Saturday, April 08, 2017

Newly constructed hangar to bring economic boom in Ames, Iowa




AMES, Iowa —   

Hundreds of community members and pilots drove or flew into the Ames Municipal Airport bright early Saturday as the community came together to celebrate a major milestone.

A new airport hangar is set to change the face of Ames.

Pilots Terry Schleisman said his passion is flying his 70-year-old Piper Cub. “It’s just a tremendous sense of freedom. Just fun, just unbound," he said.

Schleisman bonded with other aviation enthusiasts while celebrating a new 11,400-square-foot hangar.

“That puts us in the class of an airport where we can get bigger planes in versus where people may just want to go to Des Moines,” said Damion Pregitzer, airport manager and traffic engineer. “That lets them come here, do business in Ames, which is important to us.”

It’s all part of a modernization project, which also includes construction of a new terminal, bringing with it an economic boost to the area.

“When you have the facilities that can support a certain level of economy, that’s when you start to see people not just wanting to come here, but actually base their business here, their aircraft here,” Pregitzer said. “It all works together in the big picture for Ames."

It’s a culmination of six years’ worth of hard work between a private-public sector partnership.

“For many people that visit Ames, this will now be our front door,” said Rick Sanders, chairman of the Story County Board of Supervisors. “This will be their first impression of Ames.”

Leaders say it opens the door for pilots like Schleisman to come to Ames more frequently.

“It’s only the beginning, so what we hope is this will be a catalyst to get more growth, maybe get more hangars, more aircraft, on the field,” Pregitzer said. “It’s only up from here, really.”

The new hanger can hold 12 business jet-size aircraft at a time. The terminal is halfway done. It is scheduled to be complete by July 1. 

Story and video:   http://www.kcci.com

Cessna 182Q Skylane, United States Forest Service, N759LV: Accident occurred July 21, 2015 in Prichard, Shoshone County, Idaho

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entities:

Federal Aviation Administration / Flight Standards District Office; Spokane, Washington 
USDA Forest Service; Boise, Idaho

Aviation Accident Factual Report - National Transportation Safety Board:  https://app.ntsb.gov/pdf


Docket And Docket Items - National Transportation Safety Board:   https://dms.ntsb.gov/pubdms


http://registry.faa.gov/N759LV 





NTSB Identification: WPR15LA220
14 CFR Part 91: General Aviation
Accident occurred Tuesday, July 21, 2015 in Prichard, ID
Probable Cause Approval Date: 05/23/2017
Aircraft: CESSNA 182Q, registration: N759LV
Injuries: 2 Uninjured.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

The commercial pilot reported that, during cruise on the fire reconnaissance flight, he heard a loud pop, followed by oil covering the windscreen; the engine subsequently experienced a total loss of power. Despite the pilot’s attempts, the engine would not restart, and he initiated a forced landing to an open field. During the landing roll, the nose landing gear separated from the airplane and the right wing impacted the ground. Postaccident examination of the engine revealed that the bottom portion of the No. 6 cylinder piston, piston pin, and connecting rod cap were separated.

Metallurgical examination of the piston pin revealed evidence of a fatigue fracture originating from the outside of the pin that progressed inward until the final fracture along the middle of the pin cross-section. The fatigue crack initiation site did not reveal any material or mechanical defects, such as pits, voids, or inclusions. Examination of the piston, connecting rod bolts, and connecting rod cap revealed fractures consistent with overstress. No additional anomalies were noted with the engine.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
A total loss of engine power due to the fatigue failure of the No. 6 cylinder piston pin.

On July 21, 2015, about 1446 mountain daylight time, a Cessna 182Q, N759LV, was substantially damaged during a forced landing near Prichard, Idaho. The airplane was registered to and operated by Interstate Aviation, Pullman, Washington, under contract with the United States Forest Service. The local fire reconnaissance flight was operated under the provisions of 14 Code of Federal Regulations (CFR) Part 135. The commercial pilot and his passenger were not injured. Visual meteorological conditions prevailed and a company flight plan was filed for aerial observation flight. The local flight originated from Coeur d'Alene, Idaho, about 2 hours prior to the accident.

The pilot reported that during cruise flight, he heard a loud pop, followed by oil covering the windscreen. Despite the pilot's attempts, the engine would not restart and he initiated a forced landing to an open field. Subsequently, during the landing roll, the nose wheel landing gear separated from the airplane and the right wing impacted the ground.

Examination of the airplane by the pilot revealed that the right wing was substantially damaged. The wreckage was recovered to a secure location for further examination.

Examination of the recovered airframe and engine revealed a large hole in the crankcase above cylinder number 6. Several pieces of the engine case and the number 6 piston pin were found outside the engine case lying between the cylinders. The upper portion of the number 6 piston was still in the cylinder. The piston could be moved by hand within the cylinder. Portions of the lower part of the piston, piston rings, the connecting rod cap and bolts were located within the oil sump. No evidence of any overheat or thermal damage was observed on the crankshaft.

The remains of the number 6 piston, piston pin, and connecting rod were sent to the NTSB Materials Laboratory, Washington, DC, for further examination.

According to a materials engineer, the examination revealed that the underside of the piston crown was fractured into smaller pieces near the piston pin position. The fracture surface exhibited a rough, tortuous appearance along with a dull luster. The fracture surface of the piston crown exhibited river lines and chevron marks consistent with fracture originating at the pin position. The fracture features of the piston crown underside were consistent with overstress failure. No indications of pre-existing cracking or progressive failure were observed on the piston fracture surfaces.

One of the two connecting rod bolts was fractured in two halves, exhibiting a 45 degree slant fracture surface with localized necking adjacent to the fractures. The bolt fracture surface showed a dull luster and rough surface. All of these features were consistent with failure from tensile overstress. Only half of the other bolt was found, and was bent over, with a relatively flat fracture surface along the bolt threads. This fracture surface also exhibited dull, gray, and rough features. These characteristics were consistent with failure from overstress in bending.

The connecting rod was generally intact with no indication of cracking, fracture, twisting or gross deformation along the rod. The connecting rod cap exhibited twisting and deformation consistent with batter from impacts with an adjacent object. However, there were no indications consistent with the connecting rod or cap having failed prior to the bolts fracturing.

The piston pin exhibited some wear and impact marks along the barrel. Of note was that one of the tapered piston pin ends had separated and had become deformed into a spherical shape. Most of the fracture surface exhibited a shiny luster and general flat shape, consistent with post-fracture batter. The middle of the pin fracture had a raised, flattened feature. Around the periphery of the fracture surface, adjacent to the barrel of the pin, the fracture surface exhibited ridges consistent with ratchet marks. The ratchet marks are consistent with multiple smaller cracks that coalesce to form a larger crack. A less damaged area of the fracture surface, exhibited crack arrest marks consistent with progressive failure.

Closer examination of the visible progressive features using a scanning electron microscope (SEM), revealed striations consistent with fatigue cracking. Examination of the fatigue crack initiation site did not reveal any material or mechanical defects, such as pits, voids, or inclusions. All of the features of the pin fracture surface were consistent with fatigue cracking initiating around the outside of the pin, with the final fracture along the middle of the pin cross section.

The spherical deformed separated portion of the pin exhibited severe damage which obscured the features that would conclude fracture information. A circular impression was visible on the spherical fragment. The volume of the spherical pin remnant was consistent with a spherical impression on the underside of the piston crown and is consistent with it occurring after the severe deformation of the now spherical pin fragment.

The composition of the pin fracture surface was examined using energy dispersive x-ray spectroscopy (EDS). The composition was consistent with AA 2000 series aluminum alloy. Further inspection using x-ray fluorescence (XRF) found the pin material to be consistent with AA 2024 aluminum. The hardness was inspected per ASTM E18.2 The hardness of the section averaged 81 HRBW. The electrical conductivity of the part was inspected per ASTM E1004.3 The conductivity averaged 39.0% IACS. These data were consistent with a T6X or T8X temper for this alloy.

Review of the engine logbooks revealed that the engine was overhauled on August 8, 2008. At this time, new piston pins, part number SA 539467 were installed. The most recent logbook entry, dated July 14, 2015, was a 100-hour inspection, at a time since major overhaul (TSMOH) of 1,427.1 hours and HOBBS time of 2,344.6 hours. At the time of the accident, the engine had accumulated 1,455 hours TSMOH.

Cork runway may be too short for Norwegian Air flights to New York: Proposed route hinges on fuel consumption of new Boeing aircraft, airline says



Norwegian Air International may not be able to fly its proposed route from Cork to New York because the Irish airport’s runway is too short, according to its group chief executive, Bjorn Kjos.

The carrier will begin flying from Ireland to the US east coast from July, including the first transatlantic service from Cork, which will serve TF Green Airport in Providence.

Norwegian is also considering a service to Stewart International in New York state from Cork next year, but Mr Kjos said the airline would have to see if it was possible to fly this route “because of the runway length”.

The length of Cork Airport’s runway, 2,133m, means Norwegian cannot fill the Boeing 737 Max aircraft it intends using on the Providence route, to ensure the aircraft can take off.

Fuel consumption

However, because New York is further south, and thus a longer journey, Mr Kjos said that it may not be possible to complete it from Cork and that this would hinge on fuel consumption.

“We have to see the reality of the Max, because we are the first ones flying it,” he said. “It might be that it is better than they guarantee, and if it’s better than they guarantee, we might be able to do it. We have to find out when we start flying.”

He pointed out that aircraft manufacturers base their guarantees on prototypes and added that the aircraft added to fleets generally surpass those standards comfortably.

Mr. Kjos is chief executive of Norwegian Air International’s parent, Norwegian Air Shuttle. He was in Dublin for the industry gala ball organised by the Irish Aviation Authority (IAA), at which he received the award for his contribution to aviation.

Norwegian Air International is an Irish-registered airline which the parent intends intends using to fly low-cost, long-haul services between Europe, the US and Asia.

Three-year battle

It fought a three-year battle to get permission to fly to the US, which it finally received last December. The company employs 85 people in Dublin and has 57 craft registered in the Republic. Overall it has 2,100 pilots and crew.The Irish office is responsible for safety – which the IAA regulates – marketing, finance and leasing.

Mr. Kjos confirmed that Norwegian now has an agreement with Ryanair enabling them to transfer passengers between each other’s flights. He said both airlines were working on a way of allowing their systems to communicate with each other. He was hopeful this would be done in weeks.

He did not rule out the possibility that Norwegian would begin flying from Dublin direct to the Far East. The airline has a base in Bangkok. As it would have to use the Boeing Dreamliner on this route, it could fly only from the capital’s airport.

From next July, Norwegian will begin flying from Belfast, Cork, Dublin and Shannon to airports in the northeast US with access to Boston and New York.

Original article can be found here:    http://www.irishtimes.com

EDI Express Turbine Express 2000 RG, N44508: Fatal accident occurred May 30, 2022 and Accident occurred May 29, 2015

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed.

The National Transportation Safety Board traveled to the scene of this accident. 

Additional Participating Entities: 
Federal Aviation Administration / Flight Standards District Office; Denver, Colorado 
Transportation Safety Board of Canada


Location: Cheyenne, Wyoming
Accident Number: CEN22FA216
Date and Time: May 30, 2022, 07:48 Local 
Registration: N44508
Aircraft: Express 2000RG 
Injuries: 1 Fatal
Flight Conducted Under: Part 91: General aviation - Personal

On May 30, 2022, about 0748 mountain daylight time, an Express 2000RG airplane, N44508, was destroyed when it was involved in an accident near Cheyenne, Wyoming. The pilot was fatally injured. The airplane was operated under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight.

According to preliminary information obtained by investigators, the airplane departed the Cheyenne Regional Airport/Jerry Olson Field (CYS) from runway 27, about 0744, with the intention of flying to Texas. Shortly after takeoff, the pilot declared an emergency with air traffic control (ATC) tower personnel and informed them that he had “an engine failure” and was about 4 miles south of the airport. He later reported that he would not be able to land at the airport and intended to land in a field. He also stated that he was “on fire” and asked ATC to send fire rescue. Video cameras from a local business captured a portion of the accident sequence which showed the airplane descending, near vertical, with a right roll.

The airplane collided with a storage facility. The initial impact point was a divot in the concrete. The wreckage path continued about 15 ft into a storage locker. A post crash fire ensued which consumed a majority of the airplane.

After on-scene documentation, the airplane was moved to a secure facility for further examination. 

Aircraft and Owner/Operator Information

Aircraft Make: Express 
Registration: N44508
Model/Series: 2000RG 
Aircraft Category: Airplane
Amateur Built: Yes
Operator: On file 
Operating Certificate(s) Held: None
Operator Designator Code:

Meteorological Information and Flight Plan

Conditions at Accident Site: VMC 
Condition of Light: Day
Observation Facility, Elevation: KFEW, 6160 ft msl
Observation Time: 07:58 Local
Distance from Accident Site: 3 Nautical Miles 
Temperature/Dew Point: 10°C /0°C
Lowest Cloud Condition: Few / 12000 ft AGL
Wind Speed/Gusts, Direction: 15 knots / 22 knots, 300°
Lowest Ceiling:
Visibility: 10 miles
Altimeter Setting: 29.59 inches Hg 
Type of Flight Plan Filed:
Departure Point: Cheyenne, WY (CYS)
Destination:

Wreckage and Impact Information

Crew Injuries: 1 Fatal
Aircraft Damage: Destroyed
Passenger Injuries:
Aircraft Fire: On-ground
Ground Injuries: 
Aircraft Explosion: None
Total Injuries: 1 Fatal
Latitude, Longitude: 41.132417,-104.79194

Aircraft crashed under unknown circumstances into a storage unit.

Date: 30-MAY-22
Time: 13:49:00Z
Regis#: N44508
Aircraft Make: EXPRESS AIRCRAFT
Aircraft Model: 2000 RG
Event Type: ACCIDENT
Highest Injury: FATAL
Total Fatal: 1
Flight Crew: 1 fatal
Pax: 0 
Aircraft Missing: No
Damage: SUBSTANTIAL
Activity: PERSONAL
Flight Phase: INITIAL CLIMB (ICL)
Operation: 91
City: CHEYENNE
State: WYOMING

Those who may have information that might be relevant to the National Transportation Safety Board (NTSB) investigation may contact them by email witness@ntsb.gov, and any friends and family who want to contact investigators about the accident should email assistance@ntsb.gov. You can also call the NTSB Response Operations Center at 844-373-9922 or 202-314-6290. 



Jason Aguilera (left), Senior Air Safety Investigator
National Transportation Safety Board 




CHEYENNE, Wyoming (Wyoming News Now) - Three (3) minutes. That is the amount of time between take-off, and a deadly crash.

According to flight records, the pilot took off from Cheyenne Regional Airport at 7:44AM on Memorial Day. The flight came to an end three minutes later at 7:47AM when the plane crashed into the Cheyenne Storage facilities.

Jason Aguilera, a Senior Air Safety Investigator with the National Transportation Safety Board was on the scene today.

“What we’re looking at right now is just kind of how it actually hit the storage facility behind us, the angle it went in, and then the damage that was resulted as a part of that. So we did a documentation yesterday, we’re finishing up today. And the wreckage is being removed to a secure facility where we’ll do follow up work on the engine and propeller.” he said when asked what the NTSB was doing at the site.

The pilot was flying what authorities called an experimental aircraft. These planes are not manufactured by major corporations, but instead by amateur. The planes are still certified by the FAA.

Investigators will be looking into the pilot, the plane, weather and more to try to determine a cause for the crash.

A preliminary report is expected to be released 15 days after the accident happened.

Investigations involving fatalities can take 12-24 months to complete.




CHEYENNE, Wyoming –  An EDI Express Turbine Express 2000 RG experimentally amateur built airplane crashed at around 8 a.m. Monday into a storage unit on Crook Avenue, near Nationway.

The crash appeared to have caused a relatively small blaze that was extinguished within about half an hour. Besides the pilot, there were no other fatalities.

The pilot of the aircraft was its sole occupant. The person, who authorities did not identify by name, has died, according to an update the Cheyenne Police Department distributed by email at around 1 p.m.

The individual was an adult male, CPD spokesperson Alex Farkas said by phone Monday afternoon. "No further injuries have been reported," according to the police department's news release.

The airplane had taken off from Cheyenne Regional Airport and was headed to Texas, according to National Transportation Safety Board spokesperson Jennifer Gabris. "An NTSB investigator arrived on scene this afternoon," Gabris wrote in an email to the Wyoming Tribune Eagle.

The county coroner's office has received the body of the pilot, Coroner Rebecca Reid said in a brief phone interview. She said that it might take a few days to get a positive identification. Once that occurs, the coroner's office will notify that individual's family, she told the WTE.

First responders from multiple agencies had been on the scene, authorities had said earlier Monday. By early afternoon, CPD personnel had remained there only to direct traffic, Farkas said. "We are no longer documenting what’s happening at the scene. It's been turned over" to federal authorities, she said by phone.

Cheyenne Fire Rescue had worked to extinguish the blaze at Cheyenne Storage, 616 Crook Ave. At around the time of the crash, CFR had sent six fire engines to the location, and they were able to contain the fire at around 8:30 a.m., authorities said.

Some 30 firefighters went to the location "during the initial incident, but currently two (investigative and commander) fire personnel are here," Andrew Dykshorn, CFR's division chief of operations, wrote in an email to the WTE at around 2:30 p.m. "There is one storage unit that was involved in the incident."

Initially at the time of the crash-landing, "there was a full police response to the crash, everyone who was on shift responded (10-12 officers) for traffic control and investigation," police spokeswoman Farkas wrote to the WTE. "Some officers from the previous shift remained on the clock to cover other calls for service in town."

Cheyenne Storage

When the plane crashed, Cheyenne Storage was closed to customers, a co-owner said by phone Monday afternoon; she would not provide her name.

As she spoke with the WTE, she said that another co-owner was speaking with a representative of the NTSB. At the time of the crash, the co-owner was at the business, although he did not see the incident, the fellow co-owner recounted.

"No one here was hurt, just the pilot," the business owner said by phone. She said that the storage facility's office, from where she was speaking, was not damaged.

Part of Nationway remained closed. "They were starting to clear things up" in the early afternoon, Farkas said. "Definitely sometime today, the road should be open again; hoping (for) this evening." Residents were being asked to remain away from the area so as not to interfere with first responders.

As the CPD's early-afternoon news release said, "the scene is still active and has now been turned over to the National [Transportation] Safety Board and Federal Aviation Administration."

Federal investigation

Both the FAA and the NTSB "will investigate" what happened, an FAA spokesperson wrote in an email to the WTE.

"The NTSB will be in charge of the investigation and provide additional updates," the FAA spokesperson added in his email. The NTSB has a regional office in Denver, according to the agency's website. 

In approximately 15 business days, the NTSB will release a preliminary report on the crash, spokesperson Gabris said by phone.

The initial report will contain all of the factual information that is known about the incident, Gabris said. A final report, with an analysis and suggesting a probable cause of the crash, would typically be released within a year or two, the spokeswoman estimated.

Part of the NTSB's "investigation will be to request radar data, weather information, maintenance records and the pilot’s medical records. NTSB investigators will look at the human, machine and environment as the outline of the investigation," Gabris wrote in her later email.

In addition to CFR, CPD and the Laramie County coroner's office, Wyoming Air National Guard Fire, the Cheyenne-Laramie County Emergency Management Agency and the Laramie County Fire Authority were described as being among "the partnering agencies assisting with the initial investigation."

Clarification: An earlier online version of this report said that the NTSB could release its initial report around June 15. Given the agency expects to issue the document in about 15 business, not calendar, days, the actual date of release would be later in June. This reference has been removed from an updated version of this article.




CHEYENNE, Wyoming — The National Transportation Safety Board and Federal Aviation Administration have taken over the scene of a plane crash that killed one person this morning, officials said.

The Cheyenne Police Department and Cheyenne Fire Rescue responded at around 8 a.m. today to 616 Crook Ave., where an experimental aircraft crashed into Cheyenne Storage, the department said in a news release.

According to the Experimental Aircraft Association, amateur-built aircraft built by individuals and licensed by the FAA receive the experimental designation.

An investigation by multiple agencies determined the pilot, who was the sole occupant, sustained fatal injuries. No other injuries have been reported, police said.

Authorities have not released the identity of the pilot.

The storage facility caught fire as a result of the crash, and the fire department deployed six engines to fight it. The fire was contained at about 8:30 a.m.

The scene remains active, police said. It has been turned over to the NTSB and FAA.

Partnering agencies in the initial investigation included Cheyenne Fire Rescue, Cheyenne Police Department, Wyoming Air National Guard Fire, American Medical Response, Cheyenne/Laramie County Emergency Management Agency, Laramie County Coroner and Laramie County Fire Authority, police said.





UPDATE 12:45 p.m.: The pilot of an experimental aircraft that crashed in East Cheyenne on Monday sustained fatal injuries in the accident, according to a joint news release from the Cheyenne Police Department and Cheyenne Fire Rescue.

But the release does not name the pilot, adding that the crash will be investigated by the Federal Aviation Administration and the National Transportation Safety Board.

According to the release, the crash was reported around 8 a.m. at Cheyenne Storage at 616 Crook Avenue. Cheyenne Police and Cheyenne Fire Rescue responded to the scene, and firefighters battled a blaze that had been ignited at the storage facility by the crash. Six fire engines were deployed, and the fire was contained by 8:30 a.m.

The release says

"Cheyenne Fire Rescue, Cheyenne Police Department, Wyoming Air National Guard Fire, American Medical Response, Cheyenne/Laramie County Emergency Management Agency, Laramie County Coroner, Laramie County Fire Authority are the partnering agencies assisting with the initial investigation."

Other than the pilot, no injuries have been reported in connection with the crash.

Original Post: Cheyenne Police say an experimental aircraft has crashed in the area of Cheyenne Storage at 616 Crook Avenue

Details are still sketchy at this hour, but the aircraft was believed to have one person aboard. At the last report, the eastbound lane of Nationway was closed, and people were being asked to avoid the area.

We'll report more information as it becomes available.





CHEYENNE, Wyoming — The National Transportation Safety Board and Federal Aviation Administration have taken over the scene of a plane crash that killed one person this morning, officials said.

The Cheyenne Police Department and Cheyenne Fire Rescue responded at around 8 a.m. today to 616 Crook Ave., where an experimental aircraft crashed into Cheyenne Storage, the department said in a news release.

According to the Experimental Aircraft Association, amateur-built aircraft built by individuals and licensed by the FAA receive the experimental designation.

An investigation by multiple agencies determined the pilot, who was the sole occupant, sustained fatal injuries. No other injuries have been reported, police said.

Authorities have not released the identity of the pilot.

The storage facility caught fire as a result of the crash, and the fire department deployed six engines to fight it. The fire was contained at about 8:30 a.m.

The scene remains active, police said. It has been turned over to the NTSB and FAA.

Partnering agencies in the initial investigation included Cheyenne Fire Rescue, Cheyenne Police Department, Wyoming Air National Guard Fire, American Medical Response, Cheyenne/Laramie County Emergency Management Agency, Laramie County Coroner and Laramie County Fire Authority, police said.





CHEYENNE, Wyoming — A pilot died after an experimental aircraft crashed in east Cheyenne, Wyoming, on Monday morning.

Around 8 a.m. Monday, the Cheyenne Police Department and Cheyenne Fire Rescue responded to a report of an aircraft crash at Cheyenne Storage, located at 616 Crook Avenue, about 9 miles north of the Colorado-Wyoming border.

When authorities arrived, they found an experimental aircraft had crashed and the pilot — the only person in the aircraft — had died at the scene, police said.

The crash started a fire at the storage facility, which firefighters were able to contain by 8:30 a.m.

The scene remained active as of 1 p.m. The National Transportation Safety Board and Federal Aviation Administration is investigating the crash.

In addition to the Cheyenne police and fire departments, the Wyoming Air National Guard Fire, American Medical Response, Cheyenne/Laramie County Emergency Management Agency, Laramie County Coroner, and Laramie County Fire Authority also helped with the initial investigation.

No other details were available as of 1:45 p.m. Monday.





One person died Monday when an experimental plane crashed in Cheyenne, authorities there said. 

The aircraft crashed at Cheyenne Storage, southeast of downtown, at about 8 a.m., according to a joint statement from Cheyenne police and fire. The pilot, the only occupant, died.

No other injuries were reported.

The crash ignited a fire at the storage facility, which crews contained in about a half hour.

The National Transportation Safety Board and Federal Aviation Administration will investigate.





CHEYENNE, Wyoming (WNE) — A single-engine experimental plane crashed at around 8 a.m. Monday into a storage unit on Crook Avenue, near Nationway.

The crash appeared to have caused a relatively small blaze that was extinguished within about half an hour. Besides the pilot, there were no other fatalities.

The pilot of the aircraft, which federal air authorities described as an Express 2000 RG, was its sole occupant. The person, who authorities did not identify by name, has died, according to an update the Cheyenne Police Department distributed by email at around 1 p.m. Monday.

The individual was an adult male, CPD spokesperson Alex Farkas said by phone Monday afternoon.

“No further injuries have been reported,” according to the police department’s news release.

The airplane had taken off from Cheyenne Regional Airport and was headed to Texas, according to National Transportation Safety Board spokesperson Jennifer Gabris.

Coroner Rebecca Reid said in a brief phone interview that it might take a few days to get a positive identification of the pilot.

Both the FAA and the NTSB will investigate the incident, an FAA spokesperson wrote in an email to the WTE. In approximately 15 business days, the NTSB will release a preliminary report on the crash, Gabris said.

A final report, with an analysis and suggesting a probable cause of the crash, will be released within a year or two, the spokeswoman estimated.









Aviation Accident Final Report - National Transportation Safety Board

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:
Federal Aviation Administration / Flight Standards District Office; Scottsdale, Arizona 

Investigation Docket - National Transportation Safety Board:


Location: Glendale, Arizona 
Accident Number: WPR15LA179
Date and Time: May 29, 2015, 15:42 Local 
Registration: N44508
Aircraft: BURR EXPRESS 2000 RG 
Aircraft Damage: Substantial
Defining Event: Landing gear collapse 
Injuries: 2 None
Flight Conducted Under: Part 91: General aviation - Personal

Analysis

The private pilot reported that, following a normal landing in the experimental amateur-built airplane, he applied beta thrust to decelerate the airplane and lightly applied the brakes. Suddenly, the left main landing gear collapsed, and the airplane swerved to the left. The airplane departed the runway surface and the left wing impacted a runway sign. Postaccident examination revealed that the left main landing gear actuator heim rod failed where the threads met the rod end; however, the rod was not made available for further examination, and the reason for the landing gear collapse could not be determined.

Probable Cause and Findings

The National Transportation Safety Board determines the probable cause(s) of this accident to be:
A collapse of the left main landing gear for reasons that could not be determined based on the available information.

Findings
Not determined (general) - Unknown/Not determined

Factual Information

On May 29, 2015, about 1542 mountain standard time, a Burr Express 2000 RG, N44508, experienced a landing gear collapse during the landing roll at Glendale Municipal Airport (GEU) in Glendale, Arizona. The private pilot and one passenger were uninjured, and the airplane sustained substantial damage to the rudder and elevators. The airplane was registered to, and operated by, the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed and no flight plan was filed. The flight departed from GEU at about 1500.

The pilot reported that he landed the airplane onto the runway normally. He applied beta thrust to decelerate the airplane and started to brake lightly. Suddenly, the left main landing gear collapsed and the airplane swerved to the left. The airplane departed the runway surface and the left wing impacted a runway sign. It traversed along the dirt when the right landing gear collapsed and the tail impacted the ground before sliding to a rest.

During a postaccident examination by a Federal Aviation Administration Inspector it was revealed that the left main landing gear actuator heim rod failed where the threads meet the rod end. Given the location of the heim rod, the inspector was unable to view the fracture surface while the component was installed on the airplane. In addition, the inspector noted that the hydraulic line to the gear actuator was ripped.

The National Transportation Safety Board Investigator-in-charge attempted to obtain the heim rod for further examination, however, the pilot had already repaired the airplane and the part was no longer available.

History of Flight

Landing-landing roll Landing gear collapse (Defining event)
Landing-landing roll Runway excursion

Pilot Information

Certificate: Private
Age: 68, Male
Airplane Rating(s): Single-engine land
Seat Occupied: Left
Other Aircraft Rating(s): None 
Restraint Used: 3-point
Instrument Rating(s): Airplane
Second Pilot Present: No
Instructor Rating(s): None
Toxicology Performed: No
Medical Certification: Class 3 With waivers/limitations 
Last FAA Medical Exam: November 22, 2013
Occupational Pilot: No 
Last Flight Review or Equivalent: February 1, 2008
Flight Time: (Estimated) 739 hours (Total, all aircraft), 40 hours (Total, this make and model), 600 hours (Pilot In Command, all aircraft), 1 hours (Last 90 days, all aircraft), 1 hours (Last 30 days, all aircraft)

Aircraft and Owner/Operator Information

Aircraft Make: BURR 
Registration: N44508
Model/Series: EXPRESS 2000 RG NO SERIES
Aircraft Category: Airplane
Year of Manufacture: 2008
Amateur Built: Yes
Airworthiness Certificate: Experimental (Special)
Serial Number: 0101RG
Landing Gear Type: Tricycle 
Seats: 4
Date/Type of Last Inspection: May 26, 2015 Annual 
Certified Max Gross Wt.: 3800 lbs
Time Since Last Inspection: 48 Hrs 
Engines: 1 Turbo prop
Airframe Total Time: 48 Hrs as of last inspection 
Engine Manufacturer: P & W Canada
ELT: Installed, not activated
Engine Model/Series: PT6A-20
Registered Owner:
Rated Power:
Operator: On file
Operating Certificate(s) Held: None

Meteorological Information and Flight Plan

Conditions at Accident Site: Visual (VMC)
Condition of Light: Day
Observation Facility, Elevation: GEU,1071 ft msl
Distance from Accident Site: 0 Nautical Miles
Observation Time: 15:45 Local
Direction from Accident Site:
Lowest Cloud Condition: Few / 10000 ft AGL
Visibility 20 miles
Lowest Ceiling: None
Visibility (RVR):
Wind Speed/Gusts: 3 knots /
Turbulence Type Forecast/Actual:  / None
Wind Direction: 210° 
Turbulence Severity Forecast/Actual:  / N/A
Altimeter Setting: 29.82 inches Hg
Temperature/Dew Point: 38°C / -7°C
Precipitation and Obscuration: No Obscuration; No Precipitation
Departure Point: Glendale, AZ (GEU)
Type of Flight Plan Filed: None
Destination: Glendale, AZ (GEU)
Type of Clearance: None
Departure Time: 15:00 Local 
Type of Airspace:

Airport Information

Airport: Glendale Municipal Airport GEU 
Runway Surface Type: Asphalt
Airport Elevation: 1071 ft msl 
Runway Surface Condition: Dry
Runway Used: 19 
IFR Approach: None
Runway Length/Width: 7150 ft / 100 ft
VFR Approach/Landing: Traffic pattern

Wreckage and Impact Information

Crew Injuries: 1 None 
Aircraft Damage: Substantial
Passenger Injuries: 1 None 
Aircraft Fire: None
Ground Injuries: N/A 
Aircraft Explosion: None
Total Injuries: 2 None
Latitude, Longitude: 33.522777,-112.290557 (est)

Navy pilots train for carrier landings using the Magic Carpet and praise the ride




Super Hornet jet pilots at Lemoore Naval Air Station have a new flight simulator that trains them to use a new flight guidance system for landing on aircraft carriers.

The Navy calls the new guidance system Precision Landing Mode.

But it was originally dubbed the “Magic Carpet,” short for (take a deep breath) Maritime Augmented Guidance with Integrated Controls for Carrier Approach and Recovery Precision Enabling Technologies, according to Naval Aviation News.

The media likes Magic Carpet because it has a nice ring to it.

Whatever it’s called, it will be the norm for carrier landings by 2019.

Pilots must train and get qualified. Lemoore has a trainer, as do the naval air stations at Whidbey Island in Washington and Oceana in Virginia.

Using software on each aircraft that controls flight control surfaces, including flaps, pilots can more easily adjust their landing approach, or glidepath, onto the moving aircraft carrier.

It works well, especially for night landings, said Lt. Brant Schmall, a pilot and landing signal officer at Lemoore. When onboard, he communicates with pilots as they land.

“I would say a large percentage of pilots are happy using it,” he said. “It is absolutely appreciated – the task level is reduced, and that’s helpful … the biggest thing is when you make an adjustment, there’s a near-instantaneous correction.”

Previously, pilots would also increase or decrease power, but now that’s set to be nearly constant.

To be clear, the pilot still flies the plane. It’s not automated flying, he said.

The new system promises safe, predictable landings and so far, the number of successful landings with no need for a second pass is going up, he said.

Precision Landing Mode was rolled out for all aircraft carriers in September, and Lemoore pilots in Carrier Wing 9 started using it on the USS John C. Stennis in November in the Pacific Ocean.

It’s also used by the EA-18 Growler, a Super Hornet version for electronic warfare. The new F-35C aircraft also has a similar system.

Original article can be found here:  http://www.fresnobee.com

Cessna 208B Super Cargomaster, FedEx Express, N989FX: Accident occurred February 24, 2015 at Baltimore/Washington International Thurgood Marshall Airport (BWI), Maryland

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

NTSB Identification: ERA15LA135 
Nonscheduled 14 CFR Part 135: Air Taxi & Commuter
Accident occurred Tuesday, February 24, 2015 in Baltimore, MD
Probable Cause Approval Date: 05/25/2017
Aircraft: CESSNA 208, registration: N989FX
Injuries: 1 Uninjured.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

The airline transport pilot was taxiing the airplane to the parking ramp after a night flight. As he approached a point where the taxiway intersected a service road, a ground service vehicle crossed in front of the airplane. To avoid a collision, the pilot applied the brakes and used reverse thrust, which stopped the airplane about 3 ft from the vehicle. The rapid application of braking and reverse thrust resulted in the airplane rocking backward and the empennage striking the ground, substantially damaging the airframe. The operator of the ground service vehicle reported that he was distracted while he attempted to retrieve a security badge and did not see the airplane as it approached the intersection. State law required that ground vehicles always yield right of way to taxiing aircraft. 

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The ground service vehicle operator's failure to yield right of way to the airplane due to distraction, which necessitated the pilot's use of reverse thrust and braking to avoid a collision and resulted in the airplane's empennage striking the ground.

The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entity:  
Federal Aviation Administration / Flight Standards District Office; Baltimore, Maryland 

Aviation Accident Factual Report - National Transportation Safety Board:  https://app.ntsb.gov/pdf

Docket And Docket Items - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

Federal Express Corp:   http://registry.faa.gov/N989FX

NTSB Identification: ERA15LA135
Nonscheduled 14 CFR Part 135: Air Taxi & Commuter
Accident occurred Tuesday, February 24, 2015 in Baltimore, MD
Aircraft: CESSNA 208, registration: N989FX
Injuries: 1 Uninjured.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On February 24, 2015, at 0612 eastern standard time, a Cessna 208B, N989FX, was substantially damaged when its empennage struck the ground while taxiing at Baltimore Washington International Airport (BWI), Baltimore, Maryland. The airline transport pilot was not injured. Night visual meteorological conditions prevailed, and an instrument flight rules flight plan was filed for the flight, which originated from Newark Liberty International (EWR), Newark, New Jersey and was destined for BWI. The on-demand cargo flight was conducted under the provisions of 14 Code of Federal Regulations Part 135.

Following an uneventful flight, the pilot landed the airplane on runway 33R, before exiting to the left onto taxiway J. He then continued to taxi to the southwest and transitioned onto taxiway AA. As the airplane approached the intersection of the taxiway and a service road, a ground service vehicle approached from the airplane's right. The pilot applied the airplane's brakes and full reverse thrust, and the airplane came to a stop. The ground service vehicle passed in front of the airplane at an estimated distance of between 2 and 3 feet, and the vehicle and the airplane did not collide.

The pilot stated that the "hard" braking and reverse thrust application caused the nose landing gear strut to compress, resulting in a "spring effect that was multiplied by removing reverse thrust rapidly." The airplane then pitched up and the empennage struck the ground, resulting in substantial damage to the airframe. The pilot reported that there were no pre-accident mechanical malfunctions or failures of the airplane's systems.

The operator of the ground service vehicle stated that he was proceeding to the security gate and was reaching down to grab an airport badge. The operator noticed the airplane when he looked up and immediately "slammed" on the brakes. The vehicle eventually came to a stop after crossing the taxiway.

Review of security camera video showed a sequence of events consistent with the statements provided by the pilot and the ground vehicle operator. Additionally, the airplane was taxiing with its landing lights, taxi lights, strobe lights, and rotating beacon lights on. The ground service vehicle's headlights, taillights, running lights, and a roof-mounted beacon were also on.

The 0554 weather conditions reported at BWI included 10 statute miles visibility and scattered clouds at 22,000 feet. The beginning of civil twilight occurred at 0620 and sunrise occurred at 0647. Moonrise occurred at 1024.

Code of Maryland Regulations 11.03.01.04 K(1) titled "Yielding the Right-of-Way" states "Any person operating a motor vehicle on the air operations area shall yield the right-of-way to aircraft in motion or aircraft with engines running, ready to be put in motion."

Group-owned jet use increases during Masters



More Masters Tournament patrons flew into town this year on their own planes – or at least, their “partly owned” planes.

Flexjet, a leading provider of fractionally owned private jets (think of a timeshare with wings), says business is up again this year at Augusta Regional Airport, where the roughly 3,000 private jets that descend on the Garden City during Masters Week account for nearly three-quarters of the airport’s entire private plane activity for the year.

This year’s tournament activity was a 3 percent increase over last year, Flexjet Sales Executive Christian McCracken said, adding that this year’s private jet turnout might have been the largest to date.

Fractional jet owners are (obviously) well-heeled individuals, but many are typically owned by small groups or corporations making the most out of their investment.

“In many cases, our owners will fly down several groups from differing locations through the span of competition to view the tournament, all on one set of passes,” McCracken said.

The Cleveland-based company’s hospitality lounge at the airport’s private jet terminal this year offered bourbon-tastings, a cigar bar, “locally sourced” hors d’oeuvres and a luxury candy buffet called the “Sweet Spot.”

You won’t find any of that in the main terminal, that’s for sure. And the best part? No Transportation Security Administration patdowns.

Original article can be found here: http://chronicle.augusta.com

North American T-6G Texan, SEJ Warbirds LLC, N3167G: Accident occurred April 08, 2017 at Culpeper Regional Airport (KCJR), Virginia

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

NTSB Identification: ERA17CA149
14 CFR Part 91: General Aviation
Accident occurred Saturday, April 08, 2017 in Culpepper, VA
Probable Cause Approval Date: 10/31/2017
Aircraft: NORTH AMERICAN T 6G, registration: N3167G
Injuries: 1 Serious, 1 Minor.

NTSB investigators used data provided by various entities, including, but not limited to, the Federal Aviation Administration and/or the operator and did not travel in support of this investigation to prepare this aircraft accident report.

The pilot stated that, after a thorough preflight inspection and passenger briefing, he started the engine and noted that there was an 80° left crosswind at 5 knots, gusting to 15 knots. He performed an engine run-up, checked the flight controls, and then departed to fly around the local area for about 20 minutes. He then returned to the departure airport, and because the airplane was only equipped with a single radio and there was traffic congestion, he did not monitor the weather or ask for a wind check. He performed a "high break" at traffic pattern altitude, and while on final approach with the flaps fully extended, he maintained a left-wing-low attitude to correct for the left crosswind. He performed a wheel landing, but as the tailwheel was lowering, the left wing raised "dramatically," and the right wingtip contacted the runway. He added power to abort the landing, but because the right wing was contacting the runway, the airplane pivoted to the right. The airplane went off the right side of the runway and nosed over. 

The pilot reported that there were no preimpact mechanical failures or malfunctions of the airframe or engine that would have precluded normal operation. The reported wind conditions about 5 minutes before the accident included a variable crosswind between 80° and 170° left of the selected runway heading at 8 knots, gusting to 16 knots.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot's failure to maintain airplane and directional control during the landing roll and subsequent go-around in gusting wind conditions.

Additional Participating Entity: Federal Aviation Administration / Flight Standards District Office; Herndon, Virginia

Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

SEJ Warbirds LLC: http://registry.faa.gov/N3167G

NTSB Identification: ERA17CA149
14 CFR Part 91: General Aviation
Accident occurred Saturday, April 08, 2017 in Culpepper, VA
Aircraft: NORTH AMERICAN T 6G, registration: N3167G
Injuries: 1 Serious, 1 Minor.

NTSB investigators used data provided by various entities, including, but not limited to, the Federal Aviation Administration and/or the operator and did not travel in support of this investigation to prepare this aircraft accident report.

The pilot stated that after a thorough preflight inspection and passenger briefing, he started the engine and noted that there was an 80° left crosswind at 5 kts, with gusts to 15 kts. He performed an engine run-up and checked the flight controls, then departed to fly around the local area for about 20 minutes. He then returned to the departure airport, and because the airplane was only equipped with a single radio and traffic congestion, he did not monitor the weather or ask for a wind check. He performed a "high break" at traffic pattern altitude and while on final approach with the flaps fully extended, he maintained a left wing low attitude to correct for the left crosswind. He performed a wheel landing, but as the tailwheel was lowering, the left wing raised "dramatically" and the right wingtip contacted the runway. He added power to abort the landing, but because the right wing was contacting the runway, the airplane pivoted to the right. The airplane went off the right side of the runway and nosed over. The pilot indicated there were no preimpact mechanical failures or malfunctions of the airframe or engine that would have precluded normal operation. The reported wind conditions about 5 minutes before the accident included a crosswind that was variable between 80° and 170° left of the selected runway heading, at a velocity of 8 kts, with gusts to 16kts.










Two men have been hospitalized after a small plane crashed Saturday afternoon at an airport in Culpeper County, Virginia, state police say.

About 1:40 p.m., the plane crashed at the Culpeper Regional Airport in Brandy Station, according to a spokesperson for Virginia State Police.

The single-engine 1949 North American T6G plane was attempting to land at the airport when it ran off the side of the runway and overturned, state police said.

Fifty-six-year-old Daniel Haug, of Culpeper, was flying the plane and 74-year-old John Reavis Jr. was riding as a passenger. Haug was taken to Culpeper Hospital and Reavis Jr. was flown to INOVA Fairfax Hospital, state police said. Their conditions are not known at this time.

Witnesses told News4 the crash happened during an event held by the Capital Wing of the Commemorative Air Force, a group that hosts airshows throughout the region.

Photos show a small yellow plane upside down on a grassy area. Video from the witness showed a medevac helicopter at the scene.

State police and the FAA are investigating.

Original article can be found here: http://www.nbcwashington.com



At 1:40 p.m. Saturday (April 8, 2017), Virginia State Police were notified of a plane crash that occurred at the Culpeper Regional Airport in Culpeper County.  The plane was a 1949 North American T6G, fixed-wing, single-engine, two seater aircraft.  

The aircraft was attempting to land at the airport when it ran off the side of the runway and overturned.  There were two occupants in the aircraft at the time of the crash, the pilot is identified as Daniel Allen Haug, age 56 of Culpeper, Virginia and passenger as John Reed Reavis Jr., age 74 of Bristow, Virginia.  The pilot was transported to Culpeper Hospital and the passenger was flown to INOVA Fairfax Hospital.

The Virginia State Police along with and FAA are investigating the incident to determine the causative factors that lead to the crash.

Original article can be found here: http://www.nbc29.com

The 74-year-old male passenger inside the plane that crashed at Culpeper Regional Airport Saturday afternoon was listed in serious condition at INOVA Fairfax Hospital on Monday, according to a hospital spokesman.

John Reed Reavis Jr., of Bristow, who was airlifted to the hospital, was seated in the rear of the North American T-6G Texan, a  plane often used to train Air Force pilots and in combat during the Korean and Vietnam wars.

The pilot Daniel Allen Haug, 56, of Culpeper was transported to Culpeper Medical Center, but was not listed as a patient Monday.

According to the Virginia State Police, Haug was attempting to land at the airport at about 1:40 p.m. when the plane ran off the side of the runway and overturned.

Haug served as chairman of the Culpeper AirFest committee last year and is a member of the Commemorative Air Force’s National Capital Squadron. His North American T-6G Texan has been a part of many ceremonial flyovers and historical displays.

In early October, Haug, along with three other pilots, flew over a charity golf fundraiser in a missing man formation to honor the late J.J. Quinn, a Culpeper pilot who donated many hours to the Angel Flight organization.

The state police and the Federal Aviation Administration are investigating the incident.

Virginia State Police say a plane with two occupants crashed at Culpeper Regional Airport on Saturday afternoon.

The plane was a 1949 North American TG6, fixed-wing, single-engine, two-seater aircraft.

Officials say the plane was trying to land when it ran off the runway and overturned.

The pilot was identified as Daniel Haug, 56, of Culpeper and the passenger was identified as John Reavis Jr., 74 of Bristow.

Both were taken to the hospital.

Virginia State Police and the FAA are investigating to determine the cause of the crash. 

CULPEPER COUNTY, Va. — State Police are investigating a small plane crash that left a pilot and his passenger injured Saturday afternoon.

Troopers were notified of the crash involving a 1949 North American T6G fixed-wing, single-engine, two seater aircraft around 1:45 p.m. The aircraft was attempting to land at the Culpeper Regional Airport when it ran off the side of the runway and overturned.

There were two occupants in the aircraft at the time of the crash. The pilot, 56-year-old Daniel Allen Haug of Culpeper County, was transported to Culpeper Hospital while his passenger, 74-year-old John Reed Reavis Jr. of Bristow, was flown to INOVA Fairfax Hospital.

The extent of their injuries is unknown.

The Virginia State Police are continuing to investigate the incident along with the FAA to determine the factors that lead to the crash.


Original article can be found here:   http://wtvr.com