona. On the morning of October 26, 2020, Flight Service was notified by concerned friends that the pilot had not returned to DVT on October 25. The Federal Aviation Administration (FAA) issued an Alert Notice (ALNOT) shortly after. The wreckage of the airplane was located by a law enforcement air unit the morning of October 26. There are no known witnesses to the accident sequence.

Preliminary radar data provided by the FAA showed that the airplane had departed DVT at 1002, turned to a northerly heading and ascended to an altitude of about 7,600 ft mean sea level (msl). The data showed that at 1028:08, a slight right turn was initiated along with the start of a descent from 7,600 ft. (See figure 1). At 1028:18, the data showed the airplane at 7,300 ft msl, before a left turn was initiated. At 10:28:23, the data showed the airplane at 7,400 ft, where a right descending turn was initiated. The last recorded target was at 10:38:38, about 925 ft southwest of the accident site at an altitude of 6,200 ft. 

Examination of the accident site revealed that the airplane impacted mountainous terrain about 4.5 miles east of Cordes Lakes. All major structural components of the airplane were located within 15 ft of the main wreckage. The wreckage was recovered to a secure location for further examination.

Aircraft and Owner/Operator Information

Aircraft Make: Lancair
Registration: N25NL
Model/Series: 235
Aircraft Category: Airplane
Amateur Built: Yes
Operator:
Operating Certificate(s) Held: None
Operator Designator Code:

Meteorological Information and Flight Plan

Conditions at Accident Site: VMC 
Condition of Light: Day
Observation Facility, Elevation: KPRC,5052 ft msl 
Observation Time: 10:53 Local
Distance from Accident Site: 29 Nautical Miles
Temperature/Dew Point: 21°C /3°C
Lowest Cloud Condition: Clear
Wind Speed/Gusts, Direction: 9 knots / , 150°
Lowest Ceiling: 
Visibility: 10 miles
Altimeter Setting: 30.11 inches Hg 
Type of Flight Plan Filed: None
Departure Point: Phoenix, AZ (DVT)
Destination: Page, AZ (PGA)

Wreckage and Impact Information

Crew Injuries: 1 Fatal 
Aircraft Damage: Substantial
Passenger Injuries: 1 Fatal 
Aircraft Fire: None
Ground Injuries:
Aircraft Explosion: None
Total Injuries: 2 Fatal 
Latitude, Longitude: 34.298231,-112.01611

Those who may have information that might be relevant to the National Transportation Safety Board investigation may contact them by email eyewitnessreport@ntsb.gov, and any friends and family who want to contact investigators about the accident should email assistance@ntsb.gov.

William Engel Bell, 34, and his 8-year-old daughter, Amira Caballero, died in a Lancair 235 plane crash in Cottonwood, Yavapai County, Arizona




Marcellus, New York — Bill Bell always knew he wanted to become a pilot.

His buddies from Marcellus High School joked that he could fly a plane before he could drive a car. Over the years, Bell traveled the world, often flying some rich and famous folks along the way, his friends said. But he never forgot where he came from, they said.

William Engel Bell, 34, planned to take his 8-year-old daughter, Amira Caballero, camping in Page, Arizona, on October 24th, when the small plane Bell was piloting crashed, according to the Yavapai County Sheriff’s Office.

Bell, a 2004 Marcellus High School graduate, had flown out of Deer Valley Airport, a public airport 17 miles north of Phoenix, in Maricopa County, Arizona. He and his young daughter were reported missing October 25th after they did not return home to Peoria, Arizona.

At about 12:15 p.m. October 26th, an Arizona Department of Public Safety’s Ranger helicopter spotted Bell’s Lancair 235 aircraft in a remote area near Cordes Lakes, about 65 miles north of Phoenix, according to the Yavapai County Sheriff’s Office.

The plane had crashed, and was upside down on its wings. Both Bell and his young daughter were dead, the sheriff’s office said. The National Transportation Safety Board is investigating the crash.

“He was doing what he loved with the person he loved (when he died),” Bell’s friend Jon Thurston said this week.

Thurston and Bell’s other friends said he always took every safety precaution. They had flown with him in the past and had had conversations about safety as recent as when retired Los Angeles Lakers basketball superstar Kobe Bryant, his 13-year-old daughter, six passengers and the pilot died in a plane crash earlier this year in California.

“He said it should never have happened; it wasn’t safe with the weather,” said Thurston, who now lives outside Houston, Texas.

Bell’s bond with Thurston and three other friends — Matt Cornish, Matt Richardson and Bill Pientka — began the first day of ninth grade at Marcellus High School.

“Bill was the new kid in school,” Thurston said. “We started hanging out with him.”

Yes, they had classes together. But they also had a lot of fun together, said Richardson, who now lives in Raleigh, North Carolina.

“We’d Saran wrap people’s cars; line driveways with hundreds of driveway reflectors,” he said of their high school pranks. “Always having fun.”

Cornish, who still lives in Marcellus, said he and Bell worked together as ski instructors at Song Mountain in high school and on college breaks. He also remembers how Bell ran cross country, and how he dreamed of becoming a pilot.

“That’s all he ever wanted to do,” Cornish said.

During their senior year of high school, Bell’s life plans started to come together. He was accepted into Embry-Riddle Aeronautical University in Daytona Beach, Florida.

After graduation, his friends visited him in Florida.

“We always used to joke: He got his pilot’s license before he got his driver’s license,” Richardson said. “He could fly place to place, but once he got there, he couldn’t drive so he’d usually call a friend. Anytime we could, we gave him crap for it.”

Bell eventually got his driver’s license part-way through college, his friends said. And when he did, Richardson said, “he made a big deal, saying we couldn’t make fun of him for it anymore.”

After finishing flight school, Bell worked for a couple regional airlines and eventually moved west. At one point, he flew charter flights over the Grand Canyon; he also was a contractor for Google doing aerial photography; and he worked as a private pilot for the owners of Fox and later for a hedge fund billionaire, Cornish said.

In a group text once, Bell sent his friends a photo of him hanging out with Jerry Jones, Michael Strahan and Terry Bradshaw on the set of Fox NFL Sunday, Richardson said.

Before the coronavirus pandemic struck, Bell told his friends he was traveling frequently to New Zealand.

Then, in a text message a month or two ago, Bell told Thurston how he was flying “seven days on, seven days off for Elon,” and hoped to make it permanent. Thurston said Bell was referring to Tesla co-founder Elon Musk, although he did not know whether he flew Musk or someone else connected to Musk and his companies.

“Bill was very, very well traveled," Thurston said. “He flew to Southeast Asia, the Middle East, South America, everywhere in Europe."

“But his focus was always on his friends, asking what are you doing or how are your kids,” he said. "He was so humble; an easy-going guy; always joking around.”

Bell and his friends sent each other text messages regularly, they said. If he was flying in a city near where one of his friends lived, he’d try to stop by, hang out, have a beer and catch up.

Bell, Cornish, Thurston, Richardson and Pientka planned yearly get-togethers, and met in Florida, Ohio, Texas and North Carolina — all places someone in the group lived. This year’s trip was cancelled due to the pandemic, but the five friends still figured out a way to get together by having weekly Zoom meetings.

Throughout the years, Bell returned home to Marcellus for friends' weddings and some holidays. A couple years ago, he brought his daughter, Amira, home to meet his parents, his friends said.

Bells’ parents, William L. and Denise Bell, still live in the town of Marcellus. He’s also survived by a younger sister, Anne Bell, and a younger brother, Curt Bell.

Cornish described Bill Bell as “one of the most giving people I know.” He was so giving, Cornish said, that Bell twice gave someone in Florida and again in New York City his wallet after he took out his license and other important items. He also said Bell worked hard for all he had — and a year ago, Bell was able to buy his first plane.

“He was so excited to finally be able to own his own airplane,” Cornish said.

His friends say they’re still trying to understand how the accident happened and why Bill and Amira are gone.

“Because of covid, he was flying a lot less so he was home more and spending more time with his daughter,” Cornish said.

Bell had moved from his home just south of LAX airport to Peoria, Arizona to be closer to Amira, a third-grader who loved cheerleading and gymnastics. Bell’s girlfriend also lived in the area, so he was near those he cared about, his friends said.

In Arizona, friends, family and strangers have donated $19,000 to help Amira’s family pay for her memorial service and burial.

Cornish and Thurston said they are planning to travel to Peoria later this month for a celebration of Bell’s life on November 21st.

“Twenty years (of friendship) wasn’t enough. I think about him every day," Thurston said. “A small-town kid from Marcellus goes to Daytona Beach and in 16 years, sees the world. He’s lived and done more in his short life than most people have done in 10 life times."

Monday, October 26, 2020

Grumman American AA-5A Cheetah, N26136: Fatal accident occurred October 25, 2020 in Woodbranch, Montgomery County, Texas




This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

The National Transportation Safety Board traveled to the scene of this accident.

Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; Houston, Texas


Location: Woodbranch, TX 
Accident Number: CEN21FA026
Date & Time: October 25, 2020, 08:37 Local 
Registration: N26136
Aircraft: Grumman AA5 
Injuries: 2 Fatal
Flight Conducted Under:

On October 25, 2020, about 0837 central daylight time, a Grumman AA-5A airplane, N26136, was destroyed when it was involved in an accident near Woodbranch, Texas. The airline transport rated pilot and 1 passenger were fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight.

According to information provided by local authorities, the airplane took off on a planned IFR crosscountry flight in instrument meteorological conditions from runway 17 at the North Houston Airport (9X1) with a destination of Liberty, Texas (T78). Preliminary radar and Automatic Dependent Surveillance-Broadcast (ADS-B) data showed a normal takeoff and climb to the south and subsequent
turn to the east. Passing 1,600 ft, the pilot established communications with the air traffic controller and requested clearance to T78. The controller asked if they could maintain their own terrain and obstruction clearance until leaving 1,700 ft, to which the pilot responded in the affirmative.

The controller then cleared the airplane to T78 via radar vectors and instructed the pilot to climb to 3,000 ft and fly a heading of 270°. The airplane made a left turn to a northeast bound heading when the controller instructed them to stop their turn and climb to 3,000 ft. The airplane was climbing through 2,200 ft when the controller advised the pilot of antennas in front of them and again instructed him to climb to 3,000 ft. The airplane climbed to 2,400 ft, continued turning left, and then began descending rapidly. The Minimum Safe Altitude Warning activated as the airplane descended through 1,900 ft. The controller issued a Safety Alert and instructed the pilot to stop their descent and level off. Simultaneous loss of radar and radio communications occurred with the airplane heading east. The controller advised the pilot that radar contact was lost. There were no radio distress calls heard from the pilot. The estimated flight path is depicted in Figures 1 and 2.

A witness in the area heard what sounded like a go-cart or [motor] bike approaching. As it got louder and realized it was an airplane, he heard the engine “stall.” When the airplane was over his house, he reported the engine “cranked back up to a very high rpm” and then heard “a crash.” The airplane impacted beside his neighbor’s house.

The accident site was located in a wooded area bordering a residential neighborhood, about 8 miles east of 9X1. A photograph of the accident scene is at Figure 3. The elevation of the accident site was about 95 ft and the terrain was predominately flat. The airplane wreckage showed evidence of a nearly vertical impact. Most of the forward fuselage, engine, cabin, baggage compartment and aft fuselage was crushed aft and fragmented. Both wings were separated from the fuselage and broken in several sections. The broken wing sections showed aft crush impact damage spanning the leading edges. The propeller was fractured torsionally at the flange and both blades showed S-bending, leading edge gouges, and chordwise scratches. The wreckage was recovered and transported to a secure facility for detailed examinations of the airframe, engine, and systems.

Aircraft and Owner/Operator Information

Aircraft Make: Grumman 
Registration: N26136
Model/Series: AA5 A
Aircraft Category: Airplane
Amateur Built: No
Operator: 
Operating Certificate(s) Held: None
Operator Designator Code:

Meteorological Information and Flight Plan

Conditions at Accident Site: IMC
Condition of Light: Day
Observation Facility, Elevation: KIAH,105 ft msl 
Observation Time: 08:53 Local
Distance from Accident Site: 15 Nautical Miles 
Temperature/Dew Point: 17°C /15°C
Lowest Cloud Condition:
Wind Speed/Gusts, Direction: 4 knots / , 30°
Lowest Ceiling: Overcast / 500 ft AGL
Visibility: 3 miles
Altimeter Setting: 30 inches Hg 
Type of Flight Plan Filed: IFR
Departure Point:
Destination:

Wreckage and Impact Information

Crew Injuries: 1 Fatal 
Aircraft Damage: Destroyed
Passenger Injuries: 1 Fatal 
Aircraft Fire: None
Ground Injuries: 
Aircraft Explosion: None
Total Injuries: 2 Fatal 
Latitude, Longitude: 30.182166,-95.19281

Those who may have information that might be relevant to the National Transportation Safety Board investigation may contact them by email eyewitnessreport@ntsb.gov, and any friends and family who want to contact investigators about the accident should email assistance@ntsb.gov.


WOODBRANCH, Texas (KTRK) -- A Pearland resident was one of the two people on board a plane that crashed over the weekend in a wooded area of Montgomery County.

Texas Department of Safety identified the two people who died in the crash as Nodal Aoki, 41, of Porter, and Karthik Balakrishnan, 46, of Pearland. Aoki was behind the controls of the small aircraft.

The crash happened in the area of Linnwood Street in Woodbranch, near US 59 around 8:40 a.m. Sunday.

Residents in the area reported hearing the plane go down and Texas DPS troopers responded to the scene.

"My house shook," one resident said. "I thought something hit the house, so I ran out the front door. I looked around and the neighbors were all running outside."

Ahmad Siddiqi was distraught and said the pilot involved was his longtime friend who leaves behind a wife and three kids.

"Even until now I cannot even believe that it was him because he is such a good person, such a good pilot, such an experienced, such an all-together very, very humble and kind human being," Siddiqi said.

Woodbranch mayor Mike Tyson said the incident was completely unexpected and that this was "something new to us" and said "we hope it never happens to someone again."

The Grumman American AA-5A Cheetah was registered to a certificated pilot in Porter, according to FAA records.  Investigators with the FAA are taking the lead on the investigation into what led to the crash. The NTSB is also investigating.

Sunday, October 25, 2020

Fuel Exhaustion: Beechcraft 76 Duchess, N6015Z; accident occurred November 03, 2019 in Doral, Miami-Dade County, Florida

Fuel Gauges During Approach to Hilton Head Airport (KHXD)







National Transportation Safety Board
Aviation Accident Factual Report

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity: 
Federal Aviation Administration / Flight Standards District Office; Miramar, Florida

https://registry.faa.gov/N6015Z

Location: Doral, Florida 
Accident Number: ERA20TA030
Date & Time: November 2, 2019, 21:50 Local 
Registration: N6015Z
Aircraft: Beech 76 
Aircraft Damage: Substantial
Defining Event: Fuel exhaustion 
Injuries: 2 None
Flight Conducted Under: Part 91: General aviation - Personal

Factual Information

On November 3, 2019, about 2150 eastern standard time, a Beech 76, N6015Z, was substantially damaged during a forced landing on a road near Doral, Florida. The commercial pilot and a pilot-rated passenger were not injured. The airplane was operated by GPS Global Pilot School under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight. Night, visual meteorological conditions prevailed, and an instrument flight rules flight plan was filed for the flight. The flight originated at Hilton Head Airport (HXD), Hilton Head, South Carolina about 1840 and was destined for Miami Executive Airport (TMB), Miami, Florida.

The pilot reported that he landed at HXD with 55 to 60 gallons of fuel on board, and another 20 gallons of fuel were purchased before departing HXD. The fuel tanks were not filled to capacity at HXD. He estimated that the fuel needed to fly to TMB was 65 gallons with 15 gallons in reserve. The en route portion of the flight was uneventful. About 20 miles northwest of TMB, at 2,000 ft mean sea level (msl), the right engine "failed without warning." An attempt to restart the engine was unsuccessful. The right engine propeller was feathered. Following some radio communication problems, contact with Miami approach was re-established and the pilot diverted to Miami International Airport (MIA), Miami, Florida. About 500 ft msl, the left engine also experienced a sudden total loss of power. The pilot was unable to restart the engine and attempted a forced landing on a road to the west of MIA. Shortly before touchdown, the left wing struck a truck on the road. The airplane came to a stop and the pilots egressed the airplane and were met by first responders.

An inspector with the Federal Aviation Administration responded to the accident site and examined the wreckage. Both wings and the fuselage were structurally damaged. The airplane was equipped with a fuel tank in each wing, with a capacity of 50 gallons useable in each tank. The tanks were drained; 1/2 cup of fuel was recovered from the left tank and 1 cup of fuel was recovered from the right tank. The inspector arrived on scene within one hour of the accident and reported that there was no fuel leaking from either tank and no fuel stains were observed on the ground under the airplane. First responders also reported that there was no fuel leaking from the airplane when they arrived on scene.

Pilot Information

Certificate: Commercial; Flight instructor
Age: 27,Male
Airplane Rating(s): Single-engine land; Multi-engine land
Seat Occupied: Right
Other Aircraft Rating(s): None 
Restraint Used: 3-point
Instrument Rating(s): Airplane 
Second Pilot Present: Yes
Instructor Rating(s): Airplane single-engine; Instrument airplane
Toxicology Performed: No
Medical Certification: Class 1 Without waivers/limitations
Last FAA Medical Exam: October 22, 2019
Occupational Pilot: Yes 
Last Flight Review or Equivalent: February 28, 2019
Flight Time: 1491 hours (Total, all aircraft), 16 hours (Total, this make and model), 1400 hours (Pilot In Command, all aircraft), 157 hours (Last 90 days, all aircraft), 83 hours (Last 30 days, all aircraft), 3 hours (Last 24 hours, all aircraft) 

Pilot-rated passenger Information 

Certificate: Commercial; Flight instructor 
Age: 26,Male Airplane Rating(s): Single-engine land; Multi-engine land 
Seat Occupied: Left
Other Aircraft Rating(s): None Restraint Used: 3-point
Instrument Rating(s): Airplane 
Second Pilot Present: Yes
Instructor Rating(s): Airplane single-engine; Instrument airplane
Toxicology Performed: No
Medical Certification: Class 1 Without waivers/limitations
Last FAA Medical Exam: October 10, 2019
Occupational Pilot: Yes 
Last Flight Review or Equivalent: September 5, 2019
Flight Time: 1312 hours (Total, all aircraft), 5 hours (Total, this make and model), 1244 hours (Pilot In Command, all aircraft), 226 hours (Last 90 days, all aircraft), 78 hours (Last 30 days, all aircraft), 1 hours (Last 24 hours, all aircraft)

Aircraft and Owner/Operator Information

Aircraft Make: Beech 
Registration: N6015Z
Model/Series: 76 No Series 
Aircraft Category: Airplane
Year of Manufacture: 1979 
Amateur Built: No
Airworthiness Certificate: Normal 
Serial Number: ME-145
Landing Gear Type: Retractable - Tricycle 
Seats: 4
Date/Type of Last Inspection: October 1, 2019 Annual 
Certified Max Gross Wt.: 3900 lbs
Time Since Last Inspection: 
Engines: 2 Reciprocating
Airframe Total Time: 11508 Hrs as of last inspection
Engine Manufacturer: Lycoming
ELT: Installed 
Engine Model/Series: O360-A1G6D
Registered Owner: 
Rated Power: 180 Horsepower
Operator: 
Operating Certificate(s)Held: None

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual (VMC) 
Condition of Light: Night
Observation Facility, Elevation: KMIA,9 ft msl 
Distance from Accident Site: 3 Nautical Miles
Observation Time: 21:53 Local Direction from Accident Site: 280°
Lowest Cloud Condition: Scattered / 1100 ft AGL Visibility 10 miles
Lowest Ceiling: Broken / 2500 ft AGL 
Visibility (RVR):
Wind Speed/Gusts: 8 knots / 
Turbulence Type Forecast/Actual: None / None
Wind Direction: 40° 
Turbulence Severity Forecast/Actual: N/A / N/A
Altimeter Setting: 30.03 inches Hg 
Temperature/Dew Point: 24°C / 22°C
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: Hilton Head, SC (HXD ) 
Type of Flight Plan Filed: IFR
Destination: Miami, FL (TMB ) 
Type of Clearance: IFR
Departure Time: 18:40 Local
Type of Airspace: Class B

Airport Information

Airport: MIAMI INTL MIA 
Runway Surface Type: Asphalt
Airport Elevation: 9 ft msl 
Runway Surface Condition: Dry
Runway Used: 
IFR Approach: None
Runway Length/Width:
VFR Approach/Landing: Forced landing

Wreckage and Impact Information

Crew Injuries: 1 None 
Aircraft Damage: Substantial
Passenger Injuries: 1 None 
Aircraft Fire: None
Ground Injuries: N/A Aircraft
Explosion: None
Total Injuries: 2 None 
Latitude, Longitude: 25.796943,-80.34111(est)










Cessna 172H Skyhawk, N724BC: Fatal accident occurred October 25, 2020 and accident occurred June 29, 2019

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

The National Transportation Safety Board traveled to the scene of this accident

Additional Participating Entities: 
Federal Aviation Administration / Flight Standards District Office; Orlando, Florida
Textron Aviation; Wichita, Kansas 
Continental Motors; Tampa, Florida


Location: Dunnellon, FL 
Accident Number: ERA21FA029
Date & Time: October 25, 2020, 10:52
Local Registration: N724BC
Aircraft: Cessna 172 Injuries: 1 Fatal
Flight Conducted Under:

On October 25, 2020, at 1052 eastern daylight time, a Cessna 172H, N724BC, was substantially damaged when it was involved in an accident near Dunnellon, Florida. The pilot was fatally injured. The airplane was operated as a Title 14 Code of Federal Regulations (CFR) Part 91 personal flight.

The pilot, who was also the owner of the airplane held a private pilot certificate for single-engine airplanes with an instrument rating. A review of preliminary air traffic control (ATC) communications and radar data provided by the Federal Aviation Administration (FAA) revealed that the pilot was not in communication with ATC; however, radar data indicated that the airplane departed to the south from the Back Achers Airport (8FL3), Belleview, Florida, about 1034. He then turned toward the southeast and flew over Lake Weir before turning on a westerly heading toward the Marion County Airport (X35) at an altitude between 1,250 and 1,300 ft mean sea level (msl). Around 1038, the airplane began a slow descent to about 900 ft msl before climbing to about 1,000 ft msl. Between 1051:39 and 1052:02, the airplane decelerated from a groundspeed of about 94 knots to 47 knots. One second later, the airplane had climbed to 1,025 ft msl, then entered a descending left turn before the data ended at 1052:12. At that time, the airplane was at 600 ft msl, a heading of 086°, and a groundspeed of 60 knots. The airplane impacted a large open field in a nose-low attitude about 1.2 miles north-northeast of X35. The initial impact point was a ground scar that had pieces of the left-wing tip fairing embedded in the dirt. The airplane then traveled about 120 ft before coming to rest. On-scene examination of the airplane revealed that all major components of the airframe were located at the accident site and there was no postimpact fire. Both wings remained attached to the airframe but sustained extensive leading-edge impact damage. The flaps were retracted. The left fuel tank was breached and empty of fuel. The right fuel tank was intact; however, the fuel line was disconnected, and fuel was leaking from the line. A small amount of fuel was recovered from the airplane’s fuel system. The fuel was blue in color and absent of water and debris. The tail section was folded over the top of the airplane and sustained impact damage.

Flight control continuity was established from all major flight control surfaces to the cockpit. The fuel selector valve was in the “both” position. The airframe fuel filter was drained and about 1 tablespoon of cloudy water was removed. The fuel strainer was disassembled, and heavy corrosion was noted in the bowl and on the fuel filter screen.

The engine was partially separated from the firewall and came to rest next to the airplane. The two bladed propeller remained attached to the engine. One blade was bent aft about 20° and exhibited some leading-edge polishing and the other blade was straight.

The engine was placed on flatbed truck and the top spark plugs were removed and the engine was rotated manually via the propeller. Compression was established on all cylinders except for the No. 6 cylinder which sustained impact damage its pushrods. As the engine was being rotated, valvetrain continuity was established for each cylinder and spark was produced to each magneto ignition lead. The carburetor separated from the engine during impact. The carburetor was disassembled and empty of fuel;
however, a small amount of corrosion was observed in the fuel bowl and on the carburetor inlet screen.

The airplane was equipped with an electronic engine data monitor, which was removed for further examination and data download.

Aircraft and Owner/Operator Information

Aircraft Make: Cessna 
Registration: N724BC
Model/Series: 172 H 
Aircraft Category: Airplane
Amateur Built: No
Operator: Operating Certificate(s) Held: None
Operator Designator Code:

Meteorological Information and Flight Plan

Conditions at Accident Site: VMC 
Condition of Light: Day
Observation Facility, Elevation: OCF,89 ft msl 
Observation Time: 10:51 Local
Distance from Accident Site: 10 Nautical Miles
Temperature/Dew Point: 26°C /23°C
Lowest Cloud Condition: Clear 
Wind Speed/Gusts, Direction: 4 knots / ,
Lowest Ceiling: None
Visibility: 10 miles
Altimeter Setting: 29.95 inches Hg 
Type of Flight Plan Filed: None
Departure Point: Belleview, FL (8FL3)
Destination: 

Wreckage and Impact Information

Crew Injuries: 1 Fatal 
Aircraft Damage: Substantial
Passenger Injuries: N/A
Aircraft Fire: None
Ground Injuries: N/A 
Aircraft Explosion: None
Total Injuries: 1 Fatal 
Latitude, Longitude: 29.083241,-82.361285 (est)

Those who may have information that might be relevant to the National Transportation Safety Board investigation may contact them by email eyewitnessreport@ntsb.gov, and any friends and family who want to contact investigators about the accident should email assistance@ntsb.gov.
 
Police Chief Greg Graham, right, shown here flying with Marion County Sheriff Billy Woods.



DUNNELLON, Florida — Ocala Police Chief Greg Graham died Sunday morning in a small-plane crash in southwest Marion County, according to Ocala Mayor Kent Guinn.

The mayor said he received word from OPD Deputy Chief Mike Balken. Guinn has named Balken interim chief. 

Ocala Police Chief Greg Graham addressed the Ocala City Council in August when council was discussing the mask ordinance.

Marion County Fire Rescue received the plane crash call at 11:32 a.m. The plane crashed into an open field in the 9700 block of Southwest 140th Avenue, not far from the Marion County Airport, a county-owned facility in an unincorporated area near Dunnellon.

Valerie Strong, a spokeswoman for the Marion County Sheriff's Office, said no one else was injured.

According to Guinn, Graham had recently obtained his private pilot's certificate. He said the chief enjoyed skydiving and scuba diving and always had a fascination with flying.

"It's hard to believe," the mayor said.

Graham had served as chief since January 2012. At the time, the Star-Banner noted that he was the agency's 30th chief. (The police department dates back to 1869.)

Graham worked at OPD for many years, raising to the rank of deputy chief. He was interim chief for a short time in 2003 until Sam Williams was appointed. 

Graham left the agency in 2008 to become police chief in Cedar Rapids, Iowa. He was the first chief to be selected from outside the Cedar Rapids department in 30 years.

While in Iowa, he guided the department through rising flood waters in June 2008. Talking with a Star-Banner reporter, Graham said, “It’s trial by fire. I feel like I’m back in Florida during the 2004-2005 hurricanes we had, and we had to get ready for them.”

Graham came back to become Ocala chief after Williams resigned in late December 2011.

In 2013, after one year at the helm back in Ocala, Graham told the Star-Banner he was paying a lot of attention to department morale and best practices.

"Graham said he felt a disconnect between the administration, officers and civilian employees," the paper  wrote at the time. "So he engaged personnel, similar to an approach he used in Iowa, and adopted a few tenets he hoped would break down barriers.

"They were simple: Do the right thing, ask for forgiveness instead of permission, find ways to say yes, treat everyone with respect and have fun." 

About two dozen law enforcement vehicles, with light bars activated, were parked in front of the Ocala Police Department on Sunday. Drivers on Pine Avenue, just south of Silver Springs Boulevard honked in salute.

In 2016, Graham was placed on paid administrative leave when a grievance was filed on behalf of three police officers alleging racial discrimination, sexual harassment, hostile treatment and retaliation. He was reinstated in January 2017 after a law firm hired by the city cleared him and recommended that he be reinstated with all rights and benefits.

Despite that report, and City Council's decision to reinstate Graham, the city later agreed to pay $500,000 in settlements to the officers.

In February 2018, through the leadership of the mayor, Graham and other community leaders, the police department started a special Heroin/Opioid Amnesty Program. Simply put, the program allowed anyone experiencing a drug addiction problem to come forward and receive help – no judgment and no penalties.

"Graham said the goal is to get those who need help the assistance they need because the agency will never be able to 'arrest our way out of this crisis,' ” the Star-Banner wrote at the time.

Most recently, Graham has been a presence at demonstrations in downtown Ocala that were held in the wake of George Floyd's death. When a group marched from downtown to a local park, Graham was there with them, bullhorn in hand, so he could be heard.

"He affirmed the group’s right to gather and said he shared their dismay about what happened in Minneapolis," the Star-Banner reported at the time. "He said members of the public could call him personally if they believe one of his officers has done anything wrong. He promised that any such complaint would prompt an investigation and consequences, if wrongdoing is confirmed."

In Ocala's system of government, the mayor oversees the police department.

"His leadership was responsible for changing the direction of the department," Guinn said on Sunday. "I couldn't have asked for anybody better."

As the news spread on Sunday, leaders and residents began posting reactions on social media.

"An incredibly tragic day for Ocala. Please pray and send comforting thoughts to the entire Graham family," City Council member Matt Wardell posted on Facebook.

"I will miss you my friend," former school board candidate and community leader Shelia Arnett wrote on Facebook.

The police department itself posted a Facebook tribute. Meanwhile, more than two dozen law enforcement vehicles, light bars activated, were parked in tribute outside police headquarters on Pine Avenue just south of Silver Springs Boulevard.

"We have had the great privilege to have called him a friend, a boss, and a part of our family for well over thirty years," the department's post said. "He was the heart of the Department. His heart beat for Ocala, for his community, for his department, and especially for his family.

"We will miss his passion for community and law enforcement; his candor and personality; his strong leadership; and most definitely his smile." 

Sheriff Billy Woods, a former OPD officer and Graham's friend, said at a news conference at the Sheriff's Office said they were shocked and grieve-stricken to learn that the pilot was his friend and mentor, Chief Greg Graham.

Woods said he had the pleasure of serving with Graham for more than 30 years in law enforcement. He said they don't have all the answers on what happened, and investigators will be working on it in the coming days.

He said he and Balken met with Graham's wife and family and they will need "your prayers in the weeks and months ahead." He said he and Balken have also spoken to the staff and the men and woman of the OPD and they too will need "your prayers and thoughts."

The Sheriff said the two agencies have enjoyed "a great working relationship." He said he considered Graham a personal friend. 

"I call him a friend and mentor," Woods said, adding Graham loved being chief and loved Ocala and Ocala loved him. He said Graham did "quite a bit and was taken too soon."

In his remarks, Balken said the area has "lost one of greatest lawmen I've ever known." He called Graham "a true mentor," and "a true leader." Balken said Graham was "a forward-thinking professional," and one of the greatest friends he has ever had in his life.

Balken said Graham has done "tremendous things for this community and will be truly missed by our entire agency." He said their department is reeling upon hearing the news.

Woods said the the Federal Aviation Administration will be conducting the investigation into the cause of the crash.

  


Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; Greer, South Carolina

Location: Greer, SC
Accident Number: GAA19CA477
Date & Time: 06/29/2019, 1809 EDT
Registration: N724BC
Aircraft: Cessna 172
Aircraft Damage: Substantial
Defining Event: Loss of control on ground
Injuries: 1 None
Flight Conducted Under: Part 91: General Aviation - Personal 

The pilot reported that, he entered the traffic pattern, downwind, and that the airplane's airspeed was too fast, and the altitude was too high. The pilot decided to continue the landing and the airplane touched down about mid-field on the 1700ft runway. The pilot tried to use aerodynamic braking, but the airplane overran the end of the runway and collided with a drainage culvert.

The airplane sustained substantial damage to the left side elevator and the rudder.

The pilot reported that there were no preaccident mechanical failures or malfunctions with the airplane that would have precluded normal operation.

Pilot Information

Certificate: Private
Age: 57, Male
Airplane Rating(s): Single-engine Land
Seat Occupied: Left
Other Aircraft Rating(s): None
Restraint Used:
Instrument Rating(s): None
Second Pilot Present: No
Instructor Rating(s): None
Toxicology Performed: No
Medical Certification: Class 3 Without Waivers/Limitations
Last FAA Medical Exam: 05/03/2018
Occupational Pilot: No
Last Flight Review or Equivalent: 08/30/2018
Flight Time:   (Estimated) 206 hours (Total, all aircraft), 194 hours (Total, this make and model), 206 hours (Pilot In Command, all aircraft), 65 hours (Last 90 days, all aircraft), 18 hours (Last 30 days, all aircraft), 4 hours (Last 24 hours, all aircraft)

Aircraft and Owner/Operator Information

Aircraft Make: Cessna
Registration: N724BC
Model/Series: 172 H 
Aircraft Category: Airplane
Year of Manufacture: 1966
Amateur Built: No
Airworthiness Certificate: Normal
Serial Number: 17255148
Landing Gear Type: Tricycle
Seats: 4
Date/Type of Last Inspection: 03/13/2019, Annual
Certified Max Gross Wt.: 2300 lbs
Time Since Last Inspection:
Engines: 1 Reciprocating
Airframe Total Time: 8330.4 Hours at time of accident
Engine Manufacturer: Continental
ELT: C91 installed, not activated
Engine Model/Series: O-300-D
Registered Owner: On file
Rated Power: 145 hp
Operator: On file
Operating Certificate(s) Held: None 

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual Conditions
Condition of Light: Day
Observation Facility, Elevation: KGSP, 971 ft msl
Distance from Accident Site: 3 Nautical Miles
Observation Time: 2153 UTC
Direction from Accident Site: 175°
Lowest Cloud Condition: Clear
Visibility:  10 Miles
Lowest Ceiling: None
Visibility (RVR):
Wind Speed/Gusts: 9 knots /
Turbulence Type Forecast/Actual:
Wind Direction: 190°
Turbulence Severity Forecast/Actual:
Altimeter Setting: 30.1 inches Hg
Temperature/Dew Point: 32°C / 16°C
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: Greenville, SC (GMU)
Type of Flight Plan Filed: None
Destination: Greer, SC (PVT)
Type of Clearance: VFR
Departure Time: 1801 EDT
Type of Airspace: Class G

Airport Information

Airport: Flying Few (PVT)
Runway Surface Type: Dirt; Grass/turf
Airport Elevation: 1024 ft
Runway Surface Condition: Dry; Soft; Vegetation
Runway Used: 28
IFR Approach: None
Runway Length/Width: 1700 ft / 100 ft
VFR Approach/Landing: Full Stop; Traffic Pattern

Wreckage and Impact Information

Crew Injuries: 1 None
Aircraft Damage: Substantial
Passenger Injuries: N/A
Aircraft Fire: None
Ground Injuries: N/A
Aircraft Explosion: None
Total Injuries: 1 None
Latitude, Longitude: 34.938611, -82.227222 (est)