A packed holiday jet made an emergency landing after a series of
errors by the pilot who was stressed about being demoted, a report has
revealed.
The Thomas Cook plane with 235 passengers and seven crew
on board touched down with critically low fuel levels, according to an
inquiry.
It was due to land at Newcastle but diverted to Manchester, which has a longer runway, after a fault with the wing flaps.
The switch meant the plane would be in the air for about 20 minutes more than planned – burning more fuel.
The
Boeing 757 pilot could have gone to Edinburgh – which was closer – or
headed back to Newcastle once the flap problem was fixed, the report
said.
Instead, he continued to Manchester and eventually landed
with just 900kg of fuel left. The jet should have had 1,627kg of “final
reserve”.
The Air Accidents Investigation Branch said the “low and imbalanced fuel state … could have had serious implications”.
Experts
said that at the time, the pilot was worried about being reduced in
rank and taking a pay cut, and “sensed that the airline was in turmoil
due to a major internal re-organization program”.
A report said:
“The direct effect for him was that he had been told that he would be
one of several captains who would be demoted to first officer … and that
his salary would reduce significantly."
The drama unfolded as the plane was returning to Newcastle from
Fuerteventura when it was ordered to “go-around” and make another
approach to the runway.
A problem with the wing flap persuaded the
crew to divert to a longer runway, but while flying to Manchester they
made a series of mid-air errors, failed to carry out basic checks and
ignored standard practices.
Neither the 56-year-old pilot nor his co-pilot had flown low on fuel before – and the captain told investigators “the situation had felt unreal and that it seemed to get out of control very easily”.
The
crew could not even correctly declare a Mayday, as they should have “as
soon as it became evident that the aircraft was going to land with less
than final reserve fuel”, the report said.
The AAIB investigation into last August’s “serious incident” found “fuel caution messages were overlooked”.
A
Thomas Cook spokesman said: “As a result of the AAIB’s and our own
internal investigation, we have completely reviewed pilot training for
go-around manoeuvres to ensure operating procedures are accurately
followed and when necessary low fuel levels are appropriately declared
to air traffic control.
“At the time of the incident, proposed
demotions were entirely due to the requirement to balance our number of
captains and manage our costs in light of a significant surplus.
“Due
to the subsequent review of our fleet and new aircraft and routes, we
have now been able to reverse almost all of the demotions ahead of
2015.”
- Source: http://www.mirror.co.uk
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