Monday, August 31, 2015

Federal Aviation Administration warns six Miami towers could be too tall

The FAA notified developers of six high-rise towers in Miami in August that their proposed projects could be too tall, including two condo buildings by the Related Group.

The “notice of presumed hazard” letters are interim warnings and not final rulings. They’re based on the FAA’s initial findings that the towers could obstruct or have an adverse physical or electromagnetic effect on aircraft landing at Miami International Airport, which is west of downtown Miami.

The developers have 60 days to request that the FAA conduct further study and open for public comment, which could take an additional 120 days.

Miami-based Related Group got FAA letters on its Auberge Residences and Spa at 1400 Biscayne Blvd. and its unnamed residential/hotel tower at 444 Brickell Ave. The developer wanted Auberge to reach 530 feet and 444 Brickell to soar 635 feet, but the FAA recommended 445 feet and 465 feet, respectively.

Carlos Rosso, head of condo development at the Related Group, couldn’t immediately be reached for comment.

Florida East Coast Realty got an FAA warning for its 1201 Brickell Bay, proposed with 955 feet and 787 residences. Yet, the FAA said those plans should be cut to 489 feet. FECR VP Dean Warhaft said he's been in touch with the FAA reviewers and he's confident the high-end condo project will be approved at 995 feet tall.

"This is really not a big deal. It's part of the process," Warhaft said.

New York-based Chetrit Group’s CG Miami River wants its mixed-use project on the Miami River to rise 622 feet, but the FAA said it should be restricted to 421 feet. Located at Southwest 3rd Avenue between Southwest 5th Street and Southwest 6th Street, the project would have a mix of residential, hotel, retail and office space. Chetrit representatives could not be reached for comment.

Louis R. Montello’s Regalia Beach Developers, the same group that built the Regalia condominium in Sunny Isles Beach, plan to build a 969-foot-tall Regalia Biscayne at 340 Biscayne Blvd. The property, currently a hotel, is under contract to be sold to them. Yet, the FAA said the tower should be only 457 feet tall.

The Elysee Residences aims to be the tallest condo tower in Miami’s Edgewater neighborhood, but not if the FAA gets its way. Two Roads Development’s proposal for a 644-foot tower at 700 N.E. 23rd Street could be cut to 467 feet.

"We are aware, and were expecting, the FAA determination letter, which is a standard administrative notice and prerequisite to the commencement of the formal review process," Two Roads Development said in a statement. "Two Roads along with its counsel and consultants have been in continuous communication with the FAA administrator throughout the submission and are following the same protocols as we did with the Biscayne Beach application, which concluded with a determination of no hazard."

Executives for Regalia Beach Developers could not immediately be reached for comment.

It should be noted that the FAA’s findings are preliminary and further study could ease its height restrictions for these projects. Still, this is a reminder why Miami likely won’t have Dubai-style skyscrapers.

Original article can be found here: http://www.bizjournals.com

Asian Pilot Demand Lifts Flight Schools: Boeing says region’s carriers will need over 200,000 new pilots in next two decades




The Wall Street Journal
By DANIEL STACEY
Aug. 31, 2015 2:54 p.m. ET



SYDNEY—The outback Australian airstrips of Glenn Innes and Mangalore were built to repel potential Japanese invaders during World War II. Now, these runways and some near California’s wine country and in Arizona are looking to welcome droves of Asia’s student pilots.

These schools—some planned and some already operating—are aiming to tap the boom in commercial aviation in Asia, where a growing middle class with an itch to travel has made it the world’s largest market by annual passenger counts, according to the International Air Transport Association. But that surge has left carriers short of pilots, and safety concerns have underscored the need for good schools.

World-wide, the United Nations’ International Civil Aviation Organization says as many as 8,000 new students a year are needed at commercial flight schools to keep up with demand, primarily from Asia. Recent training-academy acquisitions indicate that establishing schools to accommodate those needs could cost more than US$3 billion. Training a pilot takes about a year, depending on the student’s aptitude.

Asia has few flight schools or instructors, and the U.S. and Australia are popular places to train cadets because of their strong safety records. Fatality rates per one million departures for large commercial passenger aircraft from 2009 through 2013 were 29.9 for Asia, and 1.2 for North America, according to the United Nations’ International Civil Aviation Organization.

The pilot training crisis is growing so acute that even manufacturers such as Boeing Co. and Airbus Group SE have begun calling for global action to develop more schools. Without new pilots, some of the 14,330 new planes Boeing predicts Asian airlines will need across the next 20 years won’t be able to be put into service, costing manufacturers billions in lost orders. In total, Boeing forecasts Asian airlines need 226,000 new pilots in the next two decades, more than North America, Europe and Africa combined.

Among the student pilots at the Australian Wings Academy, a school near the Gold Coast, is Kelvin Hsu, a 38-year-old former office worker from Taipei, Taiwan. He says that last year, after he quit his job and left his family to chase his dream of being a pilot, he chose the Australian school over an Asian one because he felt the best airlines would hire only those pilots trained overseas.

“I decided to come here to get a higher-quality pilot training,” he says, adding that he expects his job prospects are good. “By the end of my training there will be a huge pilot shortage.”

Despite the boom, however, it is tough to make a profit training pilots.

New colleges require fleets of aircraft, runway refurbishments and boarding houses. After that, operators still face the difficulty of getting contracts with airlines—a task that can be fickle because the business is cyclical. Many schools are small, training 100 students or fewer, making profitability a challenge.

School operators also complain that some students have fabricated English credentials, which can make training more time-consuming, because the instruction must begin at a more rudimentary level, and more costly, because full-time English tutors might be needed.

Phil Sweeney, who runs a pilot training academy in California’s Napa Valley, plans to double its student numbers to 400 in the next few years. But he adds that this isn’t likely to solve Asia’s pilot shortage because many other schools are struggling to stay open.

“It is a very risky area to get into,” says Mike Drinkall, general manager at the CAE Oxford Aviation Academy in the suburbs of the Australian city of Melbourne.

New schools are banking on scale to help them succeed, and looking to take over remote airports in the U.S. and the Australian outback to cut the costs often associated with training pilots at busy city airports.

CAE this year announced a rare deal to train as many as 650 China Eastern Airlines Corp. cadets during the next five years. CAE, a Canadian training firm, sold a 50% stake in its Melbourne school to China Eastern for an undisclosed sum as part of the deal to ensure the two parties shared this risk.

In Glenn Innes, a town in Australia’s New South Wales state once famed for tin and sapphire mines, a consortium known as Australia Asia Flight Training, led by airline veterans including the former deputy general manager of defunct national carrier Ansett Australia, reached a deal with the local council to take over the airport there.

The consortium is trying to raise about 25 million Australian dollars, or roughly US$18 million, to build the first stage of what could be the world’s largest pilot training facility, with the potential through further investment to train 1,000 new pilots each year. The students would mostly come from Asia, according to Neil Hansford, one of the businessmen behind the project. The school plans to seal contracts with airlines after its facilities are built, Mr. Hansford said.

In Kempsey, an old sawmilling town less than 200 kilometers away from Glenn Innes, Hainan Airlines Co., China’s biggest privately owned carrier and its fourth-largest in terms of fleet size, recently announced a plan to build a 300-cadet-per-year pilot academy at the small local airport.

China Southern Airlines Co., which has grown to become Asia’s largest carrier, already trains 250 cadets a year at a college in the Western Australian wheat farming town of Merreden, and roughly 100 more in a remote former military base in Mangalore near Australia’s southeastern seaboard.

New pilot training schools are also popping up across the U.S. In California’s Napa Valley wine district, Mr. Sweeney in 2014 reopened a training academy that had failed when it was operated by Japan Airlines Co., which spent roughly two years in bankruptcy protection starting in 2010, mainly because of its high debt combined with a slump in travel after the global financial crisis. Mr. Sweeney plans to rapidly ramp up capacity to keep costs down.

TransPac Aviation Academy at Deer Valley Airport near Phoenix has also been strengthening its relationship with Hainan Airlines, and now aims to train about 400 Chinese pilots each year.

Original article can be found here:  http://www.wsj.com

Cessna TTx T240, N452CS, H2 Aviation LLC: Accident occurred August 31, 2015 near West Houston Airport (KIWS), Harris County, Texas

National Transportation Safety Board - Aviation Accident Final Report: http://app.ntsb.gov/pdf

Docket And Docket Items -  National Transportation Safety Board:   http://dms.ntsb.gov/pubdms

Aviation Accident Data Summary  -  National Transportation Safety Board:   http://app.ntsb.gov/pdf

NTSB Identification: CEN15LA392
14 CFR Part 91: General Aviation
Accident occurred Monday, August 31, 2015 in Houston, TX
Probable Cause Approval Date: 03/14/2016
Aircraft: CESSNA T240, registration: N452CS
Injuries: 2 Uninjured.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

The flight instructor reported that, before the instructional flight with the private pilot began, the fuel tanks were filled to capacity and he visually checked the quantity of the fuel in the tanks during the preflight. The flight instructor reported that, after taking off and completing the instrument flight rules training procedures, they returned to the airport and performed three full-stop landings. During the final takeoff, as the airplane was about 300 ft above ground level, the engine experienced a total loss of power. The flight instructor took control of the airplane and subsequently conducted a forced landing to a field. The airplane landed, continued moving into trees, and then came to rest upright with the right main landing gear collapsed. 

A postaccident examination and three engine test runs were conducted, and no anomies were noted that would have precluded normal operation. The left fuel tank was found empty, and the right fuel tank contained about 25 gallons. Although the fuel selector valve was found in the “left off” position, it is likely that the left tank was selected during the accident flight and that the engine was starved of the available fuel.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The total loss of engine power due to fuel starvation, which resulted from the pilot’s inadequate fuel management and the flight instructor’s failure to verify the fuel level and fuel selector position in flight.

On August 31, 2015, about 1230 central daylight time, a Cessna T240 airplane, N452CS, made a forced landing after departure from the West Houston Airport (IWS), Houston, Texas. The flight instructor and private pilot receiving instruction were not injured. The airplane sustained substantial damage. The airplane was registered to H2 Aviation LLC and operated by the West Houston Airport under the provisions of 14 Code of Federal Regulations Part 91 as an instructional flight. Visual meteorological conditions prevailed and an instrument flight rules (IFR) flight plan was filed. The local flight was departing at the time of the accident. 

According to the flight instructor, they were conducting an instructional flight which included IFR training procedures. After the IFR training was completed, they returned to IWS and performed three full stop landings. On the final takeoff from IWS, they were about 300 ft above ground level when the engine experienced a total loss of power. The flight instructor took control and conducted a forced landing to a field beyond the departure end of the runway. The airplane landed and continued into trees where it came to rest upright with the right main landing gear collapsed. The instructor secured the airplane and called for assistance using a handheld radio. He reported that before the flight began, the fuel tanks were filled to capacity, which was 102 usable gallons. During the preflight inspection, the fuel quantity was verified and there were no contaminants observed. During the flight, both pilots switched the fuel selector in order to maintain fuel balance in the left and right tanks. Before the final takeoff, the fuel quantity gauges reportedly indicated 20 gallons on the left and 21 gallons on the right. Prior to the loss of power there were no digital or aural warnings noted from the crew-alerting system (CAS). He reported that the flight only lasted 1.81 hours and the average fuel consumption was 30 gallons per hour (gph); the airplane would have consumed about 54 of the 102 available gallons, leaving 48 gallons remaining. 

Several law enforcement officers arrived shortly after the accident and secured the scene. It was reported that fuel was leaking from the right wing fuel vent at the accident site. A plug was placed in the vent and no other fuel leakage was reportedly observed. The amount of fuel that leaked from the right tank was unknown. 

The responding Federal Aviation Administration (FAA) inspector reported that after the accident, the fuel selector knob was on the left OFF position and the emergency fuel pump was ON. The investigation could not determine when the emergency fuel pump was switched to ON. 

According to the FAA air traffic control (ATC) report, the airplane departed about 0953, the IFR flight plan was canceled at 1151 and the accident occurred about 39 minutes later. The flight was about 2.5 hours total. Using the pilot's average fuel consumption number (30 gph), the airplane would have consumed about 75 of the 102 available gallons, leaving 27 gallons remaining. 

On September 10, 2015, three engine test runs were conducted under the supervision of the Federal Aviation Administration (FAA) inspector. The Continental Motors engine remained attached to the airframe with no significant damage noted. The accident propeller had been replaced with another propeller for the test runs. The engine oil level was noted at 5 quarts. The airplane master switch was turned ON and the left fuel quantity gauge indicated 0 gallons, the right fuel quantity gauge indicated 25 gallons. All three test runs were conducted with the remaining fuel in the right tank. During the first engine run, the engine was warmed up at idle and a magneto check was completed in accordance with the checklist. No anomalies were noted. The engine power was then increased to 25 inches of mercury (in.hg) manifold pressure (MAP) and the engine was allowed to stabilize. The throttle was then advanced to the full forward position. Due to the condition of the engine mounts, it had been predetermined that after full power was reached the throttle would be reduced back to 25 in.hg MAP. As the throttle was reduced, a propeller pitch oscillation was noted. The engine was subsequently allowed to stabilize and cool down at idle before it was shut down in accordance with the checklist. Due to the pitch oscillation, a second engine run was conducted. During this run, a magneto check was again completed and the propeller was cycled. The engine was again advanced to maximum power. No propeller oscillation was heard during the throttle reduction. The engine power was set to 25 in.hg MAP and the electric boost pump was actuated. The engine subsequently experienced a total loss of power. A third engine run was conducted. With the engine at 25 in.hg MAP, the fuel selector was moved to the LEFT tank position; within one minute the engine experienced a total loss of power. The digital instruments and CAS functioned normally during the engine runs. The engine examination did not reveal any anomalies that would have precluded normal operation. 

As stated pilot's operating handbook, if the emergency fuel pump switch is switched to the ON position with the engine-driven fuel pump operating normally, total loss of engine power may occur. The engine manufacturer stated that when the engine is producing high power and the emergency fuel pump is ON, the engine can generally handle the extra fuel and the engine won't lose power. If the engine is at a lower power setting and the emergency fuel pump is ON, the engine is more likely to lose power.

http://registry.faa.gov/N452CS


NTSB Identification: CEN15LA392
14 CFR Part 91: General Aviation
Accident occurred Monday, August 31, 2015 in Houston, TX
Aircraft: CESSNA T240, registration: N452CS
Injuries: 2 Uninjured.

This is preliminary information, subject to chan
ge, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On August 31, 2015, about 1230 central daylight time, a Cessna T240 airplane, N452CS, made a forced landing after departure from the West Houston Airport (IWS), Houston, Texas. The flight instructor and private pilot under instruction were not injured. The airplane sustained substantial damage. The airplane was registered to H2 Aviation LLC and operated by the West Houston Airport as a 14 Code of Federal Regulations Part 91 instructional flight. Visual meteorological conditions prevailed and the flight was operated an in instrument flight rules (IFR) flight plan. The local flight was originating at the time of the accident. 

According to the flight instructor they were performing the last touch-and go landing. They had just departed from IWS and were about 200-300 ft. above the ground when the engine experienced a loss of power. The flight instructor conducted a forced landing into a field beyond the departure end of the runway. The airplane landed and continued into trees where it came to rest upright. 

The airplane has been retained for further examination.

FAA  Flight Standards District Office: FAA Houston FSDO-09






WEST HOUSTON (Covering Katy) – A Cessna TTx T240 airplane force landed in a section of Cullen Park near the runway of the West Houston Airport early Monday afternoon. There were no injuries according to Houston Police.

The plane crashed in a field designated as an “airport safety area” across the street from the airport runway, inside Cullen Park.

Houston Police say there were two men flying in the aircraft when it went down. A Texas State Trooper who was also on the scene told Covering Katy the men said their engine failed shortly after takeoff.

There was a small amount of debris in the field where the plane crashed. It came to rest against a small tree where the field ends and the brush and trees begin.

Investigators from the National Transportation Safety Board have been alerted and an investigator is expected to be at the scene later today.

The Westlake Fire Department also responded to the scene.





A small plane force landed Monday afternoon in a wooded area near West Houston Airport.

Harris County sheriff's deputies and Westlake Volunteer Fire Department firefighters responded to a location near the airport at 18000 Groschke Road in west Harris County.

The Texas Department of Public Safety said two men inside the plane were practicing a touch-and go landing when they experienced engine failure.

They were able to land the plane but it went off the runway.

Sky 2 aerials show the Cessna TTx T240 plane rested partially in some brush about 1/4 mile away from the airport runway.

DPS said no one was injured.

Lancair IVP, N864KM: Accident occurred August 30, 2015 near Fort Lauderdale Executive Airport (KFXE), Broward County, Florida

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

Analysis 

The pilot stated that, during the climb to cruise altitude, he noticed a loss of engine oil pressure. He declared an emergency with air traffic control (ATC) and requested to return to the airport. After ATC acknowledged, the pilot advised ATC that he lost all engine power and had to make an emergency landing. During the forced landing, the airplane collided with a ditch and was destroyed by postcrash fire. An examination of the engine revealed that it failed catastrophically, displaying signatures of lubrication distress; further, no measurable quantity of oil could be recovered from within the engine. Detailed examination of the engine's turbochargers revealed that one of the two units displayed evidence of burnt oil on the external surface and evidence of a foreign material in the unit's center housing, on the thrust bearing, and on the thrust collar. The foreign material was identified as polyethylene (plastic), similar to that used to protect the exposed orifices of the engine during shipment.

Review of maintenance records revealed that the pilot/mechanic had replaced both turbochargers with overhauled units two days before the accident flight. The turbocharger overhauler provided installation instructions and warnings that, in part, stated, "Remove all protective caps and plugs BEFORE installing this turbocharger." The foreign material discovered within the turbocharger's center housing suggests that the protective plastic cap at the oil outlet was likely not removed during the installation. It is likely that the turbocharger center housing filled with oil, which then flowed out of the engine via the turbocharger housing backplate, resulting in oil starvation and the subsequent total loss of engine power. 

Probable Cause and Findings

The National Transportation Safety Board determines the probable cause(s) of this accident to be: 

The mechanic's improper installation of the turbocharger assembly, which resulted in oil starvation and a subsequent total loss of the engine power.

Findings

Aircraft
Turbocharger - Incorrect service/maintenance (Cause)
Recip engine power section - Failure (Cause)

Personnel issues
Installation - Maintenance personnel (Cause)

Sonia and Ken McKenzie
~



The National Transportation Safety Board did not travel to the scene of this accident.

Additional Participating Entities:
Federal Aviation Administration / Flight Standards District Office; Orlando, Florida
Continental Motors; Mobile, Alabama 

Aviation Accident Factual Report - National Transportation Safety Board:  https://app.ntsb.gov/pdf


Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms




Ken McKenzie 
~

NTSB Identification: ERA15LA332
14 CFR Part 91: General Aviation
Accident occurred Sunday, August 30, 2015 in Fort Lauderdale, FL
Aircraft: LANCAIR IV, registration: N864KM
Injuries: 1 Serious, 1 Uninjured.

NTSB investigators may not have traveled in support of this investigation and used data provided by various sources to prepare this aircraft accident report.

On August 30, 2015, about 1055 eastern daylight time, an experimental amateur-built Lancair IV-P, N564KM, was destroyed by collision with terrain and a postcrash fire during a forced landing after takeoff from the Fort Lauderdale Executive Airport (FXE), Fort Lauderdale, Florida. The commercial pilot sustained serious injuries, and the passenger was not injured. The privately owned and operated airplane was operated under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual flight rules conditions were reported at the airport about the time of the accident, and an instrument flight rules flight plan had been filed for the flight destined for Lynchburg Regional Airport (LYH), Lynchburg, Virginia.

According to the pilot, during a climb to cruise he noticed that the engine's oil pressure dropped to 9 psi. He declared an emergency with air traffic control (ATC) due to the low oil pressure indication and requested to return to FXE. ATC provided radar vectors and cleared the airplane for the visual approach to runway 9. Shortly thereafter, the pilot contacted the FXE tower controller and reported an "engine failure." The pilot made a forced landing on a levee located 5 miles west of the approach end of runway 9. During the landing rollout, the airplane veered off the levee, collided with a ditch, and caught fire.

The airplane was recovered and the engine was retained for examination. During the examination of the engine puncture holes were discovered in both upper crankcase halves. Further examination revealed that no measurable amount oil could be drained from the engine. All of the spark plugs were removed and displayed a sooty appearance. The cylinders were removed and the cylinder attaching hardware torque and break away torque was checked and found within manufactures specifications; the No. 1, No. 2 and No. 3 pistons and cylinder skirts were damaged. The No. 1 piston exhibited signatures consistent with a valve strike on the dome. The oil sump was removed and contained pieces of connecting rod, rod bolts, rod bearing, and aluminum material in the bottom of the sump.

The crankcase was separated and the main bearings were not damaged. All of the bearing tabs were intact and no fretting was noted on the thru-bolt bosses. There was no evidence of bearing shift and the crankcase mating surfaces were machined. Puncture holes were also noted on bottom right crankcase half below the No. 1 cylinder. No obstructions were found in the crankcase oil galleries. Prior to removal, the camshaft was bent forward of the rear journal.

The crankshaft was removed and disassembled, the main journals had a normal operating appearance. The No. 1 connecting rod journal was found burnt and deformed. The No. 4 connecting rod journal was found burnt; the No. 2, No. 3, No. 5 and No. 6 connecting rod journals had a normal operating appearance. Examination of the connecting rod bearings revealed the No. 1 rod bearing was located in oil sump and found burnt and wiped. The No. 4 rod bearing was found burnt and wiped but was still contained within the rod and cap; No.2, No. 3, No. 5, and No.6 rod bearings indicated signs of lubrication distress.

The oil pump was disassembled and scoring was present in the internal oil pump housing and oil pump gear facing. Metal contamination was present in the oil relief valve. The oil filter was removed and opened for examination. The filter element exhibited metal contamination (aluminum & steel).

A visual examination of both turbochargers revealed one turbocharger had a normal grayish coloration on the internal turbine blades, while the other turbocharger was found blackend and oily on the turbine and compressor impeller blades.

The turbochargers were sent to Hartzell Engine Technologies for further examination and identified as urbo A (serial No. tKL01420), and turbo B (serial No. KFN00434). Examination of the turbo A revealed the turbocharger was overhauled by Main Turbo Systems. The turbocharger rotating assembly spun freely with no indication of compressor or turbine rub. Both the axial and radial end play was within specification. The turbocharger assembly was consistent with the design data and there was no evidence of mechanical malfunction. The internal lubrication passages were present with no indications of concern. The turbocharger was dry and displayed evidence of internal and external corrosion.

Examination of turbo B revealed that it was also overhauled by Main Turbo Systems. The turbocharger rotating assembly spun freely with no indication of compressor or turbine rub. Both the axial and radial end play was within specification. The turbocharger assembly was consistent with the design data and there was no evidence of mechanical malfunction. The internal lubrication passages were present with no indications of concern. There was evidence of foreign material in the center housing, on the thrust bearing, and on the thrust collar. Evidence of "burnt" oil was discovered on the external surfaces of turbocharger. The turbo was dissembled and it was revealed that oil residue was evident on the backside of the compressor wheel. Further examination also revealed oil residue on the turbo backplate.

A review of the engine logbook entries revealed that both turbochargers were removed and replaced by the pilot/mechanic with overhauled units two days prior to the accident flight. The entry in the logbook noted, "three engine test runs/operational checks and conducted leak check in accordance with SB no. 23, dated Feb 8, 2006. No leak/discrepancies noted at this time."

An examination of the foreign material located in the center housing of the turbo was conducted. The unknown material was examined using a Fourier Transform Infrared (FTIR) spectrometer with a diamond attenuated total reflectance (ATR) accessory in accordance to ASTM E1252-98 (American Society for Testing Materials E1252- 98). The spectrum was consistent with a straight-chained aliphatic hydrocarbon. A spectral library search found a very strong spectral match to polyethylene.

During the shipment of the turbochargers, polyethylene protective caps and plugs were used to plug the oil line openings. These protective caps and plugs must be removed before installation. The turbocharger overhauler provided instruction and warning tags with the units, one of which stated, "Remove all protective caps and plugs BEFORE installing this turbocharger."
============

 MIAMI (WSVN) -- A pilot recovering in the hospital is thanking God after his plane crash-landed in the Everglades.

Pilot Ken McKenzie told 7News that he credits his faith and his military experience for getting himself and his wife out just in time. "I opened the door, jumped out. Everything was engulfed in flames. I turned around and Sonia was working to get out of her seatbelt, so I grabbed a hold of her," he said.

He is expected to recover after several days at Jackson Memorial Hospital, but as he looks over at his wife, who only received a cut and bruises from the crash, he is simply grateful he was able to lead her to safety. Officials released the 911 call that was made during the landing. "It appears he has gone down about 11 miles North, Northwest," the caller said. "We don't know if he's in the road, or if he's in the Everglades or anything. We've lost contact with him."

McKenzie said that he is astonished how his training from the military instantly resurfaced. "With the time I spent in the Air Force, we did a lot of training on jet aircraft and how to get out of an aircraft on the ground," he said. "It was funny how all those thoughts came back."

As an experienced pilot, he described how his decades of aviation and service in the Canadian Armed Forces served him well. "He's lucky to not have more severe burns given the nature of the accident," said Dr. Carl Schulman, of Jackson Memorial Hospital's University of Miami Burn Center.

Schulman described McKenzie's second degree burns that cover up eight percent of his body as painful.

Still, the McKenzie family's faith has not faltered. "It's in the book of Isaiah, and it's about God's angels who will take care of the distress and that fire that surrounds you," said the pilot's wife, Sonia McKenzie.

McKenzie's eldest daughter, Monika McKenzie, who they were flying to visit in Virginia calls him her hero. "Even while he's laying in his hospital bed, and he's doing this for me, he's thinking about others," she said.

"When I look at all of what could have gone much worse than it did, I think we have a great deal of faith that there's a plan for our lives," McKenzie said.

Doctors said that McKenzie may be a perfect candidate for a stem cell trial that speeds the recovery process in burn patients only offered at this hospital.


MIAMI (WSVN) -- The pilot of a small plane is recovering in the hospital, hours after he and his wife crash-landed in the Everglades, off the Sawgrass Expressway, Sunday morning. 

Authorities said Ken McKenzie and his wife Sonia were heading to Lynchburg, Va. on board a Lancair IV-P when, shortly after takeoff from Fort Lauderdale Executive Airport, they ran into mechanical issues. "The pilot told his wife that they had engine problems with the oil pressure, and ultimately an engine failure," said Broward Sheriff's Office spokesperson Mike Jachles.

Faced with the certainty that the single engine aircraft was not going to stay airborne, McKenzie reportedly opted to head for an access road surrounded by mangroves and water near the Broward-Palm Beach County line, just before noon.

Witnesses fishing in the area said they were stunned by the commotion. "I see an ambulance coming down with lights on," said Julie Podmokly.

Officials released the 911 call made after the plane made its emergency landing. "He's in the Coral Springs vicinity. It appears he's gone down about 11 miles north-northwest," said the caller.

"How many souls on board?" asked the dispatcher.

"Two souls on board," responded the caller.

A thick black column of smoke helped rescue crews locate the couple. Dramatic photographs taken by the Coral Springs Fire Department captured the Lancair's charred remains. "The aircraft was completely destroyed by the flames. It's barely recognizable," said Coral Springs Fire Division Chief Mike Moser.

Jachles said McKenzie and his wife were injured, but they were able to exit the aircraft at the right time. "They were both really lucky to get out of the wreckage and sustain as minimal injuries as they did considering the impact," he said.

McKenzie was transported to Jackson Memorial Hospital, where he is spending his birthday Monday, receiving treatment for severe burns he sustained after the crash.

Sonia was airlifted to Broward Health North, where she was listed in good condition. She was later released and spoke to the media about the frightening flight. "Really, really odd. It was almost surreal, as if I was watching it in a movie," she said. "We just spun around really quickly, and he had already unlatched the door like you're supposed to on approaching an emergency landing, and he said, 'Sonia, we have to get out.' He went to jump out, I undid our seat belts I noticed his wasn't, and he ran out onto the wing."

Sonia continued, "As soon as we touched down, there was orange and red flames everywhere. He jumped out, reached back to grab my hand," she said.

Investigators said the pilot's professional experience may have helped prevent a tragic outcome. McKenzie, a father of two, is a dedicated Calvary Chapel board member who works for Airbus Group. He spent 14 years in the Canadian Armed Forces. "I think our faith in God just ... I knew we were gonna be OK. If it was gonna be our time, it was gonna be our time, and apparently it's not, so we're here for a little longer, and I think God has a purpose for our life," said Sonia.

The crash remains under investigation.

Story and video: http://www.wsvn.com


A day after a pilot suffered burns during a fiery crash landing in the Everglades, he remained hospitalized in stable condition while his wife and passenger in the single-engine aircraft was treated and released. 

Kenneth McKenzie, former chief operating officer of Spirit Airlines and Canadian Armed Forces pilot, marked his 53rd birthday Monday at Ryder Trauma Center in Miami.

After Sonia McKenzie's release from Broward Health North, she told reporters she remained "surprisingly calm" during the dramatic landing into a levee in the Everglades near the Broward-Palm Beach county line.

"We just spun around super quickly," Sonia McKenzie, 50, said. "As soon as we touched down there were orange and red flames everywhere."

A 911 call from Fort Lauderdale Executive Airport reporting that an airplane in the Coral Springs area had gone down came in at 10:44 a.m. Sunday.

"It appears he's gone down," the tower told the 911 dispatcher. "We don't know if he's in the road or if he's in the Everglades or anything, we've lost contact with him."

Shortly after the Fort Lauderdale couple departed the airport in a Lancair IV-P aircraft bound for Lynchburg, Va. they reported low oil pressure, authorities said.

The pilot told air traffic controllers he was unable to return to the airport and would attempt to land on a road near the Everglades, an FAA spokesman said.

Sonia McKenzie said that as they made their descent, her husband unlatched the door and told her: "'Sonia, we have to get out.'"

"It was almost surreal," she said, "like watching a movie."

After the plane went down, a thick column of black smoke rose into the air followed by gunshot-like explosions nearby anglers said.

Within minutes, a Broward Sheriff's Office helicopter landed a couple hundred feet from the burning aircraft. They were joined by Coral Springs firefighters who used foam and water to douse the flames.

The survivors were standing on the levee when firefighters arrived. The aircraft was completely destroyed.

Sonia McKenzie credited their survival to her husband's piloting experience and quick-thinking.

"I think God has a purpose for our life," she said.

Sunday, August 30, 2015

Business magnet: Spruce Creek Fly-In home to several aviation service firms

Pahan Ranasingha stands Monday in the hangar of his building at Avionics Installations at the Spruce Creek fly-In in Port Orange, Florida.
~



PORT ORANGE —With more than 600 flying machines based at the Spruce Creek Fly-In, it's no wonder several aircraft businesses choose to call it home.

With a 4,000-foot runway as the community's centerpiece and about 13 miles of taxiways leading to homes — some where you can almost slide out of the cockpit into your dining room — the gated community is one-of-a-kind and a natural fit to aviation businesses that have discovered the benefits of a home-grown customer base.

The land under the Port Orange-area community was originally a U.S. Naval Air Force training facility during World War II, but after the war ended the property was left vacant and it attracted vagrants and teenagers looking for a party spot.

A group of five investors became interested in the property back in the late 1960s and decided to purchase it in the mid-'70s with the intent to create an airplane-friendly community. Another developer, Jay Thompson of Thompson Properties, bought the Spruce Creek Fly-In when it was for sale in the late '80s.

Now, the once-abandoned air park has become a haven for what residents call "toy enthusiasts," and that concentrated interest makes for a business niche like no other.

IF YOU CAN'T BUILD OUT, BUILD UP

Pahan Ranasingha, owner of Avionics Installations Inc., opened up his firm in 1991 and works out of a Fly-In hangar on Cessna Boulevard.

Since that time, the firm's seven employees have had a constant stream of work at the two Fly-In commercial hangars he owns. So much so he was running out of space, but since the taxiways prevent a build-out, Ranasingha hired local contractor Mike Ceralosi to custom build an office inside the hangar that would still allow planes in.

Ceralosi came up with a design to make the office space at 212 Cessna Blvd. look like part of the fuselage of an old Boeing 747 Jumbo Jet and anchored it to the wall diagonally — 16 feet off the ground and out of the way of his employees.

Ranasingha, who incorporated his digital avionics, navigation and communication installation company in 1993, says being at the Fly-In has been the perfect location for him, in part because of his proximity to other aircraft machinists like Michael Collier, who operates an aircraft composite construction firm called Fibercraft in the Fly-In, across the taxiway from Avionics Installations.

A BUILT-IN CONSUMER BASE

Collier employs five workers who work with composite materials to build experimental aircraft, many of them one-of-a-kind. Case in point: one mock-up he and his crew designed included a fishing dock.

Collier started his business in Oregon in 1999. He relocated it to the Fly-In in 2012. The location just made sense, he said.

Most of my customers travel along the East Coast and the Fly-In is more convenient for them, he said.

In addition to building machines and kit planes from scratch and making body modifications, Collier has added inspections to the list of services offered. But before each of those inspections is made by Collier's company, Federal Aviation Administration rules state they have to be spick-and-span.

Enter Talon Rayne.

A ROLL OF THE DICE


Rayne started a detailing business in the Fly-In two years ago when he realized all aircraft had to be cleaned before each annual inspection and every 100 hours of flight as part of the FAA's maintenance and safety regulations. While there is no rule against cleaning your own plane, it's a time-consuming process, which gave Rayne the idea to open up shop in the community.

Rayne's company, Aerodyne Detail LLC, cleans, polishes and restores aircraft and business has been booming. His firm takes care of more than 150 aircraft on a revolving basis, but it didn't start out easy.

Rayne went to school to get his license to become an aircraft mechanic a few years back. Since it takes at least three years to become certified to do inspections on aircraft and his mechanic work wasn't exactly taking off, Rayne said he was keeping his eye out for other avenues to keep the bills paid and he came across the FAA inspection regulation. He said that was the catalyst for deciding the Fly-In would be his niche.

At the time, since money was pretty tight, getting into the community to start his business was a leap of faith.

"When I got there I didn't know anybody," Rayne said. "It was kind of a roll of the dice to get in there and really see if I could make the business successful."

But now that he's spent time in the Fly-In, "Now it's happening," Rayne said. "We get new customers every month. It just keeps growing and growing."

Commercial space or hangar space can be rented at the Spruce Creek Airport or you can be mobile. But while you don't have to own property within the super high-security community to do business there it certainly helps. Rayne says having that network surrounding him where he lives is the main reason his firm is so busy.

"We know each other more than the average community does," said Rayne, who said that while 90 percent of his detailing work is done within the confines of the community, the other 10 percent is done at large air shows like the National Championship Air Races in Reno, Nevada, and the EAA AirVenture in Oshkosh, Wisconsin, where he follows his clients.

"We're supporting people that are our neighbors," he said.

"Being inside Spruce Creek (Fly-In) really does lend a lot to your credibility," Rayne said.

On the other hand, "You've really got to bring your A-game if your going to be doing business in there," he said. "People will just basically ignore you if you're no good."

Rayne said he has customers bring him airplanes to detail from as far away as New Hampshire and considers that an honor and gauge of his success.

"If you're doing business and you're doing business well inside the Creek, then you're doing alright," he said.

Original article can be found here:  http://www.news-journalonline.com

As an air traffic controller in the 1990s, I had to close down the airport due to bird activity --Tri Ratina Manandhar, former director general of the Civil Aviation Authority Nepal

An official at the Tribhuvan International Airport aiming at a bird.
~


By TRI RATNA MANANDHAR 
August 30, 2015

On October 9, 1996, a Thai Airways Flight 312 bound for Bangkok narrowly escaped a major mishap when it slammed into a group of vultures during take-off from Tribhuvan International Airport (TIA). The Thai pilot acted very calmly and continued with the predetermined take-off procedure. Once the Airbus 330-600 had stabilized in the air, he turned around and made an emergency landing at the TIA. The jet was carrying 228 persons including the crew. The passengers were unharmed. However, five dead vultures were recovered from the impact site, and one of the aircraft’s engines was severely damaged, requiring it to be grounded for several days.  The incident was front-page news in The Kathmandu Post. ‘Thai jet survives major mishap’, the headline screamed. One American passenger named Matt Carpenter even got the entire crew to sign autographs on a copy of the newspaper.  

Adamant birds

Bird hazards are a constant threat at the TIA, especially from September to November. During those months, earthworms come out of the grass seeking warmth and die on the runway. This attracts vultures that come to feed on the abundant supply of earthworms. There used to be landfill sites, garbage dumps and uncontrolled commercial activities close to the runway which attracted birds, creating a great nuisance for flight operations. I was one of the air traffic controllers (ATC) on duty that day and I vividly remember the intense bird activities around the TIA. All the available techniques and resources had been deployed to scare away the birds, and helicopters were even requested to hover over the runway. The airport’s fire hoses were also used to drive them away. But the vultures were very adamant. They would fly a short distance before returning to the runway.

An Indian Airlines (IA) flight from Delhi was inbound even as the airport was encountering intense bird activities. The pilots opted to land despite the warnings of the ATCs. Fortunately, the landing was safe. After landing, the upset IA pilots requested us to get rid of them before their next flight. It was very unfortunate that they did not know about the ground team’s enormous efforts to keep the runway clear.  

Timid authorities

About half an hour after the IA flight landed, Thai Flight 312 requested clearance for takeoff. The ATC informed the pilots about the severe bird activities around the airport. Since Thai Airways was very particular about maintaining their schedule, they decided to depart in spite of the precarious bird activities. It was evident that the ATC was not comfortable with issuing a clearance to Flight 312. During such difficult circumstances, junior ATCs usually seek their supervisor’s help to deal with the situation. The supervisor had to take over and started giving authoritative instructions to the pilot though the airport was not closed.

Recalling that incident from almost 20 years ago and trying to figure out why the supervisor did not stop the Thai flight and left everything to the pilot, I think there were several reasons behind his decision. The first reason was obviously the dominant nature of Thai Airways and their link with the higher authorities. Second, the IA flight had landed safely just half an hour earlier. Third, and may be most importantly, there was no history of the airport being closed as a result of bird activity. In addition, the ATCs were known for their humility when dealing with pilots. As the investigators of the crash of PIA Flight 268 in 1992 had also noted, “Nepalese ATCs were timid and reluctant to intervene in what they saw as piloting matters.”

Setting a precedent

A year after the Thai incident, I was working as the supervisor at the control tower. There was high level of bird activities around the TIA, and I was feeling a bit apprehensive as I recalled the Thai incident. As usual, all the efforts to scare away the birds failed. In the meantime, there was an Aeroflot flight inbound from Moscow. The Aeroflot aircraft was informed well in advance about the hazardous bird activities at the TIA. The ground team was struggling hard to shoo away the birds before the plane arrived, but all their efforts were in vain and bird activities became even more intense. They reached an alarmingly critical level as the Aeroflot flight was nearing Kathmandu.

I consulted my seniors about closing down the airport, but no one wanted to be involved in taking such a decision. Ultimately, I took the unprecedented action of closing down the airport. The Aeroflot jet circled over Kathmandu for a few minutes and then headed for Delhi as there was no sign of improvement. The next day, the Aeroflot flight landed in Kathmandu with its Delhi-based senior executive officer on board. As soon as the aircraft landed, he headed straight to the general manager of the TIA to submit a formal letter asking for compensation for the loss caused by the flight’s diversion. I was immediately summoned by the general manager and asked to explain my actions. I had a very tough time convincing them as nobody made an attempt to understand the real circumstances. I did feel very sorry for closing the airport. However, my decision had been right and it set a precedent.

Over the last several years, there have been significant improvements in the TIA’s Air Traffic Control system. The Licensing and Rating system has been introduced and the ATCs are paid a fair compensation in terms of Rating Allowance and Stress Allowance. All those positive changes have helped to improve the confidence and morale of ATCs. Most importantly, as far as safety is concerned, ATCs have high professional confidence and do not hesitate to intervene and use their authority when the situation warrants it. Bird strike problems at airports are universal in nature and not unique to the TIA. Even though every possible technique is employed to prevent bird strikes, a number of incidents are reported every year.

Manandhar is a former director general of the Civil Aviation Authority Nepal

Original article can be found here: http://kathmandupost.ekantipur.com

Cirrus SR22, N765CD: Fatal accident occurred August 30, 2015 near Kewanee Municipal Airport (KEZI), Henry County, Illinois

Aviation Accident Final Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

NTSB Identification: CEN15FA388
14 CFR Part 91: General Aviation
Accident occurred Sunday, August 30, 2015 in Kewanee, IL
Probable Cause Approval Date: 09/18/2017
Aircraft: CIRRUS DESIGN CORP SR22, registration: N765CD
Injuries: 2 Fatal, 1 Serious.

NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

The instrument-rated private pilot and two passengers departed on an instrument flight rules flight plan in low instrument meteorological conditions (IMC), including fog and cloud ceilings at 200 ft above ground level. Before takeoff, the pilot announced on the airport's common traffic advisory frequency that the airplane was departing runway 19; however, the airplane departed runway 27. Radar data indicated that the airplane made 3 nearly 360° left turns in close succession just before ground impact. The airplane's altitude during the turns varied between 1,200 ft and 1,800 ft msl. Examination of the airframe and engine did not reveal any anomalies that would have precluded normal operation, and data retrieved from onboard engine monitoring equipment indicated that the engine was operating normally throughout the flight. 

Conditions conducive to the development of spatial disorientation existed at the time of the accident, including restricted visibility, entry into IMC, and maneuvering for an assigned course after takeoff. It could not be determined whether the pilot recognized his error in departing from the incorrect runway, but it is possible that this error presented the pilot with an operational distraction about the time the airplane was entering IMC, and could have precipitated the pilot's spatial disorientation. Additionally, the pilot had reported to the airplane's co-owner the day before the accident that the airplane's autopilot was inoperative and that he did not plan to use it. Thus, the pilot did not have the autopilot available to help manage his workload during the flight. The radar depiction of the accident flight path was consistent with the known effects of spatial disorientation, and it is likely that the pilot became disoriented shortly after entering IMC after takeoff.

The National Transportation Safety Board determines the probable cause(s) of this accident as follows:
The pilot's loss of control due to spatial disorientation shortly after takeoff into low instrument meteorological conditions.


Steven Mark Murray 

Mark Haydn Murray 


The National Transportation Safety Board traveled to the scene of this accident.

Additional Participating Entities:
Federal Aviation Administration / Flight Standards District Office; DuPage, Illinois
Continental Motors; Mobile, Alabama
Cirrus Aircraft; Duluth, Minnesota

Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

Investigation Docket - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

http://registry.faa.gov/N765CD





NTSB Identification: CEN15FA388 
14 CFR Part 91: General Aviation
Accident occurred Sunday, August 30, 2015 in Kewanee, IL
Aircraft: CIRRUS DESIGN CORP SR22, registration: N765CD
Injuries: 2 Fatal, 1 Serious.

NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

HISTORY OF FLIGHT

On August 30, 2015, about 0918 central standard time, a Cirrus SR22 airplane, N765CD, was destroyed when it collided with terrain shortly after takeoff from Kewanee Municipal Airport (EZI), Kewanee, Illinois. The private pilot and one passenger were fatally injured; the second passenger sustained serious injuries. The airplane was privately owned, and the personal flight was operated under the provisions of 14 Code of Federal Regulations Part 91. Instrument meteorological conditions prevailed throughout the area, and an instrument flight rules (IFR) flight plan was filed for the cross-country flight, with an intended destination of Hot Springs, Arkansas.

A family member drove the pilot and passengers to EZI at 0745. During the short drive, the pilot discussed the fact that the airplane's autopilot had stopped working during the flight to EZI a few days before. The pilot thought that this would make the trip a little harder but that it was not a critical system preventing his departure. The pilot said that he initially planned to fly under the clouds then climb above the clouds to his desired cruise altitude of 11,000 ft. Upon arriving at the airport, the pilot decided to delay the flight due to the amount of fog in the area. The pilot and passengers subsequently returned to the airport about 0900 for departure. 

There were no witnesses to the accident and no distress calls were broadcast via radio. According to Flight Service, the pilot called before takeoff to file an IFR flight plan. He was given clearance to take off with a void time of ten minutes to activate the flight plan. The airport manager reported that the pilot taxied for takeoff on runway 27; however, the pilot's radio calls indicated that he thought he was using runway 19. After an aborted takeoff, the pilot completed a back-taxi on runway 27, but again his radio calls were for runway 19. The airplane subsequently departed runway 27. 

The surviving passenger, who was seated in the left rear seat, stated that the aborted takeoff was due to an open door. After securing the door, the airplane subsequently departed. She stated that when the airplane took off, it went quickly into the clouds. She stated that it did not feel as if the airplane was "going up." She stated that she heard a discussion between the pilot and then passenger seated in the front seat: the front seat passenger had reached for the activation handle for the airframe parachute system, and the pilot stated that the airplane was "too low." She then saw the ground approaching, and the impact occurred.

According to radar data obtained from the Federal Aviation Administration (FAA) Quad City Terminal Radar Approach Control facility, identified targets corresponded with the accident airplane's assigned transponder code. Additionally, five subsequent primary targets were consistent with the track of the accident airplane. There were no other aircraft operating in the immediate vicinity. The radar data corresponding to the airplane's transponder code began at 0914:53 at a Mode C reported altitude of 1,500 ft after the airplane departed EZI. The target continued in a left turn to the west and south and climbed to an altitude of 1,800 ft before beginning a descent to 1,200 ft. That data ended, and the primary radar returns consistent with the accident airplane begin at 0915:37 and continued until the last associated target at 0916:35 and an altitude of 1,600 ft. EZI airport elevation was 858 ft. A flight path superimposed between the primary targets suggested that the pilot made three nearly 360° left turns in close succession before impacting the ground. See figure 1.

PERSONNEL INFORMATION

The pilot held a private pilot certificate with ratings for airplane single-engine land and instrument airplane. His most recent FAA third-class medical certificate was issued on August 14, 2014. Review of the pilot's logbooks indicated a total flight experience of 922 hours of which 37 hours were in the accident airplane make and model. The pilot completed a Cirrus Advanced Transitional Instrument Training Course in May 2015. The pilot had logged 130 hours of actual instrument flight experience and 94.1 hours of simulated instrument experience. In the 90 days before the accident, the pilot logged 3.1 hours simulated instrument experience and 4.8 hours actual instrument experience, all of which were in the accident airplane make and model. 

AIRCRAFT INFORMATION

The airplane's most recent annual inspection was completed on March 5, 2015, at a Hobbs meter time of 1,635.1 hours. On June 25, 2015, at a Hobbs time of 1,635.2 hours, a new Engine Data Management System was installed. The aircraft logbook included an entry stating that the Cirrus Airframe Parachute System (CAPS) was replaced on October 4, 2011, at a Hobbs time of 1,134.2 hours. At the time of the accident, the Hobbs time was 1,734.8 hours.

The co-owner of the airplane reported that he had flown the airplane 9 days before the accident. He reported that there were no problems with the aileron trim or the autopilot. He flew using GPS navigation and with the autopilot engaged for the entire flight. The 5.4-hour flight had 3 occupants onboard with 50 pounds of baggage. He also stated that he had talked to the accident pilot the morning before the accident. The pilot told him that the autopilot would hold altitude, but it would not hold the horizontal situation indicator (HSI) heading bug or the GPS. The pilot also told him that the trim on the sidestick was not working and that he could hold straight and level flight with a bit of right aileron. The co-owner and pilot agreed to have the trim looked at upon his return flight.

A family member reported that he and the pilot had flown the airplane on a local flight from EZI for about 15-20 minutes on the morning before the accident. He reported that the flight was normal and that they did not experience any problems.

METEOROLOGICAL INFORMATION

First responders reported foggy conditions and low cloud ceilings about the time of the accident. 

EZI listed no official weather reporting capability; however, an unofficial weather station was collocated at EZI and reported the following conditions at 0910: wind from 090° at 1 knot, temperature 18.9°C, dew point 18°C, relative humidity 99%, altimeter 30.11 inches of mercury (Hg). Visibility and sky conditions were not reported.

The closest reporting station to the accident site was from Galesburg Municipal Airport (GBG), Galesburg, Illinois, located 28 miles southwest of the accident site at an elevation of 764 ft. The airport had an Automated Weather Observation System (AWOS), which issued observations every 20 minutes. The 0915 observation included: calm wind, visibility 1 miles in mist, ceiling overcast at 200 ft, temperature and dew point 19°C, altimeter 30.09 inches of Hg. 

A review of the observations for the day indicated that IFR conditions were reported as early as 2215 the previous evening, with low ceilings and visibility in fog and mist continuing through the time of the accident, and clearing by 1115. A weather study was completed by a NTSB staff meteorologist and is referenced in the public docket to this report.

WRECKAGE AND IMPACT INFORMATION

Examinations of the airframe and engine were accomplished at the accident site and a secured hangar located at the Kewanee Airport.

The accident occurred in a planted soybean field, about 1.5 miles west of the Kewanee airport. The airplane impacted terrain in an approximate 45° nose-down, right-wing-low attitude on a heading of about 130-140°. The debris field extended to the east about 260 ft from the initial point of impact on a headings from 080 to 110°. The main wreckage came to rest on a heading about 190°.

An examination of the ground impact scars and debris path showed that the tip of the right wing struck the ground at the western end of the debris field. The scar from the right wing tip was the initial point of impact. Propeller cuts, dirt clumps, and an impact depression were noted in the soft soil about 38 to 45 ft from the initial impact point. The separated propeller was located at 55 ft, and the right cabin door was located at 65 ft. The tip of the right wing and aileron were at 67 ft. The upper engine cowling was at 72 ft and the lower engine cowling was at 78 ft. The CAPS enclosure cover was at 75 ft. The left cabin door was at 120 ft, the main wreckage was at 160 ft, and the engine was at 185 ft. The parachute was stretched out on a heading of 110° to about 240 ft. The CAPS D-Bag and rocket motor were at 260 ft.

Fuselage

The fuselage was mostly destroyed by impact forces. The lower forward fuselage was crushed up and aft. The firewall was separated from the fuselage and the upper engine cowling was separated from the fuselage. The right forward corner of the upper engine cowling was crushed aft about 25°. The lower left and right engine cowlings were fractured into several pieces. The forward fuselage was fractured and crushed aft. The spar cover was separated from the fuselage. Both front seats remained attached to the spar cover. The rear section of the cabin floor was separated from the fuselage and the rear seats remained attached to it.

Wing

The wing was mostly destroyed by impact forces, and the wing spar was fractured in multiple places. All upper and lower wing skins were separated from the wing spar. The left and right flaps were separated from the wing. The right aileron was separated from the wing, and the left aileron remained attached to the wing. Aileron control cable continuity was confirmed. The roll trim motor shaft was found fractured. The fractured end of the roll trim motor shaft remained attached to the roll trim cartridge. The roll trim cartridge remained attached to the left aileron actuation pulley. Two rub marks were located adjacent to the roll trim motor mounting location. One rub mark was on the roll trim motor access panel, and one rub mark was on the lower wing skin. It could not be determined when the rub marks occurred. The flap actuator was separated from the flap torque tube. The flap actuator shaft was located in a position extending approximately 2 inches, consistent with a "Flaps 50" position. 

Empennage/Stabilizers

The empennage was separated from the fuselage about 1 ft forward of the leading edge of the horizontal stabilizer. The rudder remained attached to the vertical stabilizer and rudder control cable continuity was confirmed. The right elevator remained attached to the horizontal stabilizer and the right elevator tip exhibited impact damage. The left elevator remained attached to the horizontal stabilizer and the left elevator tip was separated from the elevator. Elevator control cable continuity was confirmed. The pitch trim motor was in an approximate neutral position.

Landing Gear

The nose landing gear assembly was buckled aft under the engine. The nose landing gear upper weldment remained attached to the engine mount. The nose landing gear leg, tire and wheel assembly was separated from the nose landing gear upper weldment. Both the left and right main landing gear assemblies exhibited impact damage. Both main landing gear assemblies remained attached to the wing.

Doors

The right and left cabin doors were separated from the fuselage. Both door's upper and lower pins exhibited impact damage. The baggage door remained attached to the fuselage.

Cockpit 

The instrument panel exhibited impact damage and was separated into two sections. The center console exhibited impact damage. The center console was equipped with a Garmin GMA 340 Nav/Com, dual Garmin GNS 430's, S-TEC 55X autopilot, and a Garmin GTX 327 transponder. The ignition key remained in the ignition switch and the ignition switch was in the "Both" position. The bolster panel in front of the left crew seat was modified with a JPI Engine Data Management System. The instrument panel in front of the right crew seat was modified to accept a Garmin GPS map 696, which was installed.

The following settings, indications and switch positions were noted:

• Hobbs meter indicated 1,734.8 hours.

• Altimeter's Kollsman window indicated a setting of 30.01. 

• Flap switch was in the flaps "100" position.

• GPS #2 circuit breaker was in the "open" position. 

• Encoder/transponder circuit breaker was in the open position. 

• MFD circuit breaker was "zip-tied" in the "open" position. 

• Strobe and landing light switches were in the "on" position. 

• Strobe lights circuit breaker was in the "open" position. 

• Battery #2 circuit breaker was in the open position. 

• Battery #1, Alternator #1 and Alternator #2 master switches were in the "on" position. 

Seats and Restraints

Both front seats remained attached to the spar cover. First responders cut the left seat belt webbing to aid in the extraction of the left seat occupant. The separated left seat belt remained buckled together. The right seat belt was found unbuckled. The right seat belt webbing exhibited load damage. The right seat belt webbing was torn and partially pulled through the load bar. The left rear seat belt remained buckled together. The left rear seat belt webbing exhibited load damage and was crushed and gathered against the load bar.

Cirrus Airframe Parachute System (CAPS)

The forward section of the roof and the windscreen were separated from the fuselage. Impact damage was noted on the roof structure directly above and adjacent to the mounting location of the CAPS activation handle and holder. The CAPS activation handle was found out of the activation handle holder. The activation handle holder bracket was bent aft. Impact damage was noted on the activation handle and on the exposed activation cable. The CAPS safety pin was located on the ground under the main wreckage.

The CAPS was found deployed and the CAPS rocket motor propellant was expended. The CAPS rocket motor, rocket lanyards, incremental bridle, D-Bag, suspension lines, riser, rear harnesses and both front harnesses had been extracted from the airplane. The rear harness remained snubbed. Both reefing line cutters remained in place and both had been activated. The parachute was separated from the D-Bag and was found stretched out from the main wreckage on a heading about 110°. The slider was at the base of the canopy. Packing folds were present on the canopy.

The rocket motor, lanyards, incremental bridle and D-Bag were located approximately 20 ft beyond the end the parachute. The CAPS launch tube, rocket igniter, exhaust shield, and base remained attached to the bulkhead. The retention straps for the D-Bag remained in the enclosure compartment. The CAPS access panel (#CB7) exhibited impact transfer marks from the left front harness 3-point link. The CAPS enclosure cover was located approximately 20 ft south of the debris path at a point about 75 ft from the right wing tip ground scar. An impact transfer mark, consistent in size and dimension with the top of the CAPS rocket motor, was noted on the inside surface of the cover, on the "strike plate."

On-site observations of the CAPS system showed that the system was not activated in flight. All evidence correlated to a CAPS deployment as the result of impact forces. 

Engine 

The crankshaft propeller flange was fractured and remained attached to the propeller hub. All of the cylinders remained attached to the crankcase and exhibited impact damage. All damage observed was consistent with impact. The fractured crankshaft propeller flange and radii exhibited 45° shear lips and spiral cracking. The exhaust and induction systems exhibited impact damage.

Both magnetos remained attached to the engine. Rotation of the engine by hand through the accessory drive produced impulse coupling engagement from both magnetos. The magnetos produced spark on the top spark plug leads for cylinder Nos. 2, 4, 5 and 6. The ignition harness was severed at the magneto due to impact damage, which contributed to the lack of spark from the top leads of cylinder Nos. 1 and 3. The ignition harness exhibited impact and thermal damage, and some leads were found cut and severed. The top spark plugs exhibited light- and dark-colored combustion deposits and the electrodes exhibited normal wear. The bottom spark plugs were inspected using a lighted borescope and exhibited normal operating signatures.

The fuel pump remained attached to the engine and was removed. The drive coupling was intact and the pump turned freely by hand. The mixture control arm moved freely by hand from stop to stop. The fuel pump was disassembled with no anomalies noted. The fuel manifold valve was removed from the engine and disassembled. The screen was free of debris. A small amount of fuel was observed in the manifold valve cavity. The diaphragm and plunger were intact and the retaining nut was tight. The fuel injector lines exhibited impact damage. The fuel injector nozzles from all cylinders except cylinder No. 2 were removed and free of obstructions. The No. 1 cylinder fuel nozzle was slightly bent. The fuel nozzle for cylinder No. 2 could not be removed due to impact damage.

The throttle body remained attached to the engine and exhibited impact damage. The control arm moved freely by hand from stop to stop. 

The oil sump was crushed upward into the crankcase and breached. The oil pump was disassembled and the drive and driven gears showed no anomalies and were coated with oil. The oil pump cavity contained oil and exhibited no hard particle passage. The oil cooler remained attached to the engine and exhibited impact damage.

The cylinders exhibited impact damage to their respective fins and some valve covers. The top spark plugs were removed and the cylinders were examined with a lighted borescope. The combustion chambers contained light-colored combustion deposits. The engine was rotated by hand through the accessory drive, and thumb compression was obtained on all cylinders except cylinder No. 1. A second borescope inspection of cylinder No. 1 revealed dirt and debris from impact located around the exhaust valve seat, preventing full closure of the exhaust valve. The engine was rotated again and proper operation of the No. 1 cylinder valve was visually observed with the borescope. The starter was found in the debris field, fractured and free of the starter adaptor. 

Propeller Assembly

The three-blade propeller was separated from the engine and located in the wreckage debris field. The spinner exhibited rotational crushing. Two blades were relatively straight and displayed chordwise scratching. The third blade was bent aft approximately midway from the hub to the tip and exhibited chordwise scratches and nicks in the leading edge. Several propeller slash marks were noted in the debris field. The propeller governor remained attached and was removed for inspection. The control arm moved freely by hand from stop to stop. The drive rotated freely by hand and oil discharged from the governor. The governor's gasket screen was free of debris.

MEDICAL AND PATHOLOGICAL INFORMATION

The Henry County Coroner Office, Cambridge, Illinois, performed an autopsy of the pilot. The cause of death was listed as "Multiple Blunt Injuries."

Toxicological testing on specimens of the pilot was performed by the FAA Bioaeronautical Sciences Research Laboratory, Oklahoma City, Oklahoma. Testing for carbon monoxide, ethanol, and drugs were all negative.

TESTS AND RESEARCH

Recorded Data

The airplane was equipped with a Garmin 696 GPS MAP and a JPI EDM 900 Engine Monitoring System. The Garmin 696 was impact damaged and no data was extracted.

The JPI EDM 900 was viable and data were downloaded. The data extracted included 71 logs from June 26, 2015 through August 30, 2015. The log for the accident flight began at 09:12:38 CDT and ended at 09:14:43 CDT. Additionally, data from four previous flights were reviewed. All recorded logs showed normal engine operation.



NTSB Identification: CEN15FA388 
14 CFR Part 91: General Aviation
Accident occurred Sunday, August 30, 2015 in Kewanee, IL
Aircraft: CIRRUS DESIGN CORP SR22, registration: N765CD
Injuries: 2 Fatal, 1 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

On August 30, 2015, about 0918 central standard time, a Cirrus SR22 airplane, N765CD, registered to private individuals, collided with terrain shortly after takeoff from the Kewanee Municipal Airport (EZI), Kewanee, Illinois. Of the three occupants, the private pilot and 1 passenger sustained fatal injuries and 1 passenger sustained serious injuries. The flight was being conducted under the provisions of Federal Code of Regulations Part 91. Instrument meteorological conditions prevailed throughout the area of the accident and an IFR flight plan was placed on file with a 10 minute void time prior to takeoff. The flight was originating from EZI with an intended destination of Hot Springs, Arkansas.

There were no direct witnesses to the accident and no distress calls were received. According to Flight Service, the pilot called prior to takeoff to file an IFR flight plan. He was given clearance to takeoff with a void time of ten minutes to activate the flight plan. Local residents reported foggy conditions and low cloud ceilings about the time of the accident. The surviving passenger who was seated in the rear seat reported that the airplane took off, went quickly into the clouds. She stated that it did not feel as if the airplane was "going up." She looked up, saw the ground approaching, and the impact occurred. 

The accident occurred in a planted soybean field, approximately 1.5 miles west of the Kewanee airport. The wreckage was located at a position approximately 0.5 miles west of the intersection of North 400th Avenue and East 2250th Street and approximately 250 feet south of the North 400th Avenue.

An examination of the main impact site and energy debris path revealed that the airplane impacted terrain in an approximate 45 degree nose down, right wing low attitude, on a heading of approximately 130 to 140 degrees. The debris field extended to the east approximately 260 feet from the initial point-of-impact on a heading from 080 degrees to 110 degrees. The main wreckage came to rest on a heading of approximately 190 degrees.

An examination of the impact scars and wreckage debris revealed that the right wing tip struck the terrain at the western end of the debris field. The right wing tip scar was the initial point-of-impact. All subsequent debris measurements are approximate from this point. Propeller cuts, dirt clumps and an impact depression were noted in the soft soil from 38 feet to 45 feet. The separated propeller was located at 55 feet. The right cabin door was located at 65 feet. The right wing tip and aileron was at 67 feet. The upper engine cowling was at 72 feet. The CAPS enclosure cover was at 75 feet. The lower engine cowling was at 78 feet. The left cabin door was at 120 feet. The main wreckage was at 160 feet. The engine was at 185 feet. The parachute was stretched out on a heading of 110 degrees to approximately 240 feet. The CAPS D-Bag and rocket motor was at 260 feet.

The forward section of the roof and the windshield were separated from the fuselage. Impact damage was noted on the roof structure directly above and adjacent to the mounting location of the CAPS activation handle and holder. The CAPS activation handle was found out of the activation handle holder. The activation handle holder bracket was bent aft. Impact damage was noted on the activation handle and on the exposed activation cable. CAPS safety pin was located on the ground under the main wreckage. 

The CAPS was found deployed and the CAPS rocket motor propellant was expended. The CAPS rocket motor, rocket lanyards, incremental bridal, D-Bag, suspension lines, riser, rear harnesses and both front harnesses had been extracted from the aircraft. The rear harness remained snubbed. Both reefing line cutters remained in place and both had been activated. The parachute was separated from the D-Bag and was found stretched out from the main wreckage on a heading of approximately 110 degrees. The slider was at the base of the canopy. Packing folds were present on the canopy. 

The rocket motor, lanyards, incremental bridal and D-Bag were located approximately 20 feet beyond the end of stretched out parachute. The CAPS launch tube, rocket igniter, exhaust shield, and base, remained attached to FS 222 Bulkhead. The retention straps for the D-Bag remained in the enclosure compartment. The CAPS access panel (#CB7) exhibited Impact transfer marks from the left front harnesses 3-point link. The CAPS enclosure cover was located approximately 20 feet south of the debris path at a point approximately 75 feet from the right wing tip ground scar. An impact transfer mark, consistent in size and dimension to the top of the CAPS rocker motor, was noted on the inside surface of the cover, on the "strike plate." 

On site observations of the CAPS system showed that the system was not activated in flight. All of the on-site evidence correlated to a CAPS deployment due to impact forces. Additionally, the surviving passenger stated that she heard a discussion between the pilot and passenger seated in front. She stated that the front seated passenger had reached up for the CAPS handle, and the pilot said that "we were too low."

The aircraft was recovered and more detailed examinations of the airframe and engine were conducted in a secure hangar located at Kewanee Airport. The results of these examinations will be included in the final report.
Steven Mark Murray

Mark Haydn Murray



The National Transportation Safety Board traveled to the scene of this accident.

Additional Participating Entities:
Federal Aviation Administration / Flight Standards District Office; DuPage, Illinois
Continental Motors; Mobile, Alabama
Cirrus Aircraft; Duluth, Minnesota

Aviation Accident Factual Report - National Transportation Safety Board: https://app.ntsb.gov/pdf

Investigation Docket  - National Transportation Safety Board: https://dms.ntsb.gov/pubdms

http://registry.faa.gov/N765CD

NTSB Identification: CEN15FA388 
14 CFR Part 91: General Aviation
Accident occurred Sunday, August 30, 2015 in Kewanee, IL
Aircraft: CIRRUS DESIGN CORP SR22, registration: N765CD
Injuries: 2 Fatal, 1 Serious.

NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

HISTORY OF FLIGHT

On August 30, 2015, about 0918 central standard time, a Cirrus SR22 airplane, N765CD, was destroyed when it collided with terrain shortly after takeoff from Kewanee Municipal Airport (EZI), Kewanee, Illinois. The private pilot and one passenger were fatally injured; the second passenger sustained serious injuries. The airplane was privately owned, and the personal flight was operated under the provisions of 14 Code of Federal Regulations Part 91. Instrument meteorological conditions prevailed throughout the area, and an instrument flight rules (IFR) flight plan was filed for the cross-country flight, with an intended destination of Hot Springs, Arkansas.

A family member drove the pilot and passengers to EZI at 0745. During the short drive, the pilot discussed the fact that the airplane's autopilot had stopped working during the flight to EZI a few days before. The pilot thought that this would make the trip a little harder but that it was not a critical system preventing his departure. The pilot said that he initially planned to fly under the clouds then climb above the clouds to his desired cruise altitude of 11,000 ft. Upon arriving at the airport, the pilot decided to delay the flight due to the amount of fog in the area. The pilot and passengers subsequently returned to the airport about 0900 for departure. 

There were no witnesses to the accident and no distress calls were broadcast via radio. According to Flight Service, the pilot called before takeoff to file an IFR flight plan. He was given clearance to take off with a void time of ten minutes to activate the flight plan. The airport manager reported that the pilot taxied for takeoff on runway 27; however, the pilot's radio calls indicated that he thought he was using runway 19. After an aborted takeoff, the pilot completed a back-taxi on runway 27, but again his radio calls were for runway 19. The airplane subsequently departed runway 27. 

The surviving passenger, who was seated in the left rear seat, stated that the aborted takeoff was due to an open door. After securing the door, the airplane subsequently departed. She stated that when the airplane took off, it went quickly into the clouds. She stated that it did not feel as if the airplane was "going up." She stated that she heard a discussion between the pilot and then passenger seated in the front seat: the front seat passenger had reached for the activation handle for the airframe parachute system, and the pilot stated that the airplane was "too low." She then saw the ground approaching, and the impact occurred.

According to radar data obtained from the Federal Aviation Administration (FAA) Quad City Terminal Radar Approach Control facility, identified targets corresponded with the accident airplane's assigned transponder code. Additionally, five subsequent primary targets were consistent with the track of the accident airplane. There were no other aircraft operating in the immediate vicinity. The radar data corresponding to the airplane's transponder code began at 0914:53 at a Mode C reported altitude of 1,500 ft after the airplane departed EZI. The target continued in a left turn to the west and south and climbed to an altitude of 1,800 ft before beginning a descent to 1,200 ft. That data ended, and the primary radar returns consistent with the accident airplane begin at 0915:37 and continued until the last associated target at 0916:35 and an altitude of 1,600 ft. EZI airport elevation was 858 ft. A flight path superimposed between the primary targets suggested that the pilot made three nearly 360° left turns in close succession before impacting the ground. See figure 1.



PERSONNEL INFORMATION

The pilot held a private pilot certificate with ratings for airplane single-engine land and instrument airplane. His most recent FAA third-class medical certificate was issued on August 14, 2014. Review of the pilot's logbooks indicated a total flight experience of 922 hours of which 37 hours were in the accident airplane make and model. The pilot completed a Cirrus Advanced Transitional Instrument Training Course in May 2015. The pilot had logged 130 hours of actual instrument flight experience and 94.1 hours of simulated instrument experience. In the 90 days before the accident, the pilot logged 3.1 hours simulated instrument experience and 4.8 hours actual instrument experience, all of which were in the accident airplane make and model. 

AIRCRAFT INFORMATION

The airplane's most recent annual inspection was completed on March 5, 2015, at a Hobbs meter time of 1,635.1 hours. On June 25, 2015, at a Hobbs time of 1,635.2 hours, a new Engine Data Management System was installed. The aircraft logbook included an entry stating that the Cirrus Airframe Parachute System (CAPS) was replaced on October 4, 2011, at a Hobbs time of 1,134.2 hours. At the time of the accident, the Hobbs time was 1,734.8 hours.

The co-owner of the airplane reported that he had flown the airplane 9 days before the accident. He reported that there were no problems with the aileron trim or the autopilot. He flew using GPS navigation and with the autopilot engaged for the entire flight. The 5.4-hour flight had 3 occupants onboard with 50 pounds of baggage. He also stated that he had talked to the accident pilot the morning before the accident. The pilot told him that the autopilot would hold altitude, but it would not hold the horizontal situation indicator (HSI) heading bug or the GPS. The pilot also told him that the trim on the sidestick was not working and that he could hold straight and level flight with a bit of right aileron. The co-owner and pilot agreed to have the trim looked at upon his return flight.

A family member reported that he and the pilot had flown the airplane on a local flight from EZI for about 15-20 minutes on the morning before the accident. He reported that the flight was normal and that they did not experience any problems.

METEOROLOGICAL INFORMATION

First responders reported foggy conditions and low cloud ceilings about the time of the accident. 

EZI listed no official weather reporting capability; however, an unofficial weather station was collocated at EZI and reported the following conditions at 0910: wind from 090° at 1 knot, temperature 18.9°C, dew point 18°C, relative humidity 99%, altimeter 30.11 inches of mercury (Hg). Visibility and sky conditions were not reported.

The closest reporting station to the accident site was from Galesburg Municipal Airport (GBG), Galesburg, Illinois, located 28 miles southwest of the accident site at an elevation of 764 ft. The airport had an Automated Weather Observation System (AWOS), which issued observations every 20 minutes. The 0915 observation included: calm wind, visibility 1 miles in mist, ceiling overcast at 200 ft, temperature and dew point 19°C, altimeter 30.09 inches of Hg. 

A review of the observations for the day indicated that IFR conditions were reported as early as 2215 the previous evening, with low ceilings and visibility in fog and mist continuing through the time of the accident, and clearing by 1115. A weather study was completed by a NTSB staff meteorologist and is referenced in the public docket to this report.

WRECKAGE AND IMPACT INFORMATION

Examinations of the airframe and engine were accomplished at the accident site and a secured hangar located at the Kewanee Airport.

The accident occurred in a planted soybean field, about 1.5 miles west of the Kewanee airport. The airplane impacted terrain in an approximate 45° nose-down, right-wing-low attitude on a heading of about 130-140°. The debris field extended to the east about 260 ft from the initial point of impact on a headings from 080 to 110°. The main wreckage came to rest on a heading about 190°.

An examination of the ground impact scars and debris path showed that the tip of the right wing struck the ground at the western end of the debris field. The scar from the right wing tip was the initial point of impact. Propeller cuts, dirt clumps, and an impact depression were noted in the soft soil about 38 to 45 ft from the initial impact point. The separated propeller was located at 55 ft, and the right cabin door was located at 65 ft. The tip of the right wing and aileron were at 67 ft. The upper engine cowling was at 72 ft and the lower engine cowling was at 78 ft. The CAPS enclosure cover was at 75 ft. The left cabin door was at 120 ft, the main wreckage was at 160 ft, and the engine was at 185 ft. The parachute was stretched out on a heading of 110° to about 240 ft. The CAPS D-Bag and rocket motor were at 260 ft.

Fuselage

The fuselage was mostly destroyed by impact forces. The lower forward fuselage was crushed up and aft. The firewall was separated from the fuselage and the upper engine cowling was separated from the fuselage. The right forward corner of the upper engine cowling was crushed aft about 25°. The lower left and right engine cowlings were fractured into several pieces. The forward fuselage was fractured and crushed aft. The spar cover was separated from the fuselage. Both front seats remained attached to the spar cover. The rear section of the cabin floor was separated from the fuselage and the rear seats remained attached to it.

Wing

The wing was mostly destroyed by impact forces, and the wing spar was fractured in multiple places. All upper and lower wing skins were separated from the wing spar. The left and right flaps were separated from the wing. The right aileron was separated from the wing, and the left aileron remained attached to the wing. Aileron control cable continuity was confirmed. The roll trim motor shaft was found fractured. The fractured end of the roll trim motor shaft remained attached to the roll trim cartridge. The roll trim cartridge remained attached to the left aileron actuation pulley. Two rub marks were located adjacent to the roll trim motor mounting location. One rub mark was on the roll trim motor access panel, and one rub mark was on the lower wing skin. It could not be determined when the rub marks occurred. The flap actuator was separated from the flap torque tube. The flap actuator shaft was located in a position extending approximately 2 inches, consistent with a "Flaps 50" position. 

Empennage/Stabilizers

The empennage was separated from the fuselage about 1 ft forward of the leading edge of the horizontal stabilizer. The rudder remained attached to the vertical stabilizer and rudder control cable continuity was confirmed. The right elevator remained attached to the horizontal stabilizer and the right elevator tip exhibited impact damage. The left elevator remained attached to the horizontal stabilizer and the left elevator tip was separated from the elevator. Elevator control cable continuity was confirmed. The pitch trim motor was in an approximate neutral position.

Landing Gear

The nose landing gear assembly was buckled aft under the engine. The nose landing gear upper weldment remained attached to the engine mount. The nose landing gear leg, tire and wheel assembly was separated from the nose landing gear upper weldment. Both the left and right main landing gear assemblies exhibited impact damage. Both main landing gear assemblies remained attached to the wing.

Doors

The right and left cabin doors were separated from the fuselage. Both door's upper and lower pins exhibited impact damage. The baggage door remained attached to the fuselage.

Cockpit 

The instrument panel exhibited impact damage and was separated into two sections. The center console exhibited impact damage. The center console was equipped with a Garmin GMA 340 Nav/Com, dual Garmin GNS 430's, S-TEC 55X autopilot, and a Garmin GTX 327 transponder. The ignition key remained in the ignition switch and the ignition switch was in the "Both" position. The bolster panel in front of the left crew seat was modified with a JPI Engine Data Management System. The instrument panel in front of the right crew seat was modified to accept a Garmin GPS map 696, which was installed.

The following settings, indications and switch positions were noted:

• Hobbs meter indicated 1,734.8 hours. • Altimeter's Kollsman window indicated a setting of 30.01. • Flap switch was in the flaps "100" position. • GPS #2 circuit breaker was in the "open" position. • Encoder/transponder circuit breaker was in the open position. • MFD circuit breaker was "zip-tied" in the "open" position. • Strobe and landing light switches were in the "on" position. • Strobe lights circuit breaker was in the "open" position. • Battery #2 circuit breaker was in the open position. • Battery #1, Alternator #1 and Alternator #2 master switches were in the "on" position. Seats and Restraints

Both front seats remained attached to the spar cover. First responders cut the left seat belt webbing to aid in the extraction of the left seat occupant. The separated left seat belt remained buckled together. The right seat belt was found unbuckled. The right seat belt webbing exhibited load damage. The right seat belt webbing was torn and partially pulled through the load bar. The left rear seat belt remained buckled together. The left rear seat belt webbing exhibited load damage and was crushed and gathered against the load bar.

Cirrus Airframe Parachute System (CAPS)

The forward section of the roof and the windscreen were separated from the fuselage. Impact damage was noted on the roof structure directly above and adjacent to the mounting location of the CAPS activation handle and holder. The CAPS activation handle was found out of the activation handle holder. The activation handle holder bracket was bent aft. Impact damage was noted on the activation handle and on the exposed activation cable. The CAPS safety pin was located on the ground under the main wreckage.

The CAPS was found deployed and the CAPS rocket motor propellant was expended. The CAPS rocket motor, rocket lanyards, incremental bridle, D-Bag, suspension lines, riser, rear harnesses and both front harnesses had been extracted from the airplane. The rear harness remained snubbed. Both reefing line cutters remained in place and both had been activated. The parachute was separated from the D-Bag and was found stretched out from the main wreckage on a heading about 110°. The slider was at the base of the canopy. Packing folds were present on the canopy.

The rocket motor, lanyards, incremental bridle and D-Bag were located approximately 20 ft beyond the end the parachute. The CAPS launch tube, rocket igniter, exhaust shield, and base remained attached to the bulkhead. The retention straps for the D-Bag remained in the enclosure compartment. The CAPS access panel (#CB7) exhibited impact transfer marks from the left front harness 3-point link. The CAPS enclosure cover was located approximately 20 ft south of the debris path at a point about 75 ft from the right wing tip ground scar. An impact transfer mark, consistent in size and dimension with the top of the CAPS rocket motor, was noted on the inside surface of the cover, on the "strike plate."

On-site observations of the CAPS system showed that the system was not activated in flight. All evidence correlated to a CAPS deployment as the result of impact forces. 

Engine 

The crankshaft propeller flange was fractured and remained attached to the propeller hub. All of the cylinders remained attached to the crankcase and exhibited impact damage. All damage observed was consistent with impact. The fractured crankshaft propeller flange and radii exhibited 45° shear lips and spiral cracking. The exhaust and induction systems exhibited impact damage.

Both magnetos remained attached to the engine. Rotation of the engine by hand through the accessory drive produced impulse coupling engagement from both magnetos. The magnetos produced spark on the top spark plug leads for cylinder Nos. 2, 4, 5 and 6. The ignition harness was severed at the magneto due to impact damage, which contributed to the lack of spark from the top leads of cylinder Nos. 1 and 3. The ignition harness exhibited impact and thermal damage, and some leads were found cut and severed. The top spark plugs exhibited light- and dark-colored combustion deposits and the electrodes exhibited normal wear. The bottom spark plugs were inspected using a lighted borescope and exhibited normal operating signatures.

The fuel pump remained attached to the engine and was removed. The drive coupling was intact and the pump turned freely by hand. The mixture control arm moved freely by hand from stop to stop. The fuel pump was disassembled with no anomalies noted. The fuel manifold valve was removed from the engine and disassembled. The screen was free of debris. A small amount of fuel was observed in the manifold valve cavity. The diaphragm and plunger were intact and the retaining nut was tight. The fuel injector lines exhibited impact damage. The fuel injector nozzles from all cylinders except cylinder No. 2 were removed and free of obstructions. The No. 1 cylinder fuel nozzle was slightly bent. The fuel nozzle for cylinder No. 2 could not be removed due to impact damage.

The throttle body remained attached to the engine and exhibited impact damage. The control arm moved freely by hand from stop to stop. 

The oil sump was crushed upward into the crankcase and breached. The oil pump was disassembled and the drive and driven gears showed no anomalies and were coated with oil. The oil pump cavity contained oil and exhibited no hard particle passage. The oil cooler remained attached to the engine and exhibited impact damage.

The cylinders exhibited impact damage to their respective fins and some valve covers. The top spark plugs were removed and the cylinders were examined with a lighted borescope. The combustion chambers contained light-colored combustion deposits. The engine was rotated by hand through the accessory drive, and thumb compression was obtained on all cylinders except cylinder No. 1. A second borescope inspection of cylinder No. 1 revealed dirt and debris from impact located around the exhaust valve seat, preventing full closure of the exhaust valve. The engine was rotated again and proper operation of the No. 1 cylinder valve was visually observed with the borescope. The starter was found in the debris field, fractured and free of the starter adaptor. 

Propeller Assembly

The three-blade propeller was separated from the engine and located in the wreckage debris field. The spinner exhibited rotational crushing. Two blades were relatively straight and displayed chordwise scratching. The third blade was bent aft approximately midway from the hub to the tip and exhibited chordwise scratches and nicks in the leading edge. Several propeller slash marks were noted in the debris field. The propeller governor remained attached and was removed for inspection. The control arm moved freely by hand from stop to stop. The drive rotated freely by hand and oil discharged from the governor. The governor's gasket screen was free of debris.

MEDICAL AND PATHOLOGICAL INFORMATION

The Henry County Coroner Office, Cambridge, Illinois, performed an autopsy of the pilot. The cause of death was listed as "Multiple Blunt Injuries."

Toxicological testing on specimens of the pilot was performed by the FAA Bioaeronautical Sciences Research Laboratory, Oklahoma City, Oklahoma. Testing for carbon monoxide, ethanol, and drugs were all negative.

TESTS AND RESEARCH

Recorded Data

The airplane was equipped with a Garmin 696 GPS MAP and a JPI EDM 900 Engine Monitoring System. The Garmin 696 was impact damaged and no data was extracted.

The JPI EDM 900 was viable and data were downloaded. The data extracted included 71 logs from June 26, 2015 through August 30, 2015. The log for the accident flight began at 09:12:38 CDT and ended at 09:14:43 CDT. Additionally, data from four previous flights were reviewed. All recorded logs showed normal engine operation.

NTSB Identification: CEN15FA388 
14 CFR Part 91: General Aviation
Accident occurred Sunday, August 30, 2015 in Kewanee, IL
Aircraft: CIRRUS DESIGN CORP SR22, registration: N765CD
Injuries: 2 Fatal, 1 Serious.

This is preliminary information, subject to change, and may contain errors. Any errors in this report will be corrected when the final report has been completed. NTSB investigators either traveled in support of this investigation or conducted a significant amount of investigative work without any travel, and used data obtained from various sources to prepare this aircraft accident report.

On August 30, 2015, about 0918 central standard time, a Cirrus SR22 airplane, N765CD, registered to private individuals, collided with terrain shortly after takeoff from the Kewanee Municipal Airport (EZI), Kewanee, Illinois. Of the three occupants, the private pilot and 1 passenger sustained fatal injuries and 1 passenger sustained serious injuries. The flight was being conducted under the provisions of Federal Code of Regulations Part 91. Instrument meteorological conditions prevailed throughout the area of the accident and an IFR flight plan was placed on file with a 10 minute void time prior to takeoff. The flight was originating from EZI with an intended destination of Hot Springs, Arkansas.

There were no direct witnesses to the accident and no distress calls were received. According to Flight Service, the pilot called prior to takeoff to file an IFR flight plan. He was given clearance to takeoff with a void time of ten minutes to activate the flight plan. Local residents reported foggy conditions and low cloud ceilings about the time of the accident. The surviving passenger who was seated in the rear seat reported that the airplane took off, went quickly into the clouds. She stated that it did not feel as if the airplane was "going up." She looked up, saw the ground approaching, and the impact occurred. 

The accident occurred in a planted soybean field, approximately 1.5 miles west of the Kewanee airport. The wreckage was located at a position approximately 0.5 miles west of the intersection of North 400th Avenue and East 2250th Street and approximately 250 feet south of the North 400th Avenue.

An examination of the main impact site and energy debris path revealed that the airplane impacted terrain in an approximate 45 degree nose down, right wing low attitude, on a heading of approximately 130 to 140 degrees. The debris field extended to the east approximately 260 feet from the initial point-of-impact on a heading from 080 degrees to 110 degrees. The main wreckage came to rest on a heading of approximately 190 degrees.

An examination of the impact scars and wreckage debris revealed that the right wing tip struck the terrain at the western end of the debris field. The right wing tip scar was the initial point-of-impact. All subsequent debris measurements are approximate from this point. Propeller cuts, dirt clumps and an impact depression were noted in the soft soil from 38 feet to 45 feet. The separated propeller was located at 55 feet. The right cabin door was located at 65 feet. The right wing tip and aileron was at 67 feet. The upper engine cowling was at 72 feet. The CAPS enclosure cover was at 75 feet. The lower engine cowling was at 78 feet. The left cabin door was at 120 feet. The main wreckage was at 160 feet. The engine was at 185 feet. The parachute was stretched out on a heading of 110 degrees to approximately 240 feet. The CAPS D-Bag and rocket motor was at 260 feet.

The forward section of the roof and the windshield were separated from the fuselage. Impact damage was noted on the roof structure directly above and adjacent to the mounting location of the CAPS activation handle and holder. The CAPS activation handle was found out of the activation handle holder. The activation handle holder bracket was bent aft. Impact damage was noted on the activation handle and on the exposed activation cable. CAPS safety pin was located on the ground under the main wreckage. 

The CAPS was found deployed and the CAPS rocket motor propellant was expended. The CAPS rocket motor, rocket lanyards, incremental bridal, D-Bag, suspension lines, riser, rear harnesses and both front harnesses had been extracted from the aircraft. The rear harness remained snubbed. Both reefing line cutters remained in place and both had been activated. The parachute was separated from the D-Bag and was found stretched out from the main wreckage on a heading of approximately 110 degrees. The slider was at the base of the canopy. Packing folds were present on the canopy. 

The rocket motor, lanyards, incremental bridal and D-Bag were located approximately 20 feet beyond the end of stretched out parachute. The CAPS launch tube, rocket igniter, exhaust shield, and base, remained attached to FS 222 Bulkhead. The retention straps for the D-Bag remained in the enclosure compartment. The CAPS access panel (#CB7) exhibited Impact transfer marks from the left front harnesses 3-point link. The CAPS enclosure cover was located approximately 20 feet south of the debris path at a point approximately 75 feet from the right wing tip ground scar. An impact transfer mark, consistent in size and dimension to the top of the CAPS rocker motor, was noted on the inside surface of the cover, on the "strike plate." 

On site observations of the CAPS system showed that the system was not activated in flight. All of the on-site evidence correlated to a CAPS deployment due to impact forces. Additionally, the surviving passenger stated that she heard a discussion between the pilot and passenger seated in front. She stated that the front seated passenger had reached up for the CAPS handle, and the pilot said that "we were too low."

The aircraft was recovered and more detailed examinations of the airframe and engine were conducted in a secure hanger located at Kewanee Airport. The results of these examinations will be included in the final report.

Any witnesses should email witness@ntsb.gov, and any friends and family who want to contact investigators about the accident should email assistance@ntsb.gov


TOULON — The victims of a plane crash west of Kewanee on Sunday had flown to the area to attend a family inurnment ceremony Saturday.

Local family members confirmed Monday that Steven Murray, 67, Houston, Texas, was the pilot of the small private aircraft that crashed after leaving the Kewanee Municipal Airport.

Murray, his son Mark Murray, 38, and daughter Samantha Murray, 40, had flown in last week to attend a family memorial service.

Steven and Mark Murray were pronounced dead at the scene of the crash on Sunday by Henry County Coroner David Johnson.

Samantha Murray was transported by ambulance to OSF St. Luke Medical Center in Kewanee before being transferred to OSF St. Francis Medical Center in Peoria.

She sustained a broken arm, cuts and bruises, and remains in stable condition.

Steven’s father, Dr. Haydn H. Murray of Bloomington, Ind., passed away in February. With local ties to the community, the family held the inurnment ceremony for Murray in Elmira Cemetery.

Murray was born in Kewanee and married his high school sweetheart, Juanita Appenheimer. He became a world-renowned geologist and was a longtime professor of geology at Indiana University.

Steven and his children attended the service Saturday and visited relatives in the Toulon area before leaving for home Sunday morning.

Steven is the nephew of Dorothy Schmidt and a second cousin to Doug Murray, both of Toulon.

The plane crashed around 9:35 a.m. in a soybean field 2 miles west of the airport on Galva Township Road 400N. A nearby farmer heard the crash and called authorities.

Responding were the Henry County Sheriff’s Department, District 7 Illinois State Police, Galva police, Bishop Hill and Galva fire departments, Illinois Emergency Management Agency and the Stark County Ambulance Service.

Rural roads in the vicinity were closed to traffic while the crash was being investigated Sunday.

The crash is under investigation by the National Transportation Safety Board and the Federal Aviation Administration.

http://www.galesburg.com 

     

UPDATE: A woman is now listed in fair condition after a deadly plane crash. It happened Sunday morning in a field outside of the Kewanee Municipal Airport in Henry County. 

Steven Murray and Mark Murray, a father and son, were pronounced dead at the scene. Another family member Samantha Murray, 40, was taken to OSF Saint Francis Medical Center with an arm injury, cuts and bruises. Samantha Murray’s 41st birthday is reportedly September 1st.

The National Transportation Safety Board is wrapping up its investigation Monday into why the small plane crashed. An autopsy on Steven and Mark Murray is scheduled for Tuesday in Peoria.

ORIGINAL:  Two men are dead and a woman is in the hospital Sunday after a plane crash.

Police say it happened just before 10 o'clock Sunday morning.

A small plane crashed in a field outside the Kewanee municipal airport in Kewanee, Illinois.

The Murrays were in town for a family gathering when something went terribly wrong.

"They were leaving this morning from the Kewanee airport and they were going to go back to Texas," said David A. Johnson, Henry County Coroner.

Johnson said when he arrived on scene 67-year-old Steven Murray and 38-year-old Mark Murray, a father and son, were pronounced dead at the scene.

Another family member, 30-year-old Samantha Murray was taken to an area hospital with an arm injury, cuts and bruises, but later airlifted to a hospital in Peoria. Her condition is unknown at this time.

Authorities on scene say that North 40th avenue, where the crash happened will remain closed, as the National Transportation Safety Board completes their investigation Monday morning.

Then the aircraft will be taken to a secure location, where they will look further into what caused the crash.

“It's really no different than a larger aircraft it's just on a smaller scale so they do the same procedures to figure out what the cause is and what caused the aircraft to go down,” Keenan Campbell, Director of Bureau County Emergency Management.

On Tuesday morning, an autopsy will be conducted for Mark and Steven Murray in Peoria.

A father and son from Houston, Texas, were killed Sunday in a plane crash west of the Kewanee Municipal Airport.

The crash of a Cirrus SR22 aircraft occurred at 9:30 a.m. Sunday. Steven Murray, 67, and his 38-year-old son, Mark Murray, were pronounced dead at 12:45 p.m. by Henry County Coroner David A. Johnson.


Another passenger, Samantha Murray, 40, who is believed to be Steven Murray's daughter, was taken to Kewanee Hospital for treatment, and then airlifted to OSF St. Francis Medical Center in Peoria, Mr. Johnson said. The group was visiting the area for a family gathering and took off from the Kewanee airport Sunday morning to head back to Texas, he said.


The Bishop Hill Fire Department and Illinois State Police responded to the crash, as well as a representative from the Federal Aviation Administration from Chicago. The FAA and National Transportation Safety Board will lead the investigation, Mr. Johnson said.


Original article can be found here: http://www.qconline.com




Kewanee: Two Texas residents were killed when a small plane crashed in rural Kewanee Sunday morning.

Emergency crews were dispatched to the scene shortly after 9:30 a.m. when a local resident reported the accident.

Pronounced dead at the scene at 12:45 p.m. Sunday by Henry County Coroner David Johnson were Steven Murray, 67, and his son Mark Murray, 38, both of Houston, Texas.

A third victim, Samantha Murray, 40, was transported by ambulance to Kewanee’s OSF St. Luke Medical Center and then air-flighted to a Peoria hospital.

Johnson said Samantha Murray, also of Houston, sustained injuries to an arm.

The plane’s wreckage was in a soybean field two miles west of Kewanee Municipal Airport on 400N.  

Johnson said the three victims had been in this area for a family gathering over the weekend and were returning home.

The plane had left from the Kewanee airport prior to the accident.

Illinois State Police Officer Steve Icenogle said a nearby farmer heard the crash and saw a cloud of smoke. He found the downed plane and called authorities.

Responding were the Henry County Sheriff’s Department, District 7 Illinois State Police, Bishop Hill and Galva fire departments, Illinois Emergency Management Agency and the Stark County Ambulance Service.

Federal Aviation Administration (FAA) officials from Chicago were expect to arrive later in the afternoon to assist with the investigation, as were representatives of the National Transportation Safety Board in Colorado, who were due to arrive late Sunday night.

Emergency personnel remained at the scene throughout the day and closed the area off to local traffic.  

Source: http://www.starcourier.com



HENRY COUNTY, Ill. (KWQC) – Two men from Texas were killed and another woman, also from Texas, was injured when their small plane crashed this morning between Bishop Hill and the Kewanee Airport at North 400 Avenue and East 2350 Street. 

According to Henry County Coroner, David Johnson, the crash happened before 9:30 a.m., Sunday, August 30, 2015. Johnson arrived on scene around 12:30 p.m where he said 67-year-old, Steven Murray and 38-year-old, Mark Murray were pronounced dead at 12:45 p.m. Johnson said he believed the two were a father-son pair from Houston, Texas.

The third passenger, 40-year-old Samantha Murray was also from Houston, Texas, Johnson said. She was taken to a hospital in Peoria and is being treated for an arm injury.

Johnson said they had been in the area for a family gathering, and just taken off from the Kewanee Airport to return home when the crash happened.

The Federal Aviation Administration from Chicago is on the scene along with the Bishop Hill Fire Department and the Illinois State Police. Johnson said the National Transportation Safety Board is also expected to arrive from Colorado tomorrow to assist with the investigation.

Crews are asking for people to stay clear of the area as it is being investigated.

Original article can be found here:  http://kwqc.com